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{{#Wiki_filter:ADAMS Accession Number:  ML19087A148 Part B Items (Onsite) - NRC information Requests (March 27, 2019) - ISI Byron U 2  1) ITEM B.1 - requested documents for the following selected weld activities
{{#Wiki_filter:Part B Items (Onsite) - NRC information Requests (March 27, 2019) - ISI Byron U2
A. Welding activity completed during prior outage.
: 1) ITEM B.1 - requested documents for the following selected weld activities:
Work Order Code Class Description 01952003-01     2 (2CV8351) Install Additional Isolation Valve downstream of 2CV8350 per EC040564 B. Welding activity scheduled to occur during the current outage.
A. Welding activity completed during prior outage.
Work Order Code Class Description 01380459-01 2 2SIJ7A, CM 2SIJ7A
Work Order       Code Class                   Description 01952003-01       2                             (2CV8351) Install Additional Isolation Valve downstream of 2CV8350 per EC040564 B. Welding activity scheduled to occur during the current outage.
-3/4"- Fab/Install SI Vent in 2A Suction per EC 381903
Work Order       Code Class                   Description 01380459-01       2                             2SIJ7A, CM 2SIJ7A-3/4"-
: 2) ITEM B.2 Documents  
Fab/Install SI Vent in 2A Suction per EC 381903
- ISI related corrective actions AR/IR Number Description/Topic 04097807 01/27/2018 CORROSION ON 2A DG JACKET WATER COOLER CHANNEL HEAD 0 4062274 2SI8905D - LOOP 4 HOT LEG SI CHK VL V  04137953 05/15/2018 CORROSION ON SX RISER VALVE PIPING 04058120 2RC8037C BODY/BONNET INACTIVE LEAK 04059080 BORIC ACID LEAK ON 2RC8037A 04059953 ACTIVE BORIC ACID LEAK ON 2SI051 04059979 ACTIVE BODY TO BONNET LEAK ON 2SI8905D 04064624 ACTIVE LEAK ON 2CV8368B 04085285 RCS LEAK RATE EXCEEDED ACTION LEVEL 3 04085629 U-2 RCS LEAK RATE DEVIATION ACTION LEVEL II 04087635  UNIT 2 RCS LEAK RATE CALCULATION EXCEEDED PARAMETERS 04090712 RCS LEAK RATE ACTION LEVEL 2 04121830 SX LEAK ON JACKET WATER COOLER DURING SX FLUSH 04209055 UNEXPECTED ALARM  
: 2) ITEM B.2 Documents - ISI related corrective actions AR/IR           Description/Topic Number 04097807       01/27/2018 CORROSION ON 2A DG JACKET WATER COOLER CHANNEL HEAD 04062274        2SI8905D - LOOP 4 HOT LEG SI CHK VLV 04137953       05/15/2018 CORROSION ON SX RISER VALVE PIPING 04058120       2RC8037C BODY/BONNET INACTIVE LEAK 04059080       BORIC ACID LEAK ON 2RC8037A 04059953       ACTIVE BORIC ACID LEAK ON 2SI051 04059979       ACTIVE BODY TO BONNET LEAK ON 2SI8905D 04064624       ACTIVE LEAK ON 2CV8368B 04085285       RCS LEAK RATE EXCEEDED ACTION LEVEL 3 04085629       U-2 RCS LEAK RATE DEVIATION ACTION LEVEL II UNIT 2 RCS LEAK RATE CALCULATION EXCEEDED 04087635 PARAMETERS 04090712       RCS LEAK RATE ACTION LEVEL 2 04121830       SX LEAK ON JACKET WATER COOLER DURING SX FLUSH UNEXPECTED ALARM - U-2 CONTAINMENT LEAK 04209055 DETECTION HIGH 04222319       RCS LEAK RATE EXCEEDED ACTION LEVEL 3 04230553       POTENTIAL INACTIVE LEAK ON 2SX03B LINE U2 LOOSE PARTS IMPACT NOISE MULTIPLE ALARMS 04155764 RECEIVED 01326215        BBS-10 Small Bore Class 1 Weld Actions 02704898       2SX035 Leak ADAMS Accession Number: ML19087A148
- U-2 CONTAINMENT LEAK DETECTION HIGH 04222319 RCS LEAK RATE EXCEEDED ACTION LEVEL 3 04230553 POTENTIAL INACTIVE LEAK ON 2SX03B LINE 04155764 U2 LOOSE PARTS IMPACT NOISE MULTIPLE ALARMS RECEIVED 0 1326215 BB S-10 Small Bore Class 1 Weld Actions 02704898 2SX035 - Leak
