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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217H6231999-10-18018 October 1999 Discusses Completion of Licensing Action for GL 98-01 & Suppl 1, Yr 2000 Readiness of Computer Sys at Npps, to All Holders of Operating Licenses for NPPs ML20217J4331999-10-15015 October 1999 Forwards Insp Rept 50-461/99-19 on 990913-17.One Violation Re Individual Failure to Follow Radiation Protection Procedures When Accessing High Radiation Area Noted & Being Treated as Noncited Violation U-603280, Forwards Rev 27 to Clinton Power Station Physical Security Plan,Iaw 10CFR50.54(p).Encl Withheld from Public Disclosure, Per 10CFR50.54(p)1999-10-12012 October 1999 Forwards Rev 27 to Clinton Power Station Physical Security Plan,Iaw 10CFR50.54(p).Encl Withheld from Public Disclosure, Per 10CFR50.54(p) ML20217C0871999-10-11011 October 1999 Forwards Proprietary Attachment Inadvertently Omitted from Encl 2 to Submitting Responses to NRC RAI Re License Transfer Application for Plant.Proprietary Encl Withheld U-603276, Forwards Rev 8 to CPS USAR, Which Includes Changes from 970701 Through 990630 & Available Changes Approved After 990630 That Reduce Overall Burden of Submittal Changes for Forthcoming Reporting period.10CFR50.59 Rept Included1999-10-0808 October 1999 Forwards Rev 8 to CPS USAR, Which Includes Changes from 970701 Through 990630 & Available Changes Approved After 990630 That Reduce Overall Burden of Submittal Changes for Forthcoming Reporting period.10CFR50.59 Rept Included U-603279, Forwards non-proprietary & Proprietary Responses to NRC RAI Re License Transfer Application for Plant.Attached Responses Also Respond to Comments of Environ Law & Policy Center Dtd 990920.Proprietary Encl Withheld1999-10-0707 October 1999 Forwards non-proprietary & Proprietary Responses to NRC RAI Re License Transfer Application for Plant.Attached Responses Also Respond to Comments of Environ Law & Policy Center Dtd 990920.Proprietary Encl Withheld U-603275, Provides Updated Illinois Power Rept on Status of Decommissioning Funding for Clinton Power Station1999-10-0707 October 1999 Provides Updated Illinois Power Rept on Status of Decommissioning Funding for Clinton Power Station ML20217A9881999-10-0101 October 1999 Advises of NRC Plans for Future Insp Activities at Facility for Licensee to Have Opportunity to Prepare for Insps & to Provide NRC with Feedback on Any Planned Insps Which May Conflict with Plant Activities ML20217A7361999-10-0101 October 1999 Forwards Insp Repts 50-461/99-14 & 50-461/98-12 on 990729-0908.Two Violations Identified,One Re Failure to Place Control Switch in Proper Position to Identify Piece of out-of-svc Equipment & Being Treated as NCVs ML20217J1251999-09-30030 September 1999 Refers to Investigation 3-1997-040 Conducted from 971028- 980921 & Forwards Nov.Investigations Determined That During Jan 1997,supervisor Qv Dept Discriminated Against Qv Inspector in Retaliation for Inspector Contacts with NRC ML20217J1421999-09-30030 September 1999 Refers to Investigation 3-97-040 Conducted from 971028- 980921 & Forwards Nov.Investigation Concluded That Recipient Engaged in Deliberate Misconduct in That Recipient Discriminated Againt Qv Inspector for Having Contacted NRC ML20212G6751999-09-22022 September 1999 Forwards Comment Submitted to NRC by Environ Law & Policy Ctr Re Proposed License Transfer for Clinton Power Station U-603272, Provides Update to Final Response to GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants. 3-D Monicore & Station Security Sys remediated.Y2K Readiness Disclosure for Cps,Encl1999-09-22022 September 1999 Provides Update to Final Response to GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants. 3-D Monicore & Station Security Sys remediated.Y2K Readiness Disclosure for Cps,Encl U-603225, Provides Closure of Util Commitments Re Ci Cv Noted in Previous Ltr to Nrc.Basis for Expecting Valves to Remain in leak-tight Condition Throughout Operating Cycle & Basis That Justifies Not Performing mid-cycle Leak Testing,Encl1999-09-20020 September 1999 Provides Closure of Util Commitments Re Ci Cv Noted in Previous Ltr to Nrc.Basis for Expecting Valves to Remain in leak-tight Condition Throughout Operating Cycle & Basis That Justifies Not Performing mid-cycle Leak Testing,Encl ML20212G6981999-09-20020 September 1999 Requests That NRC Reject Proposed License Transfer for Clinton Power Station & That NRC State That Public Interest in Safe Nuclear Power Industry Will Not Be Subordinated to Interest in Maximizing Profit by Limiting Liability ML20217H3421999-09-17017 September 1999 Forwards Request for Addl Info Re Licensee 990723 Application for License Transfer & Conforming Administrative License Amend.Response Requested within 20 Days of Receipt of Ltr 05000461/LER-1996-010, Forwards LER 96-010-01, Plant Shutdown Due to Unidentified RCS Leakage from Degraded Reactor Recirculation Pump Seal Greater than TS Limit. Revised Rept Includes Cause of Event,Corrective Actions & Discussion of Similar Events1999-09-13013 September 1999 Forwards LER 96-010-01, Plant Shutdown Due to Unidentified RCS Leakage from Degraded Reactor Recirculation Pump Seal Greater than TS Limit. Revised Rept Includes Cause of Event,Corrective Actions & Discussion of Similar Events 05000461/LER-1999-011, Forwards LER 99-011-00 Re Improper Restoration of a APRM Which Caused Monitor to Not Meet Seismic Qualification Requirements.Rept Contains Listed Commitments1999-09-10010 September 1999 Forwards LER 99-011-00 Re Improper Restoration of a APRM Which Caused Monitor to Not Meet Seismic Qualification Requirements.Rept Contains Listed Commitments U-603269, Certifies That DB Livingston,License OP-31136,successfully Completed Facility Licensees Requirements to Be Licensed as Ro,Per 10CFR55 & Has Need for RO License to Perform Assigned Duties.Five Significant Control Manipulations,Listed1999-09-10010 September 1999 Certifies That DB Livingston,License OP-31136,successfully Completed Facility Licensees Requirements to Be Licensed as Ro,Per 10CFR55 & Has Need for RO License to Perform Assigned Duties.Five Significant Control Manipulations,Listed ML20211Q2671999-09-0808 September 1999 Informs That NRC Tentatively re-scheduled Initial Licensing Exams for License Operator License Applicants During Weeks of June 5 & 12,2000.Validation of Exams Will Occur at Station During Weeks of May 15,2000 U-603229, Provides Response to NRC RAI Re GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, Dtd 990528.Rev 0 to Calculation IP-M-0556 & Rev 0 to Calculation IP-M-0570,encl1999-08-25025 August 1999 Provides Response to NRC RAI Re GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, Dtd 990528.Rev 0 to Calculation IP-M-0556 & Rev 0 to Calculation IP-M-0570,encl U-603243, Forwards Response to NRC GL 99-02, Lab Testing of Nuclear-Grade Activated Charcoal. Util Performing Testing of ESF Ventilation Sys Charcoal Samples Using ASTM D3803- 1989 Methodology as Required by TS 5.5.71999-08-23023 August 1999 Forwards Response to NRC GL 99-02, Lab Testing of Nuclear-Grade Activated Charcoal. Util Performing Testing of ESF Ventilation Sys Charcoal Samples Using ASTM D3803- 1989 Methodology as Required by TS 5.5.7 ML20211D2201999-08-23023 August 1999 Confirms 990817 Telcon with J Neuschwanger & D Mcneil Re Arrangements Made for NRC to Inspect Licensed Operator Requalification Program at Plant U-603258, Forwards ISI Summary Rept, IAW ASME Section Xi,Article IWA-6000.Summary Rept Addresses ISI Activities Performed at Plant from 950429-990527,including Extended Sixth Refueling Outage1999-08-23023 August 1999 Forwards ISI Summary Rept, IAW ASME Section Xi,Article IWA-6000.Summary Rept Addresses ISI Activities Performed at Plant from 950429-990527,including Extended Sixth Refueling Outage ML20211B0871999-08-20020 August 1999 Responds to J Hopkins Inquiry Re Application for Order Consenting to License Transfer & Approving Conforming Administrative License Amend Filed by Ilpr & Amergen Energy Co on 990723 U-603259, Provides Notification That Cl Kreidler Has Resigned Position with Util,Effective 990818.License Status Should Be Changed to Expired1999-08-19019 August 1999 Provides Notification That Cl Kreidler Has Resigned Position with Util,Effective 990818.License Status Should Be Changed to Expired ML20211A8931999-08-19019 August 1999 Forwards Insp Rept 50-461/99-13 