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On April 30, 2017, at 1818 (EDT), the main … On April 30, 2017, at 1818 (EDT), the main turbine steam bypass valve #1 partially opened. Power was incrementally lowered. While lowering power the bypass valve would shut and then reopen and power would again be lowered. When power was lowered to approximately 74 percent the bypass valve remained closed. During the transient the reactor protection system (RPS) Turbine Stop Valve Closure and Control Valve Fast Closure trip functions were declared inoperable due to the opening of the bypass valve which affects the bypass setpoint for those RPS trip functions. With the loss of these RPS trip functions a loss of safety function existed intermittently for approximately 37 minutes. The manual reactor trip function and other RPS functions remained operable.</br>Both channels of the rod withdrawal limiter (RWL) and the end of cycle reactor recirculation pump trip (EOC-RPT) function were also declared inoperable. These functions are credited in accident analysis, this also resulted in a loss of safety function.</br>Currently the bypass valve is closed and the RWL, EOC-RPT and RPS function are operable. Troubleshooting continues to determine the issue with the main turbine that caused the bypass valve to open.</br>NRC Resident Inspector has been notified.
NRC Resident Inspector has been notified. +
22:18:00, 30 April 2017 +
12:59:00, 3 May 2017 +
22:18:00, 30 April 2017 +
On April 30, 2017, at 1818 (EDT), the main … On April 30, 2017, at 1818 (EDT), the main turbine steam bypass valve #1 partially opened. Power was incrementally lowered. While lowering power the bypass valve would shut and then reopen and power would again be lowered. When power was lowered to approximately 74 percent the bypass valve remained closed. During the transient the reactor protection system (RPS) Turbine Stop Valve Closure and Control Valve Fast Closure trip functions were declared inoperable due to the opening of the bypass valve which affects the bypass setpoint for those RPS trip functions. With the loss of these RPS trip functions a loss of safety function existed intermittently for approximately 37 minutes. The manual reactor trip function and other RPS functions remained operable.</br>Both channels of the rod withdrawal limiter (RWL) and the end of cycle reactor recirculation pump trip (EOC-RPT) function were also declared inoperable. These functions are credited in accident analysis, this also resulted in a loss of safety function.</br>Currently the bypass valve is closed and the RWL, EOC-RPT and RPS function are operable. Troubleshooting continues to determine the issue with the main turbine that caused the bypass valve to open.</br>NRC Resident Inspector has been notified.
NRC Resident Inspector has been notified. +
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100 +
00:00:00, 3 May 2017 +
Modification date"Modification date" is a predefined property that corresponds to the date of the last modification of a subject and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
01:42:47, 2 March 2018 +
12:59:00, 3 May 2017 +
true +
false +
2.612 d (62.68 hours, 0.373 weeks, 0.0859 months) +
22:18:00, 30 April 2017 +
URL"URL" is a <a href="/Special:Types/URL" title="Special:Types/URL">type</a> and predefined property provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a> to represent URI/URL values.