: 3) Item B.3- Documents for Components with Relevant Indications Component                     AR No or Letter     Supporting docs 10/12/2017 - NDE - LINEAR Provide a copy of       Detailed INDICATION OBSERVED            AR 04062252 with construction/fabrication DURING EXAM                    all corrective     drawing for affected action             component and associated assignments        piping drawing.
: 3) Item B.3- Documents for Components with Relevant Indications Component AR No or Letter Supporting docs 10/12/2017  
(CAs).              Nondestructive Exam report(s) and completed corrective actions for AR and site procedure with acceptance criteria that were applied for this issue.
- NDE - LINEAR INDICATION OBSERVED DURING EXAM Provide a copy of AR 04062252 with all corrective action assignment s (CA s). Detailed construction/fabrication drawing for affected component and associated piping drawing.
10/12/2017 B2R20 M4 NDE Provide a copy of          Detailed construction/
  - LINEAR INDICATION            AR 04062274 with fabrication drawing for OBSERVED DURING                all CAs.            affected component and EXAM                                              associated piping drawing.
Nondestructive Exam report(s) and completed corrective actions for AR and site procedure with acceptance criteria that were applied for this issue.
Nondestructive Exam report(s) and completed corrective actions for AR and site procedure with acceptance criteria that were applied for this issue.
10/12/2017 B2R20 M4 NDE
Unit 2 Containment Liner       Byron Letter dated Provide ARs and CAs Corrosion-                     January 18, 2018- associated with these liner Based on ultrasonic           BYRON 2018-        pits as described in your testing, the maximum metal 0002                    January 18, 2018 letter.
- LINEAR INDICATION OBSERVED DURING EXAM Provide a copy of AR 04062274 with all CAs. Detailed construction/
loss observed on the           Byron Station Unit Nondestructive Exam containment liner is 0.103   2 90-Day Inservice report(s) and site procedure at one location. This is the   Inspection Report  with acceptance criteria only location on the           for Interval 3,    applied to these degraded containment liner that has     Period 3 and        areas.
fabrication drawing for affected component and associated piping drawing.
reached 40% metal loss         Interval 4, Period from nominal thickness. The 1, (B2R20)            Applicable calculations that nominal plate thickness of                        support the evaluations of the containment liner                             each degraded areas as is 0.250 thick. The two pits                     described in your January identified in B2R20 are the                       18, 2018 letter.
Nondestructive Exam report(s) and completed corrective actions for AR and site procedure with acceptance criteria that were applied for this issue.
only locations for Unit-2 that exceed the ASME Code Section Xl Subsection IWE acceptance criteria of 10%.
Unit 2 Containment Liner Corrosion- "Based on ultrasonic testing, the maximum metal loss observed on the containment liner is 0.103" at one location. This is the only location on the containment liner that has reached 40% metal loss from nominal thickness. The nominal plate thickness of the containment liner is 0.250" thick. The two pits identified in B2R20 are the only locations for Unit
The pit at D2 Location 1 is 27.2% metal loss from nominal thickness and the pit at D2 Location 3, mentioned previously, resulted in 41.2% metal loss.