on 990611-0728.Two Violations Noted & Being Treated as Ncvs.Violation Re Three Examples Where Licensee Procedural Requirements for Minor Maint Work Were Not Followed U-603253, Notifies NRC That Je Smith,License SOP-30819-1,has Resigned from Position with Ilpr Effective 990813.Status of License Should Be Changed to Expired,Effective 9908131999-08-16016 August 1999 Notifies NRC That Je Smith,License SOP-30819-1,has Resigned from Position with Ilpr Effective 990813.Status of License Should Be Changed to Expired,Effective 990813 ML20210U3771999-08-12012 August 1999 Forwards Notice of Consideration of Approval of Transfer of FOL & Issuance of Conforming Amend & Opportunity for Hearing Re Amend Request for Approval of Clinton Power Station License NPF-62 Transfer to Amergen U-603250, Notifies NRC That Ma Freihofer (License SOP-31296-1) Has Resigned from Position with Illinois Power Effective 990729 & License Status Should Be Changed to Expired Effective 9907291999-08-10010 August 1999 Notifies NRC That Ma Freihofer (License SOP-31296-1) Has Resigned from Position with Illinois Power Effective 990729 & License Status Should Be Changed to Expired Effective 990729 U-603249, Notifies NRC That He Bouska (License SOP-3055-1) Has Resigned from Position with Illnois Power Effective 990809. & License Status Should Be Changed to Expired Effective 9908091999-08-10010 August 1999 Notifies NRC That He Bouska (License SOP-3055-1) Has Resigned from Position with Illnois Power Effective 990809. & License Status Should Be Changed to Expired Effective 990809 ML20210N2961999-08-0909 August 1999 Forwards Form of Nuclear Decommissioning Master Trust Agreement,Per CPS Application for License Transfer & Conforming Administrative License Amend U-603248, Requests Unrestricted License for Kc Scott,License SOP-31532.Scott Has Successfully Completed Facility Licensee Requirements to Be Licensed as Operator/Senior Operator Per 10CFR551999-08-0606 August 1999 Requests Unrestricted License for Kc Scott,License SOP-31532.Scott Has Successfully Completed Facility Licensee Requirements to Be Licensed as Operator/Senior Operator Per 10CFR55 U-603236, Forwards Revised Data Point Ref File Sheets for Clinton Power Station Computer Points That Input to ERDS1999-08-0202 August 1999 Forwards Revised Data Point Ref File Sheets for Clinton Power Station Computer Points That Input to ERDS ML20210J0541999-07-30030 July 1999 Forwards Three Original Signature Pages of Gr Rainey for Application for License Transfer & Conforming Administrative License Amend, for NRC Files U-603178, Forwards Four ASME Section XI Relief Requests Re Performance of non-destructive Exams for First 120-month Inservice Insp for CPS1999-07-29029 July 1999 Forwards Four ASME Section XI Relief Requests Re Performance of non-destructive Exams for First 120-month Inservice Insp for CPS U-603237, Informs That Util Will Provide Response to fire-related Questions One & Two of NRC RAI Re CPS Ipeee,By 0001311999-07-28028 July 1999 Informs That Util Will Provide Response to fire-related Questions One & Two of NRC RAI Re CPS Ipeee,By 000131 U-603240, Forwards Clinton Power Station semi-annual Fitness for Duty Rept for Period Ending 990630,IAW 10CFR26.711999-07-27027 July 1999 Forwards Clinton Power Station semi-annual Fitness for Duty Rept for Period Ending 990630,IAW 10CFR26.71 U-603235, Forwards Application for License Transfer & Conforming Administrative License Amend for OL NPF-62.Proprietary & Nonproprietary Asset Purchase Agreement Encl.Proprietary Info Withheld,Per 10CFR2.7901999-07-23023 July 1999 Forwards Application for License Transfer & Conforming Administrative License Amend for OL NPF-62.Proprietary & Nonproprietary Asset Purchase Agreement Encl.Proprietary Info Withheld,Per 10CFR2.790 ML20210A4401999-07-16016 July 1999 Forwards Insp Rept 50-461/99-10 on 990422-0610.Four Violations Being Treated as Noncited Violations ML20209G7671999-07-12012 July 1999 Ack Receipt of Encl FEMA Correspondence ,which Transmitted FEMA Evaluation Rept for 981118 Biennial EP Exercise at Clinton Power Station.No Deficiencies Were Observed ML20209D5691999-07-0707 July 1999 Forwards Insp Rept 50-461/99-12 on 990607-11.No Violations Noted.Insp Consisted of Selective Exam of Procedures & Representative Records,Observations of Work in Progress & Interviews with Personnel U-603231, Forwards Summary of Status of Plan for Excellence (Pee) Initiatives & Clinton Power Station (CPS) 1999 Business Plan.Encl Documents Provide Status & Disposition for Actions Not Completed to Date1999-07-0707 July 1999 Forwards Summary of Status of Plan for Excellence (Pee) Initiatives & Clinton Power Station (CPS) 1999 Business Plan.Encl Documents Provide Status & Disposition for Actions Not Completed to Date U-603214, Forwards Results of Analysis Performed on Recently Completed Vendor Contracts,Per GL 83-28, Required Actions Based on Generic Implications of Salem ATWS Events1999-07-0606 July 1999 Forwards Results of Analysis Performed on Recently Completed Vendor Contracts,Per GL 83-28, Required Actions Based on Generic Implications of Salem ATWS Events ML20196J9651999-07-0202 July 1999 Confirms Discussion Between Members of Staffs to Conduct Meeting on 990714 at Clinton Power Station to Discuss Results of Restart Insp & Licensee Progress in Addressing Remaining Long Term C/A Actions to Sustain Improvements ML20196J7131999-06-30030 June 1999 Informs of Closure of Response to Requests for Addl Info to GL 92-01,Rev 1,Supplement 1, Reactor Vessel Structural Integrity, for Clinton Power Station Unit 1 U-603218, Provides Final Response to GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants. Attachment Provides Y2K Readiness Disclosure for Plant1999-06-28028 June 1999 Provides Final Response to GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants. Attachment Provides Y2K Readiness Disclosure for Plant U-603212, Forwards Response to NRC 990315 Telcon Re Proposed Amend of License NPF-62,implementing Feedwater Leakage Control Sys Mode of RHR Sys1999-06-24024 June 1999 Forwards Response to NRC 990315 Telcon Re Proposed Amend of License NPF-62,implementing Feedwater Leakage Control Sys Mode of RHR Sys U-603227, Provides Updated Rept on Status of Decommissioning Funding for Plant.Updated Rept Provides Min Decommissioning Fund Estimate,Per 10CFR50.75(b) & (C) Utilizing NUREG-1307,Rev 8 Methodology1999-06-24024 June 1999 Provides Updated Rept on Status of Decommissioning Funding for Plant.Updated Rept Provides Min Decommissioning Fund Estimate,Per 10CFR50.75(b) & (C) Utilizing NUREG-1307,Rev 8 Methodology ML20196A3471999-06-16016 June 1999 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-461/99-11 Issued on 990430.Corrective Actions Will Be Examined During Future Inspections 1999-09-08
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARU-603280, Forwards Rev 27 to Clinton Power Station Physical Security Plan,Iaw 10CFR50.54(p).Encl Withheld from Public Disclosure, Per 10CFR50.54(p)1999-10-12012 October 1999 Forwards Rev 27 to Clinton Power Station Physical Security Plan,Iaw 10CFR50.54(p).Encl Withheld from Public Disclosure, Per 10CFR50.54(p) ML20217C0871999-10-11011 October 1999 Forwards Proprietary Attachment Inadvertently Omitted from Encl 2 to Submitting Responses to NRC RAI Re License Transfer Application for Plant.Proprietary Encl Withheld U-603276, Forwards Rev 8 to CPS USAR, Which Includes Changes from 970701 Through 990630 & Available Changes Approved After 990630 That Reduce Overall Burden of Submittal Changes for Forthcoming Reporting period.10CFR50.59 Rept Included1999-10-0808 October 1999 Forwards Rev 8 to CPS USAR, Which Includes Changes from 970701 Through 990630 & Available Changes Approved After 990630 That Reduce Overall Burden of Submittal Changes for Forthcoming Reporting period.10CFR50.59 Rept Included U-603279, Forwards non-proprietary & Proprietary Responses to NRC RAI Re License Transfer Application for Plant.Attached Responses Also Respond to Comments of Environ Law & Policy Center Dtd 990920.Proprietary Encl Withheld1999-10-0707 October 1999 Forwards non-proprietary & Proprietary Responses to NRC RAI Re License Transfer Application for Plant.Attached Responses Also Respond to Comments of Environ Law & Policy Center Dtd 990920.Proprietary Encl Withheld U-603275, Provides Updated Illinois Power Rept on Status of Decommissioning Funding for Clinton