Browse wiki

Jump to navigation Jump to search
In accordance with 10 CFR 50.72(b)(2)(iv)(In accordance with 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A), this notification reports an automatic reactor trip on Byron Unit 1. The trip occurred following a trip of the Byron Unit 1 East Main Power Transformer (MPT). Initial indications appear that the MPT trip was caused by a large (~ 5 foot) section of ice that fell from a bus bar over the 1E MPT. This ice shorted out a MPT bushing, resulting in the unit trip. Reactor operators performed a manual start of the Auxiliary Feedwater System in response to the unit trip. All other safety systems responded as expected. </br>The plant trip occurred at 1101 CST on March 03, 2015. Unit 1 is presently in Mode 3 and stable. Unit 2, the opposite unit, is operating at 100% power and stable. This condition was entered into the Byron CAP Program. An investigation is in progress to determine the extent of required repairs, if any, required prior to unit restart. </br>This event resulted in the actuation of the Reactor Protection System with a subsequent Reactor Trip and therefore, requires notification to the NRC within 4 hours of discovery in accordance with 10 CFR 50.72(b)(2)(iv)(B). This event resulted in the manual actuation of the Auxiliary Feedwater System and therefore, requires notification to the NRC within 8 hours of discovery in accordance with 10 CFR 50.72(b)(3)(iv)(A). </br>This ENS call will be followed up with a Licensee Event Report (LER) within 60 days.</br>All rods inserted during reactor trip, offsite power and emergency power sources are currently available and decay heat is being removed via the startup feedwater systems. No safety relief valves lifted as a result of the transient.</br>The NRC Resident Inspector and the State of Illinois were notified.r and the State of Illinois were notified.  +
17:01:00, 3 March 2015  +
50,859  +
14:21:00, 3 March 2015  +
17:01:00, 3 March 2015  +
In accordance with 10 CFR 50.72(b)(2)(iv)(In accordance with 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A), this notification reports an automatic reactor trip on Byron Unit 1. The trip occurred following a trip of the Byron Unit 1 East Main Power Transformer (MPT). Initial indications appear that the MPT trip was caused by a large (~ 5 foot) section of ice that fell from a bus bar over the 1E MPT. This ice shorted out a MPT bushing, resulting in the unit trip. Reactor operators performed a manual start of the Auxiliary Feedwater System in response to the unit trip. All other safety systems responded as expected. </br>The plant trip occurred at 1101 CST on March 03, 2015. Unit 1 is presently in Mode 3 and stable. Unit 2, the opposite unit, is operating at 100% power and stable. This condition was entered into the Byron CAP Program. An investigation is in progress to determine the extent of required repairs, if any, required prior to unit restart. </br>This event resulted in the actuation of the Reactor Protection System with a subsequent Reactor Trip and therefore, requires notification to the NRC within 4 hours of discovery in accordance with 10 CFR 50.72(b)(2)(iv)(B). This event resulted in the manual actuation of the Auxiliary Feedwater System and therefore, requires notification to the NRC within 8 hours of discovery in accordance with 10 CFR 50.72(b)(3)(iv)(A). </br>This ENS call will be followed up with a Licensee Event Report (LER) within 60 days.</br>All rods inserted during reactor trip, offsite power and emergency power sources are currently available and decay heat is being removed via the startup feedwater systems. No safety relief valves lifted as a result of the transient.</br>The NRC Resident Inspector and the State of Illinois were notified.r and the State of Illinois were notified.  +
Has query"Has query" is a predefined property that represents meta information (in form of a <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Subobject">subobject</a>) about individual queries and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
4.62963e-5 d (0.00111 hours, 6.613757e-6 weeks, 1.522e-6 months)  +  and 9.259259e-5 d (0.00222 hours, 1.322751e-5 weeks, 3.044e-6 months)  +
00:00:00, 3 March 2015  +
Modification date"Modification date" is a predefined property that corresponds to the date of the last modification of a subject and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
01:48:26, 2 March 2018  +
14:21:00, 3 March 2015  +
-0.111 d (-2.67 hours, -0.0159 weeks, -0.00366 months)  +
17:01:00, 3 March 2015  +
Automatic Reactor Trip Due to Main Power Transformer Bushing Short  +
URL"URL" is a <a href="/Special:Types/URL" title="Special:Types/URL">type</a> and predefined property provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a> to represent URI/URL values.
1  +