-2 that exceed the ASME Code Section Xl Subsection IWE acceptance criteria of 10%. The pit at D2 Location 1 is 27.2% metal loss from nominal thickness and the pit at D2 Location 3, mentioned previously, resulted in 41.2% metal loss. Byron Letter dated January 18, 2018
: 4) Item B.4- Updated Schedules - NDE and Welding Activities as identified in A.1 of Request Letter. Specifically, include the inspection priority items selected below and a current copy of the applicable procedures:
- BYRON 2018
Week of 4/8/19 (M- F) and Week of 4/15/19 (M - F) - NDE Activities UT, (Cat R-A, R1.11.3) 3 of 7 FW welds - (e.g. FW03DA-16/C15, 16, 19, 20, 21, 22 or 26). Procedure - EXE PDI-UT-1 Ultrasonic Examination of Ferritic Pipe Welds in Accordance with PDI-UT-1.
-0002 "Byron Station Unit 2 90-Day Inservice Inspection Report for Interval 3, Period 3 and Interval 4, Period 1, (B2R20)" Provide ARs and CAs associated with these liner pits as described in your January 18, 2018 letter. Nondestructive Exam report(s) and site procedure with acceptance criteria applied to these degraded areas. Applicable calculations that support the evaluation s of each degraded areas as described in your January 18, 2018 letter.
UT, (Cat B-B, Item B2.40) - SG - Stub Barrel Channel Head Weld - 2RC   BA/SGC-01. Procedure - EXE-ISI-210 - Manual Ultrasonic Examination of Vessel Welds.
: 4) Item B.4- Updated Schedules  
PT, (Cat C-B, Item C2.21) - Feedwater Nozzle Weld - 2RC-01-BA/SGN-02 Procedure - ER-AA-335-002 - liquid penetrant examinations.
- NDE and Welding Activities as identified in A.1 of Request Letter. Specifically, include the inspection priority items selected below and a current copy of the applicable procedures:
PT, (Cat C-C, Item C3.20) - Closure Plate 2AB-37 Weld - 2RH02AA-8/C47 Procedure ER-AA-335-002 - liquid penetrant examinations.
Week of 4/8/19 (M
Thursday- 4/11/19 Thermal Sleeve Wear Measurement/Examination- Work order and Procedure -
- F) and Week of 4/15/19 (M  
LCM 16-0002.
- F) - NDE Activities UT, (Cat R-A, R1.11.3) 3 of 7 FW welds - (e.g. FW03DA
Friday & Saturday & Monday 4/12, 13 & 15 of 2019 - BMV Examination Rx Head VE- BMV -2RC02R- Reactor Head Bare Metal visual examination -CC-729   Procedure - ER-AP-335-001 BARE METAL VISUAL EXAMINATION FOR NICKEL ALLOY MATERIALS, R6 04/15/19 - Monday (Note Sunday 4/14/19 at 1600 Start)
-16/C15, 16, 19, 20, 21, 22 or 26). Procedure  
Welding - WO 01380459 CM 2SIJ7A-3/4"- FAB/INSTALL SI VENT IN 2A SUCT PER EC 381903 and applicable welding procedures (e.g. 8-8-GTSM, or 1-1-GTSM PWHT.}}
- EXE PDI-UT-1 Ultrasonic Examination of Ferritic Pipe Welds in Accordance with PDI
-UT-1. UT, (Cat B-B, Item B2.40)  
- SG - Stub Barrel Channel Head Weld - 2RC-01-BA/SGC-01. Procedure  
- EXE-ISI-210 - Manual Ultrasonic Examination of Vessel Welds.
PT, (Cat C-B, Item C2.21)  
- Feedwater Nozzle Weld  
- 2RC-01-BA/SGN-02 Procedure - ER-AA-335-002 - liquid penetrant examinations
. PT, (Cat C-C, Item C3.20) - Closure Plate 2AB
-37 Weld - 2RH02AA-8/C47 Procedure ER
-AA-335-002 - liquid penetrant examinations
. Thursday- 4/11/19 Thermal Sleeve Wear Measurement/Examination
- Work order and Procedure  
- LCM 16-0002. Friday & Saturday & Monday 4/12, 13 & 15 of 2019 - BMV Examination Rx Head VE- BMV -2RC02R- Reactor Head Bare Metal visual examination  
-CC-729 Procedure - ER-AP-335-001 BARE METAL VISUAL EXAMINATION FOR NICKEL ALLOY MATERIALS, R6 04/15/19 - Monday (Note Sunday 4/14/19 at 1600 Start)
Weldi ng - WO 01380459 CM 2SIJ7A-3/4"- FAB/INSTALL SI VENT IN 2A SUCT PER EC 381903 and applicable welding procedures (e.g. 8-8-GTSM, or 1-1-GTSM PWHT.}}