Power Station1999-10-0707 October 1999 Provides Updated Illinois Power Rept on Status of Decommissioning Funding for Clinton Power Station U-603272, Provides Update to Final Response to GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants. 3-D Monicore & Station Security Sys remediated.Y2K Readiness Disclosure for Cps,Encl1999-09-22022 September 1999 Provides Update to Final Response to GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants. 3-D Monicore & Station Security Sys remediated.Y2K Readiness Disclosure for Cps,Encl U-603225, Provides Closure of Util Commitments Re Ci Cv Noted in Previous Ltr to Nrc.Basis for Expecting Valves to Remain in leak-tight Condition Throughout Operating Cycle & Basis That Justifies Not Performing mid-cycle Leak Testing,Encl1999-09-20020 September 1999 Provides Closure of Util Commitments Re Ci Cv Noted in Previous Ltr to Nrc.Basis for Expecting Valves to Remain in leak-tight Condition Throughout Operating Cycle & Basis That Justifies Not Performing mid-cycle Leak Testing,Encl ML20212G6981999-09-20020 September 1999 Requests That NRC Reject Proposed License Transfer for Clinton Power Station & That NRC State That Public Interest in Safe Nuclear Power Industry Will Not Be Subordinated to Interest in Maximizing Profit by Limiting Liability 05000461/LER-1996-010, Forwards LER 96-010-01, Plant Shutdown Due to Unidentified RCS Leakage from Degraded Reactor Recirculation Pump Seal Greater than TS Limit. Revised Rept Includes Cause of Event,Corrective Actions & Discussion of Similar Events1999-09-13013 September 1999 Forwards LER 96-010-01, Plant Shutdown Due to Unidentified RCS Leakage from Degraded Reactor Recirculation Pump Seal Greater than TS Limit. Revised Rept Includes Cause of Event,Corrective Actions & Discussion of Similar Events U-603269, Certifies That DB Livingston,License OP-31136,successfully Completed Facility Licensees Requirements to Be Licensed as Ro,Per 10CFR55 & Has Need for RO License to Perform Assigned Duties.Five Significant Control Manipulations,Listed1999-09-10010 September 1999 Certifies That DB Livingston,License OP-31136,successfully Completed Facility Licensees Requirements to Be Licensed as Ro,Per 10CFR55 & Has Need for RO License to Perform Assigned Duties.Five Significant Control Manipulations,Listed 05000461/LER-1999-011, Forwards LER 99-011-00 Re Improper Restoration of a APRM Which Caused Monitor to Not Meet Seismic Qualification Requirements.Rept Contains Listed Commitments1999-09-10010 September 1999 Forwards LER 99-011-00 Re Improper Restoration of a APRM Which Caused Monitor to Not Meet Seismic Qualification Requirements.Rept Contains Listed Commitments U-603229, Provides Response to NRC RAI Re GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, Dtd 990528.Rev 0 to Calculation IP-M-0556 & Rev 0 to Calculation IP-M-0570,encl1999-08-25025 August 1999 Provides Response to NRC RAI Re GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, Dtd 990528.Rev 0 to Calculation IP-M-0556 & Rev 0 to Calculation IP-M-0570,encl U-603243, Forwards Response to NRC GL 99-02, Lab Testing of Nuclear-Grade Activated Charcoal. Util Performing Testing of ESF Ventilation Sys Charcoal Samples Using ASTM D3803- 1989 Methodology as Required by TS 5.5.71999-08-23023 August 1999 Forwards Response to NRC GL 99-02, Lab Testing of Nuclear-Grade Activated Charcoal. Util Performing Testing of ESF Ventilation Sys Charcoal Samples Using ASTM D3803- 1989 Methodology as Required by TS 5.5.7 U-603258, Forwards ISI Summary Rept, IAW ASME Section Xi,Article IWA-6000.Summary Rept Addresses ISI Activities Performed at Plant from 950429-990527,including Extended Sixth Refueling Outage1999-08-23023 August 1999 Forwards ISI Summary Rept, IAW ASME Section Xi,Article IWA-6000.Summary Rept Addresses ISI Activities Performed at Plant from 950429-990527,including Extended Sixth Refueling Outage ML20211B0871999-08-20020 August 1999 Responds to J Hopkins Inquiry Re Application for Order Consenting to License Transfer & Approving Conforming Administrative License Amend Filed by Ilpr & Amergen Energy Co on 990723 U-603259, Provides Notification That Cl Kreidler Has Resigned Position with Util,Effective 990818.License Status Should Be Changed to Expired1999-08-19019 August 1999 Provides Notification That Cl Kreidler Has Resigned Position with Util,Effective 990818.License Status Should Be Changed to Expired U-603253, Notifies NRC That Je Smith,License SOP-30819-1,has Resigned from Position with Ilpr Effective 990813.Status of License Should Be Changed to Expired,Effective 9908131999-08-16016 August 1999 Notifies NRC That Je Smith,License SOP-30819-1,has Resigned from Position with Ilpr Effective 990813.Status of License Should Be Changed to Expired,Effective 990813 U-603250, Notifies NRC That Ma Freihofer (License SOP-31296-1) Has Resigned from Position with Illinois Power Effective 990729 & License Status Should Be Changed to Expired Effective 9907291999-08-10010 August 1999 Notifies NRC That Ma Freihofer (License SOP-31296-1) Has Resigned from Position with Illinois Power Effective 990729 & License Status Should Be Changed to Expired Effective 990729 U-603249, Notifies NRC That He Bouska (License SOP-3055-1) Has Resigned from Position with Illnois Power Effective 990809. & License Status Should Be Changed to Expired Effective 9908091999-08-10010 August 1999 Notifies NRC That He Bouska (License SOP-3055-1) Has Resigned from Position with Illnois Power Effective 990809. & License Status Should Be Changed to Expired Effective 990809 ML20210N2961999-08-0909 August 1999 Forwards Form of Nuclear Decommissioning Master Trust Agreement,Per CPS Application for License Transfer & Conforming Administrative License Amend U-603248, Requests Unrestricted License for Kc Scott,License SOP-31532.Scott Has Successfully Completed Facility Licensee Requirements to Be Licensed as Operator/Senior Operator Per 10CFR551999-08-0606 August 1999 Requests Unrestricted License for Kc Scott,License SOP-31532.Scott Has Successfully Completed Facility Licensee Requirements to Be Licensed as Operator/Senior Operator Per 10CFR55 U-603236, Forwards Revised Data Point Ref File Sheets for Clinton Power Station Computer Points That Input to ERDS1999-08-0202 August 1999 Forwards Revised Data Point Ref File Sheets for Clinton Power Station Computer Points That Input to ERDS ML20210J0541999-07-30030 July 1999 Forwards Three Original Signature Pages of Gr Rainey for Application for License Transfer & Conforming Administrative License Amend, for NRC Files U-603178, Forwards Four ASME Section XI Relief Requests Re Performance of non-destructive Exams for First 120-month Inservice Insp for CPS1999-07-29029 July 1999 Forwards Four ASME Section XI Relief Requests Re Performance of non-destructive Exams for First 120-month Inservice Insp for CPS U-603237, Informs That Util Will Provide Response to fire-related Questions One & Two of NRC RAI Re CPS Ipeee,By 0001311999-07-28028 July 1999 Informs That Util Will Provide Response to fire-related Questions One & Two of NRC RAI Re CPS Ipeee,By 000131 U-603240, Forwards Clinton Power Station semi-annual Fitness for Duty Rept for Period Ending 990630,IAW 10CFR26.711999-07-27027 July 1999 Forwards Clinton Power Station semi-annual Fitness for Duty Rept for Period Ending 990630,IAW 10CFR26.71 U-603235, Forwards Application for License Transfer & Conforming Administrative License Amend for OL NPF-62.Proprietary & Nonproprietary Asset Purchase Agreement Encl.Proprietary Info Withheld,Per 10CFR2.7901999-07-23023 July 1999 Forwards Application for License Transfer & Conforming Administrative License Amend for OL NPF-62.Proprietary & Nonproprietary Asset Purchase Agreement Encl.Proprietary Info Withheld,Per 10CFR2.790 U-603231, Forwards Summary of Status of Plan for Excellence (Pee) Initiatives & Clinton Power Station (CPS) 1999 Business Plan.Encl Documents Provide Status & Disposition for Actions Not Completed to Date1999-07-0707 July 1999 Forwards Summary of Status of Plan for Excellence (Pee) Initiatives & Clinton Power Station (CPS) 1999 Business Plan.Encl Documents Provide Status & Disposition for Actions Not Completed to Date U-603214, Forwards Results of Analysis Performed on Recently Completed Vendor Contracts,Per GL 83-28, Required Actions Based on Generic Implications of Salem ATWS Events1999-07-0606 July 1999 Forwards Results of