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| issue date = 02/28/2014
| issue date = 02/28/2014
| title = NUREG/KM-0005 2002 Davis-Besse Reactor Pressure Vessel Head Degradation Knowledge Management Digest
| title = NUREG/KM-0005 2002 Davis-Besse Reactor Pressure Vessel Head Degradation Knowledge Management Digest
| author name = Iyengar R M
| author name = Iyengar R
| author affiliation = NRC/RES
| author affiliation = NRC/RES
| addressee name =  
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Revision as of 16:40, 21 June 2019

NUREG/KM-0005 2002 Davis-Besse Reactor Pressure Vessel Head Degradation Knowledge Management Digest
ML14038A119
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 02/28/2014
From: Raj Iyengar
Office of Nuclear Regulatory Research
To:
Beltz, G
References
NUREG/KM-0005
Download: ML14038A119 (24)


Text

2002 Davis-Besse Reactor Pressure Vessel Head Degradation

Knowledge Management Digest NUREG/KM-0005 February 2014

Table of Contents Introduction

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .1 Overview of the 2002 Event

. . . . . . . . . . . . . . . . . . . . . . . . . . .2 Lessons Learned from the 2002 Event

. . . . . . . . . . . . . . . . . . . . . .6NRC Actions Based on Lessons Learned

. . . . . . . . . . . . . . . . . . . . .8Timeline . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .10 Legal. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .12 The 2010 Event

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 14 Retrospectives

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .14

1 Introduction "Knowledge is power" - Sir Francis Bacon (1561-1626)

The U.S. Nuclear Regulatory Commission (NRC) has an active knowledge management program that captures important historical events and critical

information and preserves this knowledge for future generations

.The 2002 reactor pressure vessel (RPV) head incident at Davis-Besse Nuclear Power Station (DBNPS) in Oak Harbor, OH, was one of the most serious nuclear safety events in United States history

. In March 2002, severe degradation of the reactor pressure vessel head was discovered during a refueling outage at Davis-Besse. Boric acid had eaten away the carbon steel of the RPV head, leaving only

a thin layer of stainless steel cladding to withstand the full operating pressure

of the coolant in the reactor core

. This could have led to a rupture of the reactor

pressure vessel head and caused a major public safety event

.Eight years later, in 2010, Davis-Besse experienced another serious safety event involving the reactor pressure vessel head

. During an NRC-mandated inspection, plant staff found cracking of the control rod drive mechanism (CRDM) nozzles

. Had the plant staff not performed the inspection and found the cracking, the event

would have progressed and could have led to a situation similar to the 2002 event

.Fortunately, in both 2002 and 2010, the problems at the Davis-Besse were discovered before they caused a major public safety event

. These near-miss accidents have driven NRC policies and research to ensure the continued safe

This knowledge

management digest

and accompanying

DVD contain historical

documents relating to the

technical and regulatory aspects of these incidents

. Brian Sheron, Director of the

seminar on Davis-Besse.

2 These documents can be accessed on the DVD through the interactive timelines or directly through the document listings

.The DVD also includes a multimedia presentation of the special NRC seminar "2002 Davis-Besse Reactor Pressure Vessel Degradation" held in January 2013, which offers a retrospective view of the 2002 incident

. Overview of the 2002 Event

Background

The reactor pressure vessel heads of pressurized-water reactors (PWR) contain

penetrations for CRDM and instrumentation systems

. These penetrations are

made from nickel-based alloys (e

.g., Alloy 600) and related weld metals

. Primary coolant and the operating conditions of PWR plants have been known to cause cracking of the nickel-based alloys and weldments through a process called primary water-stress corrosion cracking (PWSCC)

. In response to the detection of PWSCC at several plants, the NRC issued NRC Bulletin 2001-01, "Circumferential Cracking of Reactor Pressure Vessel Head Penetration Nozzles," that requested information related to licensees' programs for inspection of vessel head penetration (VHP) nozzles

.Bulletin 2001-01 and Davis-Besse's responses can be found on the DVD (see the 2002 Regulatory Timeline or Events Leading Up in the documents section)

.Through-Wall Cracking Detected On February 16, 2002, in response to Bulletin 2001-01, the Davis-Besse Nuclear Power Station began a refueling outage with the intent to perform work that included remotely inspecting the VHP nozzles from underneath the head focusing on the CRDM

