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On March 7, 2015, at 2140 CST, with the plOn March 7, 2015, at 2140 CST, with the plant in Mode 5, Refueling, the RSS#2, one of two Reserve Station Service offsite power sources, de-energized. This loss of RSS#2 caused the de-energization of the Division 2 Safety Bus, which caused a valid start signal to the logic of the Division 2 Emergency Diesel Generator. No start occurred, however, due to the diesel being in the maintenance mode. Division 2 Standby Service Water, which was being run for system fill and vent as well as surveillance testing, also lost power.</br>At the time RSS#2 was lost, the Division 2 Diesel generator and Division 2 Standby Service Water were inoperable for the Refuel Outage 18 Division 2 maintenance window.</br>Division 1 systems and RSS#1 were not affected by the power loss and continued to operate normally. There were 5 control building dampers and 1 floor drain air operated valve that repositioned due to the loss of power.</br>The cause of RSS#2 de-energization is still under investigation.</br>The licensee notified the NRC Resident Inspector.ensee notified the NRC Resident Inspector.  +
03:40:00, 8 March 2015  +
50,872  +
05:21:00, 8 March 2015  +
03:40:00, 8 March 2015  +
On March 7, 2015, at 2140 CST, with the plOn March 7, 2015, at 2140 CST, with the plant in Mode 5, Refueling, the RSS#2, one of two Reserve Station Service offsite power sources, de-energized. This loss of RSS#2 caused the de-energization of the Division 2 Safety Bus, which caused a valid start signal to the logic of the Division 2 Emergency Diesel Generator. No start occurred, however, due to the diesel being in the maintenance mode. Division 2 Standby Service Water, which was being run for system fill and vent as well as surveillance testing, also lost power.</br>At the time RSS#2 was lost, the Division 2 Diesel generator and Division 2 Standby Service Water were inoperable for the Refuel Outage 18 Division 2 maintenance window.</br>Division 1 systems and RSS#1 were not affected by the power loss and continued to operate normally. There were 5 control building dampers and 1 floor drain air operated valve that repositioned due to the loss of power.</br>The cause of RSS#2 de-energization is still under investigation.</br>The licensee notified the NRC Resident Inspector.ensee notified the NRC Resident Inspector.  +
Has query"Has query" is a predefined property that represents meta information (in form of a <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Subobject">subobject</a>) about individual queries and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
00:00:00, 8 March 2015  +
Modification date"Modification date" is a predefined property that corresponds to the date of the last modification of a subject and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
01:48:24, 2 March 2018  +
05:21:00, 8 March 2015  +
false  +
false  +
0.07 d (1.68 hours, 0.01 weeks, 0.0023 months)  +
03:40:00, 8 March 2015  +
Specified System Actuation Due to Loss of One Reserve Station Service Offsite Power Source  +
URL"URL" is a <a href="/Special:Types/URL" title="Special:Types/URL">type</a> and predefined property provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a> to represent URI/URL values.
1  +