Analysis Performed on Recently Completed Vendor Contracts,Per GL 83-28, Required Actions Based on Generic Implications of Salem ATWS Events U-603218, Provides Final Response to GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants. Attachment Provides Y2K Readiness Disclosure for Plant1999-06-28028 June 1999 Provides Final Response to GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants. Attachment Provides Y2K Readiness Disclosure for Plant U-603212, Forwards Response to NRC 990315 Telcon Re Proposed Amend of License NPF-62,implementing Feedwater Leakage Control Sys Mode of RHR Sys1999-06-24024 June 1999 Forwards Response to NRC 990315 Telcon Re Proposed Amend of License NPF-62,implementing Feedwater Leakage Control Sys Mode of RHR Sys U-603227, Provides Updated Rept on Status of Decommissioning Funding for Plant.Updated Rept Provides Min Decommissioning Fund Estimate,Per 10CFR50.75(b) & (C) Utilizing NUREG-1307,Rev 8 Methodology1999-06-24024 June 1999 Provides Updated Rept on Status of Decommissioning Funding for Plant.Updated Rept Provides Min Decommissioning Fund Estimate,Per 10CFR50.75(b) & (C) Utilizing NUREG-1307,Rev 8 Methodology 05000461/LER-1999-007, Forwards LER 99-007-00,re Design Error Causing Main Steam Isolation Valve Leakage Control Sys to Be Outside Design Basis.Commitment Made by Util,Listed1999-06-12012 June 1999 Forwards LER 99-007-00,re Design Error Causing Main Steam Isolation Valve Leakage Control Sys to Be Outside Design Basis.Commitment Made by Util,Listed 05000461/LER-1999-008, Forwards LER 99-008-00,re Failure of Motor Driven Reactor FW Pump Regulating Valve.Commitment Made by Util,Listed1999-06-12012 June 1999 Forwards LER 99-008-00,re Failure of Motor Driven Reactor FW Pump Regulating Valve.Commitment Made by Util,Listed U-603213, Responds to NRC Ltr Re Violations Noted in Insp Rept 50-461/99-01.Corrective Actions:Calculation 19-AK-05, Calculation for DG Load Monitoring, Was Revised Using Correct Horsepower for Hydrogen Mixing Compressors1999-05-28028 May 1999 Responds to NRC Ltr Re Violations Noted in Insp Rept 50-461/99-01.Corrective Actions:Calculation 19-AK-05, Calculation for DG Load Monitoring, Was Revised Using Correct Horsepower for Hydrogen Mixing Compressors ML20209G7731999-05-27027 May 1999 Forwards Copy of Final Rept for 981118,Biennial Radiological Emergency Preparedness Exercise for Clinton Nuclear Power Station.No Deficiencies Were Noted U-603207, Provides Util Rept Confirming Completion of Actions Required by NRC Bulletin 96-003, Potential Plugging of ECCS Strainers by Debris in Bwrs1999-05-13013 May 1999 Provides Util Rept Confirming Completion of Actions Required by NRC Bulletin 96-003, Potential Plugging of ECCS Strainers by Debris in Bwrs U-603201, Forwards 4-yr Updated Certification Rept for Plant Training Simulator.Nrc Form 474, Simulation Facility Certification Also Encl Which Was Developed in Accordance with Reg Guide 1.149 & Ansi/Ans Std Ansi/Ans 3.51999-05-0505 May 1999 Forwards 4-yr Updated Certification Rept for Plant Training Simulator.Nrc Form 474, Simulation Facility Certification Also Encl Which Was Developed in Accordance with Reg Guide 1.149 & Ansi/Ans Std Ansi/Ans 3.5 U-603196, Provides Notification That Util Has Completed Thermo-Lag 330-1 Fire Barrier Corrective Actions as Described in 970619 & s in Addition to Repair of Butt Joint Described in1999-04-27027 April 1999 Provides Notification That Util Has Completed Thermo-Lag 330-1 Fire Barrier Corrective Actions as Described in 970619 & s in Addition to Repair of Butt Joint Described in U-603205, Forwards Annual Radioactive Effluent Release Rept for Clinton Power Station for Period Jan-Dec 1998. Rev 17 to ODCM for Clinton Power Station, Also Encl1999-04-27027 April 1999 Forwards Annual Radioactive Effluent Release Rept for Clinton Power Station for Period Jan-Dec 1998. Rev 17 to ODCM for Clinton Power Station, Also Encl U-603197, Provides Details of Other Activities Being Taken as Part of CPS Plan for Excellence Re Ensureing That CPS Physical Plant & Functional Characteristics Are Consistent with & Are Being Maintained IAW CPS Design Bases1999-04-24024 April 1999 Provides Details of Other Activities Being Taken as Part of CPS Plan for Excellence Re Ensureing That CPS Physical Plant & Functional Characteristics Are Consistent with & Are Being Maintained IAW CPS Design Bases U-603194, Provides Notification That Ta Staber,License SOP-31298,has Resigned Position,Effective 990401.License Status Should Be Changed to Expired1999-04-15015 April 1999 Provides Notification That Ta Staber,License SOP-31298,has Resigned Position,Effective 990401.License Status Should Be Changed to Expired U-603189, Requests That Status of License SOP-31187-1,for Le Anderson, Be Changed to Expired,Per 10CFR50.74.Util Determined That Individual No Longer Has Need for SRO License1999-04-0505 April 1999 Requests That Status of License SOP-31187-1,for Le Anderson, Be Changed to Expired,Per 10CFR50.74.Util Determined That Individual No Longer Has Need for SRO License U-603190, Provides Update for Certain 10CFR50.74(f) Info Addressed in Licensee 980619 Submittal,But Not Included in Final Response1999-04-0202 April 1999 Provides Update for Certain 10CFR50.74(f) Info Addressed in Licensee 980619 Submittal,But Not Included in Final Response U-603185, Forwards Response to NRC RAI Re CPS GL 96-05, Periodic Verification of Design-Basis Capability of SR Movs, Program1999-03-30030 March 1999 Forwards Response to NRC RAI Re CPS GL 96-05, Periodic Verification of Design-Basis Capability of SR Movs, Program U-603186, Forwards Rept on Status of Clinton Power Station Decommissioning Funding,Iaw 10CFR50.75(f)1999-03-29029 March 1999 Forwards Rept on Status of Clinton Power Station Decommissioning Funding,Iaw 10CFR50.75(f) U-603184, Submits Info Re Current Levels of Property Insurance & Sources of Insurance for CPS as Listed,Per 10CFR50.54(w)(3)1999-03-26026 March 1999 Submits Info Re Current Levels of Property Insurance & Sources of Insurance for CPS as Listed,Per 10CFR50.54(w)(3) 05000461/LER-1999-005, Forwards LER 99-005-00,re Inoperability of Standby Gas Treatment Sys Train a Caused by Inadequate Design of Control Circuit.Commitments Listed1999-03-15015 March 1999 Forwards LER 99-005-00,re Inoperability of Standby Gas Treatment Sys Train a Caused by Inadequate Design of Control Circuit.Commitments Listed U-603165, Forwards Revised Data Point Ref File Sheet for Clinton Power Station Computer Point That Inputs to Erds.Change Necessary to Support Plant Mods to Drywell Floor Drain Instrumentation1999-03-12012 March 1999 Forwards Revised Data Point Ref File Sheet for Clinton Power Station Computer Point That Inputs to Erds.Change Necessary to Support Plant Mods to Drywell Floor Drain Instrumentation U-603179, Provides Notification That RG Giuliani & R Zacholski,No Longer Have Need for Operating License.License Status Is Therefore Requested to Be Changed to Expired1999-03-10010 March 1999 Provides Notification That RG Giuliani & R Zacholski,No Longer Have Need for Operating License.License Status Is Therefore Requested to Be Changed to Expired 1999-09-22
[Table view] Category:UTILITY TO NRC