. The licensee found that three CRDM nozzles had indications of CRDM nozzles 1, 2, and 3, which are located near the top of the reactor pressure

2002 Regulatory Timeline or Events Leading Up in the documents section)

.Repair AttemptsThe licensee attempted to repair these VHP nozzles remotely by approaching from underneath the pressure vessel head

. On March 6, 2002, the licensee

terminated the repair process on CRDM nozzle 3 to determine the cause of

unusual equipment operation and removed the machining apparatus from the 3

4 nozzle. During the removal, the nozzle tipped in the downhill direction until it rested against an adjacent CRDM

. If the surrounding steel had been structurally

sound, it should have held the nozzle in position

.InvestigationThe licensee investigated the condition of the reactor pressure vessel head surrounding CRDM nozzle 3

. The investigation included removing the CRDM nozzle and removing large boric acid deposits from the top of the reactor pressure vessel head

. Upon completing the boric acid removal on March 8, 2002, the in the reactor pressure vessel head on the downhill side of CRDM nozzle 3

. The corrosion was caused by borated water that leaked from the reactor coolant system onto the vessel head through cracks in the nozzle and the weld that attached nozzle

3 to the reactor pressure vessel head

. The licensee discovered the remaining thickness of the reactor pressure vessel head in the wastage area to be about 9.5 mm (3/8 inch)

. This thickness consisted of only stainless steel cladding on the inside surface of the reactor pressure vessel head, which is nominally 9

.5 mm (3/8 inch) thick

. The stainless steel cladding is resistant to corrosion by boric acid, but it is not intended to provide structural integrity to the vessel

. Failure of the stainless steel cladding would have resulted in a loss-of-coolant accident (LOCA)

. The LOCA would have resulted in actuation of the plant's emergency systems

. Condition reports and technical reports can be found on the DVD (see the 2002 Technical Timeline or Davis-Besse Degradation in the documents section)

.NRC Actions remain shut down until the situation could be satisfactorily addressed and (2) invoked the process outlined in Inspection Manual Chapter 0350, "Oversight

and/or Operation Concern

." This process establishes guidelines for the oversight of licensee performance during the shutdown

. The process requires that the criteria ensure that the plant is operated in a manner that provides adequate found on the DVD (see the 2002 Regulatory Timeline or NRC Actions in the documents section)

.

5 6 Lessons Learned from the 2002 Event Operational Experience During the early 1990s, the NRC and industry recognized the potential for boric acid corrosion of a reactor pressure vessel head

. In 1993, the industry and NRC wastage stemming from undetected VHP nozzle leaks involving axial cracking caused by primary water-stress corrosion cracking (PWSCC)

. The industry

concluded and the NRC agreed that the likelihood of this happening was low

vessel head degradation could occur

. Nevertheless, in spite of this awareness and contrary to this conclusion, the 2002 Davis-Besse event happened

. A history of NRC publications regarding boric acid corrosion and primary water stress corrosion cracking can be found on the DVD (see the 2002 Regulatory Timeline

or Events Leading Up in the documents section)

.Lessons Learned Task ForceThe NRC's Executive Director for Operations (EDO) at the time, Dr

. William D. Travers, directed the formation of an NRC task force to respond to the 2002

Davis-Besse event

. The objective of this task force was to independently evaluate the NRC's regulatory processes related to assuring reactor pressure vessel head integrity to identify and recommend areas for improvement that may be

applicable to either the NRC or the nuclear industry

. Consistent with its charter,

Oversight Process issues, (2) regulatory process issues, (3) research activities, (4) international practices, and (5) the NRC's Generic Issues Program

.Task Force ConclusionsThe lessons learned task force concluded that the Davis-Besse VHP nozzle

leakage and reactor pressure vessel head degradation event was preventable

. Although this review was primarily introspective, this question could not be answered without considering industry activities and Davis-Besse's performance

. At Davis-Besse, early indications of reactor pressure vessel corrosion were

and the buildup of large amounts of boric acid deposits on the RPV head

. The task Besse, and the nuclear industry failed to adequately review, assess, and follow up on relevant operating experience; (2) Davis-Besse failed to ensure that plant 7safety issues received appropriate attention; and (3) the NRC failed to integrate known or available information into its assessments of Davis-Besse's safety

performance

. Moreover, an NRC investigation concluded that Davis-Besse did not adequately execute the boric acid corrosion control program in response to an NRC generic communication, and the NRC did not adequately review the industry implementation of long-term commitments such as the commitment to maintain a

boric acid corrosion control program

. The lessons learned task force report can be

found on the DVD (see NRC Actions in the documents section)

.

