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This is an non-emergency event notificatioThis is an non-emergency event notification to the NRCOC in Accordance with 10 CFR 50.72(b)(2)(iv)(B) for a valid actuation of the Reactor Protection System (RPS) (four hour notification) and 10 CFR 50.72(b)(3)(iv)(A) for a valid Engineered Safeguards (ESF) actuation due to Auxiliary Feedwater (AFW) initiation (eight hour notification).</br>On 2/18/2013 at 0055 Unit 3 commenced a unit shutdown due to high # 1 seal leak-off on the 3A Reactor Coolant Pump (RCP). At 0129 3A RCP #1 seal leak-off exceeded operating limits. Unit 3 reactor was manually tripped. Auxiliary feedwater actuated as designed based on steam generator levels as a result of the trip. Unit 3 is currently in Mode 3 and stable. </br>No complications were noted as a result of the reactor trip. Steam generator levels are being returned to normal level following the reactor trip. All other plant systems functioned as designed during and after the reactor trip. 3A RCP high #1 seal leak-off is under investigation.</br>All control rods fully inserted on the trip. Decay heat was removed by AFW to the steam generators out the atmospheric reliefs. There was no primary to secondary leakage. Electrical buses are being supplied via offsite power.</br>The licensee notified the NRC Resident Inspector.ensee notified the NRC Resident Inspector.  +
06:31:00, 18 February 2013  +
48,764  +
03:19:00, 18 February 2013  +
06:31:00, 18 February 2013  +
This is an non-emergency event notificatioThis is an non-emergency event notification to the NRCOC in Accordance with 10 CFR 50.72(b)(2)(iv)(B) for a valid actuation of the Reactor Protection System (RPS) (four hour notification) and 10 CFR 50.72(b)(3)(iv)(A) for a valid Engineered Safeguards (ESF) actuation due to Auxiliary Feedwater (AFW) initiation (eight hour notification).</br>On 2/18/2013 at 0055 Unit 3 commenced a unit shutdown due to high # 1 seal leak-off on the 3A Reactor Coolant Pump (RCP). At 0129 3A RCP #1 seal leak-off exceeded operating limits. Unit 3 reactor was manually tripped. Auxiliary feedwater actuated as designed based on steam generator levels as a result of the trip. Unit 3 is currently in Mode 3 and stable. </br>No complications were noted as a result of the reactor trip. Steam generator levels are being returned to normal level following the reactor trip. All other plant systems functioned as designed during and after the reactor trip. 3A RCP high #1 seal leak-off is under investigation.</br>All control rods fully inserted on the trip. Decay heat was removed by AFW to the steam generators out the atmospheric reliefs. There was no primary to secondary leakage. Electrical buses are being supplied via offsite power.</br>The licensee notified the NRC Resident Inspector.ensee notified the NRC Resident Inspector.  +
Has query"Has query" is a predefined property that represents meta information (in form of a <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Subobject">subobject</a>) about individual queries and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
100  +
00:00:00, 18 February 2013  +
Modification date"Modification date" is a predefined property that corresponds to the date of the last modification of a subject and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
02:01:46, 2 March 2018  +
03:19:00, 18 February 2013  +
true  +
-0.133 d (-3.2 hours, -0.019 weeks, -0.00438 months)  +
06:31:00, 18 February 2013  +
Manual Reactor Trip Due to High Seal Leakoff on Reactor Coolant Pump 3A  +
URL"URL" is a <a href="/Special:Types/URL" title="Special:Types/URL">type</a> and predefined property provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a> to represent URI/URL values.
3  +