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The Perry Nuclear Power Plant is reportingThe Perry Nuclear Power Plant is reporting an event or condition pursuant to 10 CFR 50.72(b)(3)(v)(D).</br>On April 16, 2013, at 2323 EDT, it was identified that Emergency Service Water (ESW) pump 'A' was inoperable due to an inability to maintain minimum flow requirements. As a result, ESW 'A' and the supported Division 1 Emergency Diesel Generator (EDG) were declared inoperable. Coincident with this discovery, a test of the Division 2 emergency systems was in progress with the associated ESW 'B' pump and Division 2 EDG inoperable. Division 2 EDG was available to support the Shutdown Defense In-Depth Strategy. Division 3 EDG was operable and could supply High Pressure Core Spray system injection, if needed.</br>Both EDGs were inoperable simultaneously and Technical Specification 3.8.2 'AC Sources-Shutdown' was entered and required actions taken. These actions included immediately suspending core alterations and immediately initiating actions to restore the required EDG. The test of Division 2 emergency systems was suspended and ESW 'B' and the Division 2 EDG were restored to operable status at 0135 EDT on April 17, 2013.</br>The failure of ESW 'A' minimum flow is currently under investigation.</br>The Resident Inspector has been notified.</br>* * * RETRACTION FROM JOHN PELCIC TO CHARLES TEAL ON 4/20/13 AT 1355 EDT * * *</br>Engineering personnel performed an immediate investigation of the ESW 'A' minimum flow condition. The investigation results showed that the ESW 'A' pump flow exceeded the minimum flow requirement to protect the ESW 'A' system. Therefore, continued operation of ESW 'A' was acceptable and the minimum flow condition originally reported did not cause the Division 1 Emergency Diesel Generator to be inoperable.</br>The condition would not have prevented the fulfillment of a safety function to mitigate the consequences of an accident. Reporting is not required under 10 CFR 50.72(b)(3)(v)(D) and this notification is retracted. </br>The NRC Resident Inspector has been notified.</br>Notified R3DO (Orth).r has been notified. Notified R3DO (Orth).  
03:23:00, 17 April 2013  +
48,937  +
05:20:00, 17 April 2013  +
03:23:00, 17 April 2013  +
The Perry Nuclear Power Plant is reportingThe Perry Nuclear Power Plant is reporting an event or condition pursuant to 10 CFR 50.72(b)(3)(v)(D).</br>On April 16, 2013, at 2323 EDT, it was identified that Emergency Service Water (ESW) pump 'A' was inoperable due to an inability to maintain minimum flow requirements. As a result, ESW 'A' and the supported Division 1 Emergency Diesel Generator (EDG) were declared inoperable. Coincident with this discovery, a test of the Division 2 emergency systems was in progress with the associated ESW 'B' pump and Division 2 EDG inoperable. Division 2 EDG was available to support the Shutdown Defense In-Depth Strategy. Division 3 EDG was operable and could supply High Pressure Core Spray system injection, if needed.</br>Both EDGs were inoperable simultaneously and Technical Specification 3.8.2 'AC Sources-Shutdown' was entered and required actions taken. These actions included immediately suspending core alterations and immediately initiating actions to restore the required EDG. The test of Division 2 emergency systems was suspended and ESW 'B' and the Division 2 EDG were restored to operable status at 0135 EDT on April 17, 2013.</br>The failure of ESW 'A' minimum flow is currently under investigation.</br>The Resident Inspector has been notified.</br>* * * RETRACTION FROM JOHN PELCIC TO CHARLES TEAL ON 4/20/13 AT 1355 EDT * * *</br>Engineering personnel performed an immediate investigation of the ESW 'A' minimum flow condition. The investigation results showed that the ESW 'A' pump flow exceeded the minimum flow requirement to protect the ESW 'A' system. Therefore, continued operation of ESW 'A' was acceptable and the minimum flow condition originally reported did not cause the Division 1 Emergency Diesel Generator to be inoperable.</br>The condition would not have prevented the fulfillment of a safety function to mitigate the consequences of an accident. Reporting is not required under 10 CFR 50.72(b)(3)(v)(D) and this notification is retracted. </br>The NRC Resident Inspector has been notified.</br>Notified R3DO (Orth).r has been notified. Notified R3DO (Orth).  
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