NRC ActionsAs a result of its review, the task force determined that the NRC should take (1) stress corrosion cracking, (2) reactor coolant pressure boundary integrity, (3) operational experience, and (4) inspection and program management

.

8NRC Actions Based on Lessons Learned The lessons learned task force developed recommendations in key technical and programmatic areas

. The following are examples of some of the actions taken by

the NRC to address the recommendations of the task force

.Stress Corrosion Cracking The agency issued NRC Order EA-03-009 requiring all licensees with plants

susceptible to reactor pressure vessel head degradation to visually inspect

the reactor vessel head surface area for indications of leakage and boric acid accumulation and to inspect head penetrations using methods to detect cracks before leakage starts

.The NRC worked with the American Society of Mechanical Engineers (ASME) to develop Code Case N-729-1 to incorporate long-term inspection requirements of reactor pressure vessel heads into the ASME Code

. The NRC will incorporate into Title 10 of the Code of Federal (10 CFR) 50

.55a, "Codes and Standards," and allow the rescission of NRC Order EA-03-009

.

Order EA-03-009 can be found on

the DVD (see the 2002 Regulatory Timeline or NRC Actions in the documents section)

.Left photo: Top view of the J-groove weld with an arrow pointing to a crack.

showing the leak path of the reactor coolant.

9 Operating Experience in Management Directive 8

.7, "Reactor Operating Experience Program,"

to systematically collect, communicate, and evaluate operating experience information, including foreign operating experience

. The program makes information available to internal users and members of the public through a single Web access page

.The NRC established an organization within the agency to act as a clearinghouse that collects, communicates, and evaluates operating experience and applies

the lessons learned to the core regulatory functions of oversight, licensing, rulemaking, and incident response

. It also conducts a daily screening meeting

at which incoming event reports and other operating experience items are reviewed. A recently established new operating experience information gateway consolidates a large collection of individual databases and web sources of

information onto a single web access page

. Through this gateway, all reported

events can be reviewed and managed

. To ensure plant experience is adequately considered in licensing decisions, the NRC established new or revised expectations with regard to the duration of

visits, communication with the resident inspector staff, and maintenance of a

questioning safety attitude about plant events

. Management Directive 8

.7 can be found on the DVD (see NRC Actions in the documents section)

.Inspection and Program ManagementThe staff made several changes to the process to enhance the NRC's ability to

Davis-Besse

. For example, the review of the event indicated the deteriorating condition had been underway for several years and that the planned inspection,

earlier discovery of the condition were frequently deferred

.The NRC increased the evaluation of licensees' programs and actions relating to longstanding unresolved problems

. In addition, the NRC now audits the licensees' commitment management programs every 3 years by assessing the adequacy of the licensees' implementation of a sample of commitments made to

the NRC in past licensing actions and activities

.The NRC inspector training program has been enhanced by a web-based system to provide more timely dissemination of information to the inspection staff and 10 a method for individual study

. New training modules were developed to address lessons learned from the 2002 Davis-Besse event, such as the effects of boric acid corrosion and the importance of maintaining a questioning attitude toward safety

.The agency determined that safety culture weaknesses at Davis-Besse were at

the root causes of the reactor vessel head degradation event

. Therefore, the NRC

to detect a weak safety culture in inspections and performance assessments

. In attitudes in organizations and individuals which establishes that, as an overriding priority, nuclear plant safety issues receive the attention warranted by their

of its oversight processes

.The NRC has enhanced program management aspects of the reactor oversight process. For example, the guidance for managing NRC resources devoted to plants in an extended shutdown as a result of performance issues was revised to ensure less impact on routine oversight at other plants

