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At 0834 on 11-7-08, Oconee Nuclear StationAt 0834 on 11-7-08, Oconee Nuclear Station (ONS) Unit 3 experienced an automatic reactor trip due to a reactor protective systems (RPS) actuation. ONS Unit 3 post trip parameters are normal. Main Feedwater remained in service following the event and Emergency Feedwater was not required and remained available. Electrical power automatically transferred to the Startup power source from the switchyard and emergency AC power sources were not required and remained available. The cause of the RPS actuation and automatic reactor trip are under investigation. </br>ONS Unit 1 remained at 100% power with no issues following the ONS Unit 3 reactor trip. ONS Unit 2 remained in No-Mode. No other safety systems have actuated or exhibited abnormal behavior. Therefore, the safety significance of this condition is low.</br>All control rods fully inserted during this event. The unit is removing decay heat to the main condenser. No primary relief valves lifted and Main Steam relief valves cycled following the trip. There are no Steam Generator tube leaks. </br>The licensee notified the NRC Resident Inspector.ensee notified the NRC Resident Inspector.  +
13:34:00, 7 November 2008  +
44,638  +
12:05:00, 7 November 2008  +
13:34:00, 7 November 2008  +
At 0834 on 11-7-08, Oconee Nuclear StationAt 0834 on 11-7-08, Oconee Nuclear Station (ONS) Unit 3 experienced an automatic reactor trip due to a reactor protective systems (RPS) actuation. ONS Unit 3 post trip parameters are normal. Main Feedwater remained in service following the event and Emergency Feedwater was not required and remained available. Electrical power automatically transferred to the Startup power source from the switchyard and emergency AC power sources were not required and remained available. The cause of the RPS actuation and automatic reactor trip are under investigation. </br>ONS Unit 1 remained at 100% power with no issues following the ONS Unit 3 reactor trip. ONS Unit 2 remained in No-Mode. No other safety systems have actuated or exhibited abnormal behavior. Therefore, the safety significance of this condition is low.</br>All control rods fully inserted during this event. The unit is removing decay heat to the main condenser. No primary relief valves lifted and Main Steam relief valves cycled following the trip. There are no Steam Generator tube leaks. </br>The licensee notified the NRC Resident Inspector.ensee notified the NRC Resident Inspector.  +
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100  +
00:00:00, 7 November 2008  +
Modification date"Modification date" is a predefined property that corresponds to the date of the last modification of a subject and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
22:33:33, 24 September 2017  +
12:05:00, 7 November 2008  +
-0.0617 d (-1.48 hours, -0.00881 weeks, -0.00203 months)  +
13:34:00, 7 November 2008  +
Automatic Reactor Trip  +
URL"URL" is a <a href="/Special:Types/URL" title="Special:Types/URL">type</a> and predefined property provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a> to represent URI/URL values.
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