MONTHYEARML20059L6571990-09-19019 September 1990 Advises That Dp Hall No Longer Associated W/Facility Since Dec 1989.Mail Should Be Addressed to Js Perry JSP-739-90, Requests Expedited Review & Approval of Proposed Change to Emergency Tech Specs Re Div III Nuclear Sys Protection Sys Inverter Concerning Inoperability of Emergency Shutdown Svc Water Sys Pump1990-09-12012 September 1990 Requests Expedited Review & Approval of Proposed Change to Emergency Tech Specs Re Div III Nuclear Sys Protection Sys Inverter Concerning Inoperability of Emergency Shutdown Svc Water Sys Pump U-601729, Notifies That Bn Chambers Permanently Reassigned to Position Not Requiring Operator License.Certification of Chambers Need to Hold License Previously Provided by Dp Hall Withdrawn1990-08-27027 August 1990 Notifies That Bn Chambers Permanently Reassigned to Position Not Requiring Operator License.Certification of Chambers Need to Hold License Previously Provided by Dp Hall Withdrawn JSP-676-90, Responds to 900725 Notice of Violation & Proposed Imposition of Civil Penalty Documented in Insp Rept 50-461/90-09. Corrective Action:Critique Initiated to Identify Precise Causes & Contributing Factors Leading to Event1990-08-23023 August 1990 Responds to 900725 Notice of Violation & Proposed Imposition of Civil Penalty Documented in Insp Rept 50-461/90-09. Corrective Action:Critique Initiated to Identify Precise Causes & Contributing Factors Leading to Event U-601723, Forwards Results of fitness-for-duty Program for 900103-0630,per 10CFR26.711990-08-16016 August 1990 Forwards Results of fitness-for-duty Program for 900103-0630,per 10CFR26.71 U-601722, Forwards Reissued NPDES Permit IL00369191990-08-10010 August 1990 Forwards Reissued NPDES Permit IL0036919 U-601721, Provides Response to Re Process for Requalification Exam Security Agreements.Security Agreement Forms Revised to Direct Individuals Not to Participate in Any Instruction Involving Operators or Senior Operators1990-08-0808 August 1990 Provides Response to Re Process for Requalification Exam Security Agreements.Security Agreement Forms Revised to Direct Individuals Not to Participate in Any Instruction Involving Operators or Senior Operators U-601716, Forwards Response to Violations Noted in Insp Rept 50-461/90-10.Response Withheld (Ref 10CFR73.21(c)(2))1990-08-0303 August 1990 Forwards Response to Violations Noted in Insp Rept 50-461/90-10.Response Withheld (Ref 10CFR73.21(c)(2)) U-601715, Provides Addl Info Re Proposed Amend to Plant Tech Spec 3/4.8.1.1, AC Sources - Operating, Per .Amend Will Allow Testing Frequency of Diesel Generator to Be Returned to Monthly1990-08-0202 August 1990 Provides Addl Info Re Proposed Amend to Plant Tech Spec 3/4.8.1.1, AC Sources - Operating, Per .Amend Will Allow Testing Frequency of Diesel Generator to Be Returned to Monthly U-601708, Forwards Revised Pages to Semiannual Radioactive Effluent Release Repts for Jul-Dec 1988,Jan-June 1989 & Jul-Dec 19891990-07-19019 July 1990 Forwards Revised Pages to Semiannual Radioactive Effluent Release Repts for Jul-Dec 1988,Jan-June 1989 & Jul-Dec 1989 U-601702, Forwards Rev 9D to Physical Security Plan.Rev Withheld (Ref 10CFR73.21)1990-07-0202 July 1990 Forwards Rev 9D to Physical Security Plan.Rev Withheld (Ref 10CFR73.21) ML20044A3001990-06-22022 June 1990 Forwards Update to 890817 Response to Bulletin 88-008,Suppl 3, Thermal Stresses in Piping Connected to Rcs. Unisolable Piping Connected to RCS Identified & Evaluated to Determine Which Piping Could Be Subj to Stratified Flow Phenomena ML20044A4601990-06-22022 June 1990 Provides Followup to 900622 Request for Waiver of Compliance Re Tech Spec Limiting Condition for Operation Concerning Standby Emergency Diesel Generator 1B.Rev to Attachment 1 of Original Request for Waiver Encl ML20043H5021990-06-19019 June 1990 Requests Changes to License NPF-62,correcting Typos, Refs to Fsar,Testing to Be Done During Initial Plant Startup & Incorporating Revised Operating Power/Flow Map for Two Reactor Recirculation Loop Operation ML20043G8221990-06-0707 June 1990 Provides Update to Util Response to Item 1 of Generic Ltr 88-01, NRC Position on IGSCC in BWR Austenitic Stainless Steel Piping. ML20043F0591990-06-0606 June 1990 Forwards Endorsements 44-50 to Nelia Policy NF-261 & 25-31 to Maelu Policy MF-121 & 10 & 11 to Maelu Policy N-85 & M-85,respectively ML20043D0531990-05-31031 May 1990 Forwards 1989 Annual Rept for Illinois Power Co & Soyland Power Cooperative,Inc ML20043C7501990-05-25025 May 1990 Forwards Rev 20 to Illinois Power Nuclear Program QA Manual. Rev Evaluated by Util as Not Reducing Quality Program Commitments ML20043B4891990-05-21021 May 1990 Informs NRC of Plant Initiatives for 1990 to Improve Corrective Action Program Effectiveness,In Response to SALP Rept & Violations Noted in Insp Rept 50-461/89-32. Centralized Commitment Tracking Sys Upgraded ML20043B1141990-05-17017 May 1990 Suppls 900330 Response to Station Blackout Rule.Calculation of Heatup of Main Control Room Due to Loss of Ventilation Following Station Blackout Revised to Properly Account for Heat Sinks & Credit Existing Masonry Walls ML20043D9901990-05-14014 May 1990 Responds to NRC 900413 Ltr Re Violations Noted in Insp Rept 50-461/90-02.Corrective Actions:Safety Evaluation Prepared & Reviewed for Level Instrumentation & Annunciators Identified in Updated SAR ML20043A9811990-05-14014 May 1990 Notifies That Wc Metzner Resigned from Position of Licensed Operator W/Util,Effective 900430 ML20042E6181990-04-13013 April 1990 Updates 890406 Response to Generic Ltr 88-14, Instrument Air Supply Sys Problems Affecting Safety-Related Equipment. Condition Rept Initiated to Address Issue to Drain Instrument Air Filter Regulators ML20012E8991990-03-27027 March 1990 Forwards Rev 9C to Physical Security Plan.Rev Does Not Decrease Effectiveness of Plan.Rev Withheld (Ref 10CFR73.21) ML20012D9451990-03-20020 March 1990 Informs of Current Activities Re Restoration of Shutdown Svc Water (SX) Sys to Operability Following Cleaning of Div I HX Per Generic Ltr 89-13.SX Sys to Be Restored by Returning Sys Flows to Design Values ML20012D9641990-03-19019 March 1990 Lists Present Levels of Property Insurance Coverage & Sources of Insurance,Per 10CFR50.54(w)(2) ML20012D9901990-03-19019 March 1990 Responds to NRC 900216 Ltr Re Violations Noted in Insp Rept 50-461/89-38.Corrective Actions:Maint Supervision Added Critical Points to Existing Maint Work Requests & Preventive Maint Activities & Training Program Updated ML20012D4321990-03-16016 March 1990 Responds to Bulletin 88-008,Suppl 3, Thermal Stresses in Piping Connected to Rcs. Detailed Analytical Review & Proposed Schedule for Implementing Required Actions Scheduled to Be Completed by 900625 ML20012A2771990-02-28028 February 1990 Forwards Final Response to NRC Bulletin 88-010,Suppl 1, Nonconforming Molded Case Circuit Breakers. Actions Taken by Util Have Established That All safety-related Circuits Remaining in Stock Can Be Verifiably Traced to Mfg ML20012C2511990-02-23023 February 1990 Responds to Ninth SALP Rept 50-461/89-01 for Sept 1988 - Oct 1989.Rept Concluded That Overall Performance Satisfactory & Identified Strengths in Areas of Emergency Preparedness U-601611, Notifies That Gd Setser Resigned Position W/Util,Effective 9002131990-02-20020 February 1990 Notifies That Gd Setser Resigned Position W/Util,Effective 900213 ML20011F6501990-02-12012 February 1990 Responds to NRC 900112 Ltr Re Violations Noted in Insp Rept 50-461/89-37.Corrective Actions:Radiation Protection Technicians Provided W/Method for Identifying Radiation Work Permits Which Change Radiological Conditions ML20006C6721990-02-0505 February 1990 Responds to NRC 891207 Ltr Re Violations Noted in Insp Rept 50-461/89-35.Corrective Actions:Emergency Planning Bulletin Issued to All Emergency Response Organization Members Emphasizing Importance of Attending Required Training ML20006D1951990-01-30030 January 1990 Responds to Generic Ltr 83-28, Required Actions Based on Generic Implications of Salem ATWS Events. Util Intends to Discontinue Sending Ack Upon Receipt of Vendor Manual Matls ML20006A8291990-01-23023 January 1990 Forwards Rev 3 to Inservice Exam Plan. Changes to Text Described.Approval of Changes by 900601 to Allow Time to Plan Refueling Outage Activities Re Inservice Exam Program Requested ML20005H2711990-01-12012 January 1990 Advises That Licensee Will Remove Terminal Blocks for Control Circuits within 100% Relative Humidity Harsh Environ at Plant by End of Second Refueling Outage Currently Scheduled to Begin in Sept 1990 ML20006A7121990-01-10010 January 1990 Forwards Revised Pages to 1987 Radiological Environ Monitoring Rept ML20005F0001990-01-0505 January 1990 Responds to NRC Bulletin 88-004, Potential Safety-Related Pump Loss. Util Revised Plant Operating Procedures for Hpcs,Lpcs & RHR Pumps & Vibration Monitoring Program Expanded to Include ECCS Pumps at Plant ML20006A7921989-12-29029 December 1989 Responds to 891129 Ltr Which Forwarded Insp Rept 50-461/89-31,requesting Identification of Actions Underway to Ensure That Falsification of Interim Security Screening Records Would Be Detected in Timely Manner in Future U-601573, Responds to Generic Ltr 89-10, Safety-Related Motor- Operated Valve Testing & Surveillance. Detailed Procedures Controlling Actuator Adjustments,Repair,Preventive Maint & Other Activities Used & Updated Frequently1989-12-29029 December 1989 Responds to Generic Ltr 89-10, Safety-Related Motor- Operated Valve Testing & Surveillance. Detailed Procedures Controlling Actuator Adjustments,Repair,Preventive Maint & Other Activities Used & Updated Frequently ML20005E0891989-12-27027 December 1989 Advises That Revised Fitness for Duty Program Will Meet 10CFR26 Requirements,Effective 900103.Util Intends to Test for Substances Listed at Indicated cut-off Levels ML20006C2961989-12-21021 December 1989 Responds to NRC 891121 Ltr Re Violations Noted in Insp Rept 50-461/89-32.Corrective Actions:Review Performed to Identify Surveillances Which Require Lifting of Leads in Main Control Room ML20005D9521989-12-15015 December 1989 Forwards Monthly Operating Rept for Nov 1989 for Clinton Power Station Unit 1 & Corrections to Oct 1989 Rept ML20005E7781989-12-12012 December 1989 Advises That False Alarm Criteria Will Be Implemented by 900131,per Insp Rept 50-461/89-31.Util Established New Criterion of 100 False Alarms for Security Sys in 24 H Period ML20011D1741989-12-0707 December 1989 Informs of Changes Made to Util Fitness for Duty Program Procedure.Change Specifies That Supervisor - Medical Programs,Assistant Director - Labor Relations or Manager - Nuclear Planning & Support Will Generate Computer List ML19332F0071989-11-30030 November 1989 Responds to Violations Noted in Insp Rept 50-461/89-29. Corrective Actions:Preventive Maint for Ph Monitor & Liquid & Gaseous Gamma Monitors Added to Appropriate Tracking Programs ML19332E9431989-11-29029 November 1989 Forwards Executed Amends 4 & 5 to Indemnity Agreement B-91, Reflecting Change in Ownership of License,Effective 890327 ML19332D5031989-11-27027 November 1989 Responds to Generic Ltr 89-21 Re Status of Implementation of USI Requirements.Results of Util Review & Reporting of Status of Implementation of USIs Encl ML19332D0291989-11-22022 November 1989 Informs That Effective 891201,JS Perry Will Assume Responsibility for Mgt of Nuclear Program at Util ML19332D0431989-11-22022 November 1989 Informs NRC of Change in Schedule for Providing Info Re Environ Qualification Testing of Terminal Blocks for Control Circuits of Conax Electrical Penetrations.Wyle Labs Test Results & Util Review of Results Will Be Sent by 900112 1990-09-19
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p-U- 600282 1A.120 L42-85(09-30)-L ILLINDIS POWER 00MPANY IP CLINTON POWER STATION. P.O. BOX 678. CLINTON. ILLINOIS 61727 September 30, 1985 Mr. J. G. Keppler Regional Administrator Region III U. S. Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, Illinois 60137
Subject:
Response to Notice of Violation dated August 30, 1985 and the Executive Summary in the Construction Appraisal Team (CAT) Inspection Rep >rt 50-461/85030 dated August 15, 1985.
Dear Mr. Keppler:
This letter is in response to the August 30, 1985, letter identifying certain activities which appeared to be in noncompliance with NRC requirements and certain areas that appear to have programmatic weaknesses. Attachments A through F provide Illinois Power Company's responses to the Notice of Violation and Attachment G provides Illinois Power Company's response to the NRC identified programmatic weaknesses.
I trust that our response is satisfactory to ensure compliance with regulatory requirements.
Sincerel yours, 639 F. A. pang tberg Manager - Licensing and Safety JAB /kaf Attachments cc: B. L. Siegel, NRC Clinton Licensing Project Manager Director, Office I&E, USNRC, Washington, DC 20555 T. P. Gwynn, Chief Projects Section 1B, NRC Resident Office Illinois Department of Nuclear Safety l
8511050054 850930 00T 1 - M PDR ADCCK 05000461 G ,' PDR 7%/yl ;
n U- 600282 ATTACHMENT A Illinois Power Company Clinton Power Station Subj ect: Modeling of Snubber Supports The Notice of Violation States in pertinent part:
"... the licensee's program was not adequately implemented in that two ASME Class 1 Nuclear Steam Supply System snubber supports were found to have been modelled and analyzed as rigid supports contrary to FSAR commitments to model them as flexible supports."
I. Corrective Action Taken and Results Achieved The Clinton Power Station (CPS) Final Safety Analysis Report (FSAR) Subsection 3.9.3.4.1 addresses the analysis of supports in the NSSS scope of supply. Subsection 3.9.3.4.2 of the FSAR addresses the analysis of supports in the Balance of Plant (BOP) scope of supply. The NSSS/B0P scope division in the FSAR is based on piping analysis responsibility. The supports in question, although part of the Nuclear Boiler system and therefore a part of the NSSS, are within the BOP scope of supply for piping analysis and support design. Subsection 3.9.3.4.2 of the FSAR states in part: "The snubbers are designed and load rated in accordance with NF-3000 to be capable of carrying the design load for all operating.
conditions." These supports were, therefore, modeled as rigid supports in accordance with FSAR commitments for BOP supports.
II. Corrective Action Taken to Prevent Recurrence Illinois Power is in compliance, therefore no actions are necessary.
III. Date When Full Compliance will be Achieved Illinois Power is in full compliance.
U- 600282 ATTACHMENT B Illinois Power Company Clinton Power Station
Subject:
Implementation of Decument Control Procedures The Notice of. Violation states in pertinent part:
"... Baldwin Associates (BA) document control procedures were
'not properly implemented in that numerous discrepancies were identified in the filing and updating of procedures in the Civil and Structural Resident Engineer's copy of the BA Project Procedures Manual, and in the posting of design change documents in specifications."
I. Corrective Action Taken and Results Achieved An audit of BA Project Procedure manuals, K-Spec manuals, and associated change documents was conducted by the document' holders.- Corrective actions required by this audit have ensured that all manuals are current and correct. Also, BA document control has retrieved copies deemed unnecessary, thereby increasing control by reducing the number of copies.
II. Corrective Action Taken to Prevent Recurrence BA document control will continue to perform surveillances of manuals to ensure that they are current. In addition, BA will conduct training to ensure implementation of existing programs related to the updating of procedure and specification manuals and to reaffirm the need for maintaining ~the manuals.
III. Date When Full Compliance Will Be Achieved Illinois Power will be in full compliance on November 1, 1985.
U- 600282 ATTACHMENT C Illinois Power Company Clinton Power Station
Subject:
Welds on Vendor Supplied Items The Notice of Violation states in pertinent part:
"... the NRC CAT inspectors identified vendor procured tanks and heat exchangers that had been accepted and installed with <
deficient welds. They also identified varioue vendor and contractor supplied radiographs which did not have the required weld and film quality."
I. Corrective Action Taken and Results Achieved All tanks and pressure vessels supplied by Chicago Bridge &
Iron (CB&I) and Richmond Engineering (RFCO), the vendors of interest, have been reinspected. All nonconforming conditions were documented on Nonconformance Reports (NCRs) and are being processed in accordance with site procedures. Most of the NCRs have been dispositioned use-as-is because the discrepancies identified were found to be within the applicable ASME Code parameters.
The radiographic film for valve IE22F016 was not legible because of water damage. Nonconforming Material Report (NCMR)
No. 2-0346 was initiated to document this condition. The radiograph had been used to substantiate valve body integrity prior to the occurrence of the water damage, and the radiograph inspection report was found acceptable by the vendor and BA Quality departments. Future rek rence to the damaged film will not be required, as the Preservice/ Inservice program requires cnly that the valve be exercised to the position required to fulfill its function.
The radiograph for Lakeside Bridge & Steel piece marked 2-1-1 contained unacceptable indications. Further investigation by BA Quality and Technical Services and the CAT inspectors revealed that the unacceptable indications had been reworked and re-radiographed as a result of a BA surveillance. The second radiograph film that represented the reworked condition was identified by review and comparison of other acceptable indications common to the two radiographs. This second radiograph was determined to be acceptable and is now the radiograph of record for the weld.
