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At 1710 EDT, Unit 1 was manually tripped dAt 1710 EDT, Unit 1 was manually tripped due to two dropped control rods. All CEAs (Control Element Assemblies) fully inserted on the trip. Steam generator level control responded as expected and no pressurizer or power operated relief valves opened. RCS heat removal is being maintained by main feedwater and steam bypass control systems. All other systems functioned normally and the plant has stabilized at normal operating temperature and pressure in Mode 3. This non-emergency notification is being made pursuant 10 CFR 50.72(b)(2)(iv)(B) due to manual actuation of RPS.</br>The licensee characterized the manual trip as uncomplicated. The second rod dropped within a very short time of the first rod. The cause of the rod drops is still under investigation. The licensee noted that no activities involving the rod control system were in progress when the event occurred. The licensee was at 45% as part of its post outage power ascension unrelated to the rod drop. The manual reactor trip action was taken per procedure when the second rod dropped. The reactor trip had no impact on Unit 2 operation.</br>The NRC Resident Inspector has been notified. NRC Resident Inspector has been notified.  +
21:10:00, 16 June 2010  +
46,018  +
19:20:00, 16 June 2010  +
21:10:00, 16 June 2010  +
At 1710 EDT, Unit 1 was manually tripped dAt 1710 EDT, Unit 1 was manually tripped due to two dropped control rods. All CEAs (Control Element Assemblies) fully inserted on the trip. Steam generator level control responded as expected and no pressurizer or power operated relief valves opened. RCS heat removal is being maintained by main feedwater and steam bypass control systems. All other systems functioned normally and the plant has stabilized at normal operating temperature and pressure in Mode 3. This non-emergency notification is being made pursuant 10 CFR 50.72(b)(2)(iv)(B) due to manual actuation of RPS.</br>The licensee characterized the manual trip as uncomplicated. The second rod dropped within a very short time of the first rod. The cause of the rod drops is still under investigation. The licensee noted that no activities involving the rod control system were in progress when the event occurred. The licensee was at 45% as part of its post outage power ascension unrelated to the rod drop. The manual reactor trip action was taken per procedure when the second rod dropped. The reactor trip had no impact on Unit 2 operation.</br>The NRC Resident Inspector has been notified. NRC Resident Inspector has been notified.  +
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00:00:00, 16 June 2010  +
Modification date"Modification date" is a predefined property that corresponds to the date of the last modification of a subject and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
22:30:04, 24 September 2017  +
19:20:00, 16 June 2010  +
true  +
-0.0763 d (-1.83 hours, -0.0109 weeks, -0.00251 months)  +
21:10:00, 16 June 2010  +
Manual Reactor Trip After Two Control Rods Dropped  +
URL"URL" is a <a href="/Special:Types/URL" title="Special:Types/URL">type</a> and predefined property provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a> to represent URI/URL values.
1  +