. Also, to ensure continuity

and established the criterion of maintaining a minimum of 90-percent coverage

.Timeline The timeline of the 2002 incident has been broken down into three sections, a

technical timeline that covers the technical aspects of the incident, a regulatory

timeline that covers NRC actions related to the incident, and a legal timeline that provides a summary of criminal and civil cases stemmed from this incident

. Interactive timelines with additional information and links to relevant documents

can be found on the DVD (see the 2002 Timeline

).Technical inspection in April 2000

. The plant removed buildup and made repairs

. The following year, the NRC issued Bulletin 2001-01 mandating licensees perform special inspections of CRDM nozzles and report results to the NRC

. Davis-Besse staff requested to delay the inspections until the next refueling outage scheduled

to take place in early 2002 to limit worker radiation dose

. The NRC approved

inspections would present a limited risk

.

11 The 13th refueling outage started on February 16, 2002

. In the subsequent weeks, the Davis-Besse staff performed multiple inspections

. Boron crystal buildup on the noticed in 2000 but in larger quantity

. Inspections of the CRDM nozzles found axial cracking in 5 nozzles and a 30-degree circumferential crack in one nozzle

. On March 7, 2002, during a repair attempt of CRDM nozzle 3, the repair equipment shifted unusually, prompting an examination of the reactor pressure vessel head

. Davis-Besse staff discovered extensive degradation of

plant's operation, including replacement of the reactor pressure vessel head;

implementation began in June 2002

.RegulatoryAs early as the 1980s, boric acid corrosion and primary water-stress corrosion cracking (PWSCC) were known phenomena and had been observed in commercial

U.S. reactors. The NRC had begun addressing these issues through regulations such as Generic Letter 88-05, "Boric Acid Corrosion of Carbon Steel Reactor Pressure Boundary Components in PWR Plants," which mandated that licensees

implement a program to address boric acid corrosion of carbon steel components

.

12In 2001, the NRC issued Bulletin 2001-01, "Circumferential Cracking of Reactor Pressure Vessel Head Penetration Nozzles", in response to circumferential

cracking discovered in CRDM nozzles at a U

.S. commercial reactor

. The bulletin required that licensees perform inspections on their CRDM nozzles to check for

cracking. Severe boric acid corrosion of the carbon steel reactor pressure vessel

head was uncovered during these inspections

. Following this discovery, the NRC

Davis-Besse until further notice

.Bulletin 2002-01 was issued on March 18, 2002, and it requested information from licensees regarding their vessel head inspection and maintenance programs to ensure they adequately protect against issues that would affect the reactor pressure

vessel head integrity

.In February 2004, about 2 years after the degradation was found, NRC Order EA-03-214 allowed the restart of the Davis-Besse Nuclear Power Station provided the licensee met certain conditions

. The order also required Davis-Besse to comply with additional requirements over the next 5 years including contracting with an outside organization to conduct annual comprehensive assessments of the

operations at the Davis-Besse Nuclear Power Station

. The licensee accepted these

terms. In 2009, the NRC acknowledged that the licensee had met all the conditions of the Order and it was no longer in effect

.Legal Davis-Besse Criminal SummaryOn January 19, 2006, The United States District Court for the Northern District

statements

.On January 20, 2006, FirstEnergy Nuclear Operating Company (FENOC), agreed to pay $28 million in penalties, restitution, and community service projects as

part of an agreement to defer criminal prosecution of the company

. Under this deferred prosecution agreement, FENOC admitted that the Government could prove that FENOC employees, acting on the company's behalf, knowingly by

making false representations to the NRC in the course of attempting to persuade the NRC that its Dave-Besse Nuclear Power Station was safe to operate beyond December 31, 2001

.

13 On October 30, 2007, a jury in the Northern District of Ohio found two of the three indictees, David Geisen and Andre Siemaszko, guilty of three counts each

of concealing a material fact and making false statements to the NRC

. However, the jury found the third indictee, Rodney Cook, not guilty of all charges against him. The court placed David Geisen on probation for a term of 3 years on

each of the 3 counts to be served concurrently with standard and additional

special assessment in the amount of $300

.00 against Mr

. Geisen. As for Andrew Siemaszko, the court placed him on probation for a term of 3 years on each count to run concurrently with standard and additional conditions as noted

. The court

$4500) and a special assessment in the amount of $300

.