Three radiographs were found to contain unacceptable indications. Nonconformance reports 32681, 32597 and 32294 were initiated to document these conditions and are being processed in acenrdance with site procedures.
U-600282 ATTACHMENT C Illinois Power Company Clinton Power Station II. Corrective Action Taken to Prevent Recurrence Since all_ major plant equipment has been installed and the corrective actions noted above have been initiated, and any further modifications will be controlled by the Maintenance Work Request (MWR) program, no further corrective action is required.
III. Date When Full Compliance Will Be Achieved Illinois Power is in full compliance.
1
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r U-600282 ATTACHMENT D lllinois Power Company Clinton Power Station
Subject:
Equipment Mounting not per Drawings and Specifications The Notice of Violation states in pertinent part:
"... bolts for mounting large pump-motors, pump turbine assemblies mounted on skids, and HVAC control panel cabinets were not as required by the applicable drawings and specifications."
I. Corrective Action Taken and Results Achieved Illinois Power has issued several NCMRs to document the missing or incorrect material. A review has been performed which attempted to identify the circumstances causing lockwashers to be missing or the incorrect bolting material to be installed.
This review concluded that the installation documents lacked clarity and that this lack of clarity was a contributing factor which led to the equipment being installed without lockwashers. All known instances of missing lockwashers have been documented and are being processed in accordance with site procedures. For the incorrect materials identified on skid mounted equipment it is postulated that inspections performed prior to release for shipment or upon receipt did not identify the incorrect bolting material.
Illinois Power's Architect / Engineer, Sargent & Lundy, perforued an evaluation to determine if these deficiencies, had they gone uncorrected, would have affected the safe operation of CPS. This evaluation found that no safety significant conditions would have existed.
II. Corrective Action Taken to Prevent Recurrence The equipment which exhibited the fastener deficiencies is periodically monitored for vibration in accordance with CPS Procedure No. ITP 2600.02S, " Vibration Monitoring". This procedure outlines the performance monitoring program consisting of the acquisition, retention, and interpretation of machinery vibration data. The procedure discusses the methods by which loose mounting bolts (the problem likely to occur as a result of the deficiencies identified) will be analyzed.
In view of the ability to trend equipment performance using vibration monitoring (in conjunction with the engineering analysis), no further corrective action is required.
III. Date When Full Compliance Will Be Achieved Illinois Power is in full compliance.
w_____-_-____-_-____.
U-600282 ATTACHMENT E Illinois Power Company Clinton Power Station
Subject:
Inspection Programs The Notice of Violation states in pertinent part:
"... the licensee's inspection programs were not effectively implemented in that they:
a) Have not assured that safety-related electrical raceways have been installed in accordance with FSAR commitments for electrical separation.
b) Have failed to assure that appropriate quality verifications are conducted and that only qualified materials are used for work performed under the Maintenance Work Request Program, c) Had not assured that safety-related SkV power cable terminations were accomplished in accordance with design documents in that required insulating materials had not been installed."
I. Corrective Action Taken and Results Achieved a) Illinois Power is amending the FSAR to revise the electrical separation criteria. This revision will include an option to perform analysis of potential separation problems identified by the Interaction Analysis Program. Illinois Power has also contracted with Wyle Laboratories to conduct physical testing to support the FSAR amendment. In additio'n, Illinois Power has conducted in-depth training for the personnel performing the walkdowns to ensure that all potential interactions are correctly identified.
b) Illinois Power took the following actions regarding the deficiencies in the MWR program identified by the CAT inspectors:
Condition Report (CR) number 1-85-06-007 was issued to document the misclassification of MWR B02288 and-the resultant use of unacceptable wire. In addition, NCMR 1-1854 was written to document the use of the unacceptable wire. MWR B11255 was written to remove and replace the wire.
L
U-600282 ATTACHMENT E Illinois Power Company Clinton Power Station NCMR 1-0935 was written to document the lack of engineering evaluations of the environmental qualification of wire used in the performance of MWRs A16980 and A17116. Construction Work Requests (CWRs) 15086 and 15166 were written to replace the wire with acceptable material. In addition, CR 1-85-06-051 was written to address the use of incorrect wire in Class lE MWRs.
MWR B13553 was written and Quality Control Inspection Report 0587 was prepared to document achievement of adequate inspection of the field cable splicing cited in the inspection report.
Field Change Request (FCR) 24896 authorizes the swapping of motor leads to obtain proper motor rotation. A review of this FCR revealed that, although it does state " connections may be modified as required to obtain proper motor rotation," it does not indicate that approved design drawings do not have to depict the as-installed wiring configurations.
Illinois Power initiated the following actions to define the weaknesses in the MWR program evidenced by the three types of deficiencies referred to above:
- 1) A review of the classification process for MWRs was conducted, and
- 2) A sample review of completed MWRs was conducted.
The review of the process for classification of MWRs revealed that classification was determined by reference to the FSAR, K-Specs, or drawings. This effort was being performed by Maintenance Planners instead of by engineering personnel.
The sample review of completed MWRs for classification identified a significant number of MWRs that were questionable. Therefore, the Nuclear Station Engineering Department (NSED) is conducting a review of all completed MWRs.
c) Baldwin Associates initiated NCRs 32232 and 32081 to document the incorrect terminations identified by the CAT inspectors. Baldwin Associates Electrical Quality Control personnel will conduct a complete reinspection of safety-related SkV cable terminations and document nonconforming conditions. These NCRs and all other NCRs will be processed in accordance with site procedures.
R U-600282 ATTACHMENT E Illinois Power Company Clinton Power Station II. Corrective Action to Prevent Recurrence a) Illinois Power's Amendments 34 and 35 to the FSAR will revise the site specific electrical separation criteria, t as well as allow analysis as an alternate to existing' separation guidelines. Also, the Interaction Analysis Program walkdown checklists have been revised to add specific attributes and illustrations of acceptable conditions. The personnel performing the walkdowns have been trained in the use of the revised checklist, b) Illinois Power has issued a procedure M.1, " Safety Class Statusing of Maintenance Work Requests". This procedure has been approved and training has been conducted. The procedure institutes controls in maintaining electrical separation, in-service inspection, environmental qualification, and quality assurance. These reviews and evaluations are now being conducted by NSED, in lieu of the Maintenance Department.
Procedure M.1 has been implemented. This will ensure that MWRs receive a proper safety classification and that substitution of materials and performance of safety-related work will have adequate controls to preclude degrading design integrity. In addition, Illinois .awer's Quality Control is reviewing completed MWRs to assure that necessary Quality Inspections have been performed.
Illinois Power has initiated the required design change documents to show that 1 cads that are modified to obtain proper motor rotation do not have to be depicted on the as-installed wiring drawings.
c) Baldwin Associaten is conducting training for BA Electrical Quality Control Inspectors to emphasize the correct termination requirements for SkV power cable.
III. Date When Full Compliance Will Be Achieved a) Illinois Power will be in full compliance upon issuance of Amendment 35 of the FSAR.
b) Illinois Power will be in full compliance on December 31, 1985.
c) Illinois Power will be in full compliance on October 31, 1985.
U-600282 ATTACHMENT F Illinois Power Company Clinton Power Station
Subject:
Identification and Correction of Conditions Adverse to Quality The Notice of Violation states in pertinent part:
a) "... NCR 31282 was incorrectly dispositioned by S&L as use-as-is based on specification requirements having been met, when the specification and FSAR requirements had not been met for cadweld operator testing frequency."
b) "... The resolution on NCR S-S-S-0006 and NCR 174 had not provided a timely and comprehensive review of applicable soil test data to ensure the FSAR commitments were met. Corrective Action taken for NCR 174 had accepted structural fill placements using nuclear density test data where sand cone test data had failed which was contrary to the project specifications. Further, the evaluation performed of soil records did not identify or address that the inspection program during that period had not provided for adequate records or assurance that the structural fill was placed in 12 inch lifts as stated in the FSAR."
I. Corrective Action Taken and Results Achieved a) A review of the cited NCR was performed to establish the circumstances for the resolution and the appropriateness of the resolution provided. This review showed that the FSAR was more stringent than the appropriate standards.
Specifically, sampling and testing for each cadweld operator as required by the FSAR, is not required by the standards.
At CPS each cadweld operator is tested by a qualification test and requalified every three months. The testing frequency of cadwelds at CPS is based on a crew which is assigned a single traveler at any one time. This meets the requirements of ANSI N45.2.5-1974.
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U- 600282 ATTACHMENT F Illinois Power Company Clinton Power Station b) A review of the two cited NCRs was performed to establish the circumstances surrounding the corrective action taken on the NCRs and the appropriateness of the resolutions provided. The NCRs were written during the period of initial construction (1976-1977) and report programmatic problems related to soils test frequency, adequacy of test procedures employed, and interpretations of soils specification requirements. The review indicated that the full extent of the nonconforming conditions was not assessed and corrected by the two NCRs, and that two years were required to fully document and resolve the overall problem.
