Browse wiki

Jump to navigation Jump to search
0  +  and 100  +
On April 17, 2014 at 0335 EDT, Secondary COn April 17, 2014 at 0335 EDT, Secondary Containment Zone 3 (Unit 1&2 Reactor Building) differential pressure went to 0.15 inches WG (negative) following securing Unit 1 Zone 3 HVAC in preparation for a LOCA/LOOP test. Zone 3 HVAC was restored at 0420 EDT. Zone I (Unit 1 Reactor Building) ventilation is isolated with secondary containment relaxed for refuel outage on Unit 1. Zone II (Unit 2 Reactor Building) ventilation remained in service and stable.</br>Zone 3 differential pressure recovered to SR 3.6.4.1.1 requirements of 0.25 inches WG (negative) at 0420 EDT and was verified to be stable. LCO 3.6.4.1 was entered at 0335 EDT and exited at 0420 EDT. Tech Spec Secondary Containment Operability requires a negative pressure of at least 0.25 inches water gauge (WG) for all three Reactor Building Ventilation Zones. </br>This event is being reported under 10 CFR 50.72(b)(3)(v)(C) and per the guidance of NUREG-1022 Rev 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment System.</br>The licensee informed the NRC Resident Inspector. licensee informed the NRC Resident Inspector.  +
07:35:00, 17 April 2014  +
50,040  +
06:00:00, 17 April 2014  +
07:35:00, 17 April 2014  +
On April 17, 2014 at 0335 EDT, Secondary COn April 17, 2014 at 0335 EDT, Secondary Containment Zone 3 (Unit 1&2 Reactor Building) differential pressure went to 0.15 inches WG (negative) following securing Unit 1 Zone 3 HVAC in preparation for a LOCA/LOOP test. Zone 3 HVAC was restored at 0420 EDT. Zone I (Unit 1 Reactor Building) ventilation is isolated with secondary containment relaxed for refuel outage on Unit 1. Zone II (Unit 2 Reactor Building) ventilation remained in service and stable.</br>Zone 3 differential pressure recovered to SR 3.6.4.1.1 requirements of 0.25 inches WG (negative) at 0420 EDT and was verified to be stable. LCO 3.6.4.1 was entered at 0335 EDT and exited at 0420 EDT. Tech Spec Secondary Containment Operability requires a negative pressure of at least 0.25 inches water gauge (WG) for all three Reactor Building Ventilation Zones. </br>This event is being reported under 10 CFR 50.72(b)(3)(v)(C) and per the guidance of NUREG-1022 Rev 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment System.</br>The licensee informed the NRC Resident Inspector. licensee informed the NRC Resident Inspector.  +
Has query"Has query" is a predefined property that represents meta information (in form of a <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Subobject">subobject</a>) about individual queries and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
0  +  and 100  +
00:00:00, 17 April 2014  +
Modification date"Modification date" is a predefined property that corresponds to the date of the last modification of a subject and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
01:51:03, 2 March 2018  +
06:00:00, 17 April 2014  +
false  +  and true  +
false  +
-0.0658 d (-1.58 hours, -0.0094 weeks, -0.00216 months)  +
07:35:00, 17 April 2014  +
Loss of Secondary Containment During Preparation for Loca/Loop Testing  +
URL"URL" is a <a href="/Special:Types/URL" title="Special:Types/URL">type</a> and predefined property provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a> to represent URI/URL values.
1  +  and 2  +