Appeals for the 6th Circuit from the judgment entered against him

. Likewise, on

Court of Appeals for the 6th Circuit appealing the decision in district court

.

court's decision on both matters

.Davis-Besse Civil SummaryIn addition, to criminal charges against the company and individual employees, the NRC also pursued civil penalties against responsible parties

. Based upon an NRC investigation, the NRC found that four individuals engaged in deliberate civil misconduct in the Davis-Besse matter

. On April 21, 2005, the NRC issued an order to three of these four individuals (Andrew Siemaszko, Dale Miller, and Steven providing inaccurate and incomplete information to the NRC

. On January 4, 2006, the NRC issued an order a fourth individual, Mr

. Geisen, similarly imposing a 5 year ban against him

. In addition, the NRC issued "Notice of Violation and corrosion control and corrective action programs

.

administrative appeals of the NRC orders issued against them

. In the fall of

NRC. They agreed to take various actions that will serve both to deter others and encourage compliance with NRC regulations in the future

. In June 2009, Mr

. Siemaszko agreed to the 5 year ban

. With respect to Mr

. Geisen, after the conduct 14of an evidentiary hearing, the Atomic Safety and Licensing Board set aside the NRC's order on the basis that it had not been shown by a preponderance of

evidence that Mr

. Geisen acted knowingly regarding the falsity of the information Licensing Board's decision on appeal

.The 2010 Event On February 28, 2010, Davis-Besse operators shut down the reactor to

commence the 16th refueling outage

. As part of the outage, the licensee

conducted NRC-required inspections of the CRDM nozzles penetrating the reactor pressure vessel head

. The inspections included direct visual and ultrasonic testing examinations of 100 percent of the CRDM nozzles

. Small amounts of

boric acid buildup were found on the reactor pressure vessel head, but it was

determined that the boric acid had not compromised the structural integrity of the

evaluation, including ultrasonic testing, in 24 nozzles

. although its onset was unusually rapid since the head had been replaced following the 2002 incident

. This early onset of PWSCC is largely attributed to the vessel head temperature being slightly higher than expected during the most

recent operating cycle

. It was determined that poor material microstructure was

also likely a factor in the quickened pace of PWSCC onset

.The NRC commissioned a Special Inspection Team (SIT) to independently assess concluded that licensee actions met NRC requirements and that the vessel head was in a suitable condition to return to service; however, the NRC also decided that licensee had to replace the head again in 2011

. The SIT report can be found on the DVD (see NRC Actions in the documents section)

.Retrospectives In 2013, the NRC held a special seminar titled, "2002 Davis-Besse Reactor Pressure Vessel Head Degradation-A Retrospective View of the Event, the

Actions that Followed, and the Lessons Learned

." The seminar featured several presentations including a regulatory perspective from Jim Dyer, former Regional former NRC Chairman, Dr

. Richard A

. Meserve, and lessons learned from

15 Dr. Brian Sheron, Director of the Nuclear Regulatory Research. A full agenda of the

seminar as well

as video and

slides from all the presentations are available on the

DVD included with

this brochure

.

16 DVDTo help navigate the DVD, the outline below provides topics and headings that the user can access directly from the interactive window

.Important Note:

Many of the documents on the DVD are historical in nature and may contain information that is obsolete or superseded by today's regula

-tions and research

. Please refer to the NRC's public Web site (www

.nrc.gov) for current information on regulations, Commission policy statements, regulatory

guidelines, regulatory processes, and research results

.Main DVD 2002 Event PWSCC

Agenda Part 1 Part 2

2002 Event 2010 Event Tech Reports 17 2002 Davis-Besse Reactor Pressure Vessel Head Degradation Knowledge Management DigestPrepared By:

Jack Riley Brian McGrattan Raj Mohan Iyengar Sabrina Allen Jeanne Dion Joshua Kusnick Don Marksberry Felix E. Gonzalez Jay CollinsMel Holmberg Catherine Scott Aladar Csontos Mark Henry SalleyThis DVD was developed using Visual Basic Express 2010

. Make sure you have Windows XP or newer and Visual Basic Framework 3

.5 for the DVD to work correctly

.

NUREG/KM-0005 February 2014