A review was completed in September, 1985, of the dispositions provided on the two NCRs to determine the effect on the soils work adequacy, and confirmed that the original dispositions were, and remain, valid. The procedural deficiencies identified on the two NCRs had been investigated in 1976-1977 in sufficient depth by Sargent & Lundy. Some soil areas were recompacted, and some areas were retested to resolve the two NCRs. Other problems identified on the two NCRs were a result of arithmetic errors on test reports and were evaluated, but did not require additional soil compaction and testing.
It was also confirmed during the review of the two NCRs ,
that the governing earthwork specification did not preclude the use of the Nuclear Density Test Method for determining in-place soil density. As a result, this method may be used in_ lieu of the Sand Cone Method in evaluating the in-place soil density. Therefore, although approximately two years lapsed to obtain complete corrective action, an adequate resolution of the issues was obtained.
A review of soil placement inspection records for the period in question was also completed in September, 1985, and determined that numerous instances occurred where structural fill (type B soil) loose lift thickness exceeded the 12" limit stated in Section 2.5.4.5.1.5 of the FSAR. HovcVer, at the time in question, the FSAR had not yet been written. A review of the Preliminary Safety Analysis Report (PSAR), and the soil placement specification and procedure in effect at the time of placing the structural fill, indicated that no specific limits existed for placing the fill in 12" lifts.
U-600282 ATTACHMENT F Illinois Power Company Clinton Power Station Acceptance of the fill was based, es required by the -
governing specification in 1976-1977, on in-place moisture / density measurements, not lift thickness.
Further, compaction tests performed very early in the project determined that there was little difference in c dry density between the plccement of a 12" and 18" loose lift thickness. Therefore, placing soil in excess of 12" was technically acceptable and was not in violation of the governing requirements at the time.
II. ~ Corrective Action Taken To Prevent Recurrence 2
a) The current program for testing cadweld operators meets the requirements. However, for clarification Illinois Power is revising the FSAR to agree with the requirements of ANSI N45.2.5-1974 Illinois Power will continue to test cadweld operators at frequencies based on travelers.
b) An intensive review of soils documentation was performed by Baldwin Associates Document Review Group. The review was performcd to verify, through records review, that appropriate requirements applicable to soils work were met. The review focused on pertinent aspects of soils inspection and testing documentation as they applied to lift thickness, moisture-density relationships, one-point /five-point proctors, and density of soils in-place. Other aspects that support these activities, such as soil test technician certification, and traceability of measuring and test equipment used in soils work for the above activities, were also reviewed.
This review is complete. Eighty-one NCRs were generated as a result of this effort, all of which were dispositioned use-as-is. Illinois Power has a high degree of confidence in the structural integrity of the soils placed at CPS.
As noted in 1. above, the 12" lift thickness stated in the FSAR is not required for technical adequacy. An r AR revision has been initiated to eliminate thic coatement and will be accomplished in Amendment 35.
'III. Date When Full Compliance Will Be Achieved Illinois Power will be in full compliance upon issuance of Amendment 35 of the FSAR.
U- 600282 ATTACHMENT C Illinois Power Company Clinton Power Station
Subject:
Program Weaknesses Identified by Executive Summary The Executive Summary states in part:
". . . the NRC CAT did identify a number of construction program weaknesses, which in cost cases, have resulted in hardware deficiencies that require additional management attention. These include:
- 1) Control of work performed by plant staff on components after turr.over from construction requires improvement.
This is evidenced by the number of deficiencies identified in the Maintenance Work Request (MWR) Program.
Three MWRs were found to have used unqualified wire and three MWRs did not include, or properly document, the required quality control (QC) inspections. Also of concern is the lack of control of entries into and the number of errors in IP's Startup Punchlist Tracking System.
- 2) Current programs for verification of electrical separation require improvement. The number of raceway separation deficiencies identified indicate that control of separation through design without inspection for separation is not adequate and the current walkdown program has not been effective. The FSAR does not currently allow the use of analysis which is now being used to justify reduced separation requirements.
- 3) Examples were noted where design requirements were not implemented by construction and verified by quality control activities. This is indicated by examples of hardware deficiencies identified in several areas. For example, power cable terminations were not insulated as required, tanks and heat exchangers were not modelled as committed, and a number of pieces of equipment were found to be mounted with bolts of a material grade other than that specified.
- 4) Annumber of document control discrepancies were found between the design change data listad for a specification or drawing in the Dacument Management System (DMS) and the design change documents actually posted with the controlled construction rpecification or drawing. This is of particular concern since control of construction 4 specifications and drawings, and their computer data bases, is key in the management system established for ensuring that current design documents are used in developing work packages for installation and inspection.
However, no resulting hardware deficiencies were noted in a sample of related work checked by the team.
o U-600282 ATTACHMENT G Illinois Power Company Clinton Power Station
- 5) Corrective action was not considered timely or suffier.ently cor cehensive for deficiencies identified by the licensee in che testing of structural fill.
Deficiencies were identified in the structural fill records related to the lift thickness requirement of structural fill."
II. Illinois Power's ret; case is as follows:
- 1) An NSED review of all comph:tud MWRs has been undertaken and appropriate corrective actions have been taken to ensure that these MWRs have been correctly classified.
All completed MWRs and future MWRs will be evaluated by NSED in accordance with NSED Procedure H.1, " Safety Class Statusing of Maintenance Work Requests." The NSED procedure requires verification and documentation of proper safety class, seismic class, code class, environmental qualification and quality assurance requirements.
In order to emphasize the importance of punchlist accuracy, Startup has written, approved and implemented training on Startup Administrative Instruction 12 (SAI-12), "Startup Punchlist". Training is now complete and effectiveness will be assessed by documented reviews for errors and repetitive entries.
- 2) Illinois Power has analyzed the CAT observations, and concluded that the basic NRC issues can be summarized as follows:
a) Based on the number of raceway separation deficiencies noted by the CAT inspectors, the existing design, quality verifications, and walkdown programs had not been adequate to ensure compliance with specified commitments.
b) The personnel performing walkdown activities were not trained fully, c) Walkdown personnel had not received detailed acceptance criteria, d) Analysis is used to justify lesser spatini separation, which is inconsistent with current FSAR commitments.
-O U-600282 ATTACHMENT G Illinois Power Company Clinton Power Station Illinois Power has taken several actions to enhance the electrical separation program. The first was a detailed analysis of separation items identified in the CAT Inspection Report. Most of the CAT items had been previously identified by the Interaction Analysis Program (IAP). The remaining items resulted from new construction since the last IAP walkdown. The IAP requires periodic (at least every 6 months) walkdowns of CPS. Additionally, the resolution of potential interactions will be facilitated by Amendments 34 and 35 of the FSAR which will define alternate separation criteria based on testing and/or analysis.
The second action taken by Illinois Power was to enhance the overall training of walkdown personnel. Training was conducted on such topics as Regulatory Guide 1.75, Rev.
2, the relationship between IEEE-384-1974 and the Regulatory Guide, the CPS licensing position on electrical separation and the procedures / instructions used for electrical separation walkdowns.
The third action involved the specific acceptance criteria to be used. Supplemental checklists were developed to clearly define established separation criteria and were incorporated in the walkdown training program.
The fourth action taken involved the use of analysis in determining appropriate separation criteria.
This concern was identified by Illinois Power in early 1985. Corrective action was initiated prior to the CAT Inspection and will be completed by submittal of Amendments 34 and 35 of the FSAR.
- 3) Illinois Power's Quality Assurance Program ensures that quality construction is accomplished and verified by accurate translation of design requirements into construction activities. In addition, the results of the Overinspection and Record Verification Programs have provided additional confidence in the effectiveness of the Quality Assurance Program. Illinois Power considers the noted cases to be isolated incidents end therefore not of programmatic concern.
- 4) Illinois Power has incorporated controls into the computerized data base, which is the mechanism for maintaining current information about outstanding change documents. This allows electronic transfers of information between systems, thereby eliminating errors caused by multiple inputs. In addition, extensive training has been undertaken to emphasize the importance of properly updated material (specifications, drawings).
Baldwin Associates Document Control Center will perform surveillances on documents externally controlled. Any discrepancy will initiate an audit of that area's controlled documents.
- 5) In regard to the specific 1976-1977 instances cited relating to the structural fill, the corrective actions are described in Attachment F, above. In regard to the Corrective Action Program in general, however, Illinois Power implemented extensive improvements in the Corrective Action Program in 1982. These improvements were directed at timely identification and resolution of nonconforming conditions. The Corrective Action Program now provides extensive reviews both in line and generically with results that are reviewed by ranagement monthly. This extensive program has already handled over 40,000 documents, and while some errors are inevitable, Illinois Power considers the program comprehensive and effective.
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