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During startup physics testing, the reactoDuring startup physics testing, the reactor operator identified a discrepancy between Group 1 & Group 2 Step Demand Counters for control bank 'B'. Research identified the issue to be associated with failure of a card in the rod control power cabinet. Failure of the card impacts group step counters for control bank 'B', control bank 'D' and shutdown bank 'B.'</br>Inoperability of more than one group step counter per bank placed Unit 2 in a 6-hour clock to hot shutdown as of 0808 hrs 29 November 2009. Consequently, at 1045 hrs, the decision was made to trip Unit 2 reactor. The decision was based on time required to make repairs, complete post maintenance testing requirements, and maintaining proper control of reactivity.</br>All systems functioned as required on the trip and initiation of any auxiliary or emergency systems was not required. Current heat removal is via normal plant alignment following refueling outage activities: steam generator blowdown, main feedwater, and steam generator PORV.</br>All control rods fully inserted on the manual trip.</br>The licensee notified the NRC Resident Inspector. licensee notified the NRC Resident Inspector.  +
15:45:00, 29 November 2009  +
45,528  +
13:31:00, 29 November 2009  +
15:45:00, 29 November 2009  +
During startup physics testing, the reactoDuring startup physics testing, the reactor operator identified a discrepancy between Group 1 & Group 2 Step Demand Counters for control bank 'B'. Research identified the issue to be associated with failure of a card in the rod control power cabinet. Failure of the card impacts group step counters for control bank 'B', control bank 'D' and shutdown bank 'B.'</br>Inoperability of more than one group step counter per bank placed Unit 2 in a 6-hour clock to hot shutdown as of 0808 hrs 29 November 2009. Consequently, at 1045 hrs, the decision was made to trip Unit 2 reactor. The decision was based on time required to make repairs, complete post maintenance testing requirements, and maintaining proper control of reactivity.</br>All systems functioned as required on the trip and initiation of any auxiliary or emergency systems was not required. Current heat removal is via normal plant alignment following refueling outage activities: steam generator blowdown, main feedwater, and steam generator PORV.</br>All control rods fully inserted on the manual trip.</br>The licensee notified the NRC Resident Inspector. licensee notified the NRC Resident Inspector.  +
Has query"Has query" is a predefined property that represents meta information (in form of a <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Subobject">subobject</a>) about individual queries and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
00:00:00, 29 November 2009  +
Modification date"Modification date" is a predefined property that corresponds to the date of the last modification of a subject and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
02:10:46, 2 March 2018  +
13:31:00, 29 November 2009  +
true  +
-0.0929 d (-2.23 hours, -0.0133 weeks, -0.00305 months)  +
15:45:00, 29 November 2009  +
Trip from Intermediate Range Due to Rod Group Demand Counter Discrepancy  +
URL"URL" is a <a href="/Special:Types/URL" title="Special:Types/URL">type</a> and predefined property provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a> to represent URI/URL values.
2  +