Latest revision as of 23:23, 19 October 2019

E-Mailed Request for Information for Byron Station, Unit 2, on 03/27/19 (DRS-M.Holmberg)
ML19087A148
Person / Time
Site: Byron  Constellation icon.png
Issue date: 03/27/2019
From:
NRC/RGN-III
To:
References
Download: ML19087A148 (3)


Text

Part B Items (Onsite) - NRC information Requests (March 27, 2019) - ISI Byron U2

1) ITEM B.1 - requested documents for the following selected weld activities:

A. Welding activity completed during prior outage.

Work Order Code Class Description 01952003-01 2 (2CV8351) Install Additional Isolation Valve downstream of 2CV8350 per EC040564 B. Welding activity scheduled to occur during the current outage.

Work Order Code Class Description 01380459-01 2 2SIJ7A, CM 2SIJ7A-3/4"-

Fab/Install SI Vent in 2A Suction per EC 381903

2) ITEM B.2 Documents - ISI related corrective actions AR/IR Description/Topic Number 04097807 01/27/2018 CORROSION ON 2A DG JACKET WATER COOLER CHANNEL HEAD 04062274 2SI8905D - LOOP 4 HOT LEG SI CHK VLV 04137953 05/15/2018 CORROSION ON SX RISER VALVE PIPING 04058120 2RC8037C BODY/BONNET INACTIVE LEAK 04059080 BORIC ACID LEAK ON 2RC8037A 04059953 ACTIVE BORIC ACID LEAK ON 2SI051 04059979 ACTIVE BODY TO BONNET LEAK ON 2SI8905D 04064624 ACTIVE LEAK ON 2CV8368B 04085285 RCS LEAK RATE EXCEEDED ACTION LEVEL 3 04085629 U-2 RCS LEAK RATE DEVIATION ACTION LEVEL II UNIT 2 RCS LEAK RATE CALCULATION EXCEEDED 04087635 PARAMETERS 04090712 RCS LEAK RATE ACTION LEVEL 2 04121830 SX LEAK ON JACKET WATER COOLER DURING SX FLUSH UNEXPECTED ALARM - U-2 CONTAINMENT LEAK 04209055 DETECTION HIGH 04222319 RCS LEAK RATE EXCEEDED ACTION LEVEL 3 04230553 POTENTIAL INACTIVE LEAK ON 2SX03B LINE U2 LOOSE PARTS IMPACT NOISE MULTIPLE ALARMS 04155764 RECEIVED 01326215 BBS-10 Small Bore Class 1 Weld Actions 02704898 2SX035 Leak ADAMS Accession Number: ML19087A148
3) Item B.3- Documents for Components with Relevant Indications Component AR No or Letter Supporting docs 10/12/2017 - NDE - LINEAR Provide a copy of Detailed INDICATION OBSERVED AR 04062252 with construction/fabrication DURING EXAM all corrective drawing for affected action component and associated assignments piping drawing.

(CAs). Nondestructive Exam report(s) and completed corrective actions for AR and site procedure with acceptance criteria that were applied for this issue.

10/12/2017 B2R20 M4 NDE Provide a copy of Detailed construction/

- LINEAR INDICATION AR 04062274 with fabrication drawing for OBSERVED DURING all CAs. affected component and EXAM associated piping drawing.

Nondestructive Exam report(s) and completed corrective actions for AR and site procedure with acceptance criteria that were applied for this issue.

Unit 2 Containment Liner Byron Letter dated Provide ARs and CAs Corrosion- January 18, 2018- associated with these liner Based on ultrasonic BYRON 2018- pits as described in your testing, the maximum metal 0002 January 18, 2018 letter.

loss observed on the Byron Station Unit Nondestructive Exam containment liner is 0.103 2 90-Day Inservice report(s) and site procedure at one location. This is the Inspection Report with acceptance criteria only location on the for Interval 3, applied to these degraded containment liner that has Period 3 and areas.

reached 40% metal loss Interval 4, Period from nominal thickness. The 1, (B2R20) Applicable calculations that nominal plate thickness of support the evaluations of the containment liner each degraded areas as is 0.250 thick. The two pits described in your January identified in B2R20 are the 18, 2018 letter.

only locations for Unit-2 that exceed the ASME Code Section Xl Subsection IWE acceptance criteria of 10%.

The pit at D2 Location 1 is 27.2% metal loss from nominal thickness and the pit at D2 Location 3, mentioned previously, resulted in 41.2% metal loss.

4) Item B.4- Updated Schedules - NDE and Welding Activities as identified in A.1 of Request Letter. Specifically, include the inspection priority items selected below and a current copy of the applicable procedures:

Week of 4/8/19 (M- F) and Week of 4/15/19 (M - F) - NDE Activities UT, (Cat R-A, R1.11.3) 3 of 7 FW welds - (e.g. FW03DA-16/C15, 16, 19, 20, 21, 22 or 26). Procedure - EXE PDI-UT-1 Ultrasonic Examination of Ferritic Pipe Welds in Accordance with PDI-UT-1.

UT, (Cat B-B, Item B2.40) - SG - Stub Barrel Channel Head Weld - 2RC BA/SGC-01. Procedure - EXE-ISI-210 - Manual Ultrasonic Examination of Vessel Welds.

PT, (Cat C-B, Item C2.21) - Feedwater Nozzle Weld - 2RC-01-BA/SGN-02 Procedure - ER-AA-335-002 - liquid penetrant examinations.

PT, (Cat C-C, Item C3.20) - Closure Plate 2AB-37 Weld - 2RH02AA-8/C47 Procedure ER-AA-335-002 - liquid penetrant examinations.

Thursday- 4/11/19 Thermal Sleeve Wear Measurement/Examination- Work order and Procedure -

LCM 16-0002.

Friday & Saturday & Monday 4/12, 13 & 15 of 2019 - BMV Examination Rx Head VE- BMV -2RC02R- Reactor Head Bare Metal visual examination -CC-729 Procedure - ER-AP-335-001 BARE METAL VISUAL EXAMINATION FOR NICKEL ALLOY MATERIALS, R6 04/15/19 - Monday (Note Sunday 4/14/19 at 1600 Start)

Welding - WO 01380459 CM 2SIJ7A-3/4"- FAB/INSTALL SI VENT IN 2A SUCT PER EC 381903 and applicable welding procedures (e.g. 8-8-GTSM, or 1-1-GTSM PWHT.