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On 12/25/07 at 2110 hours EST, Unit 2 tripOn 12/25/07 at 2110 hours EST, Unit 2 tripped from 100% power due to a trip of the 'B' Reactor Coolant Pump. The reactor trip 1st out annunciator was 'Loss of flow, power >30%'. All control rods fully inserted. This event is reportable per 10 CFR 50.72(b)(2)(iv)(B). The Auxiliary Feedwater (AFW) pumps auto started due to the event and the steam driven AFW pump subsequently tripped on overspeed. The steam driven AFW pump was reset and placed in service. The ESF (Engineered Safety Function) actuation is reportable per 10 CFR 50.72(b)(3)(iv)(A). The unit is currently in mode 3 and (the licensee is) investigating the cause of the ground on the 'B' reactor coolant pump.</br>The plant is at normal operating pressure and temperature. The electrical grid is stable and supplying plant loads through the startup transformer. Decay heat is being removed via the steam dumps to the condenser with feedwater being supplied via the normal path. </br>The licensee has notified the NRC Resident Inspector.nsee has notified the NRC Resident Inspector.  +
02:10:00, 26 December 2007  +
43,866  +
23:22:00, 25 December 2007  +
02:10:00, 26 December 2007  +
On 12/25/07 at 2110 hours EST, Unit 2 tripOn 12/25/07 at 2110 hours EST, Unit 2 tripped from 100% power due to a trip of the 'B' Reactor Coolant Pump. The reactor trip 1st out annunciator was 'Loss of flow, power >30%'. All control rods fully inserted. This event is reportable per 10 CFR 50.72(b)(2)(iv)(B). The Auxiliary Feedwater (AFW) pumps auto started due to the event and the steam driven AFW pump subsequently tripped on overspeed. The steam driven AFW pump was reset and placed in service. The ESF (Engineered Safety Function) actuation is reportable per 10 CFR 50.72(b)(3)(iv)(A). The unit is currently in mode 3 and (the licensee is) investigating the cause of the ground on the 'B' reactor coolant pump.</br>The plant is at normal operating pressure and temperature. The electrical grid is stable and supplying plant loads through the startup transformer. Decay heat is being removed via the steam dumps to the condenser with feedwater being supplied via the normal path. </br>The licensee has notified the NRC Resident Inspector.nsee has notified the NRC Resident Inspector.  +
Has query"Has query" is a predefined property that represents meta information (in form of a <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Subobject">subobject</a>) about individual queries and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
0.0244 d (0.586 hours, 0.00349 weeks, 8.02855e-4 months)  +
00:00:00, 25 December 2007  +
Modification date"Modification date" is a predefined property that corresponds to the date of the last modification of a subject and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
02:15:22, 2 March 2018  +
23:22:00, 25 December 2007  +
-0.117 d (-2.8 hours, -0.0167 weeks, -0.00384 months)  +
02:10:00, 26 December 2007  +
Automatic Reactor Trip Due to Trip of "B" Reactor Coolant Pump  +
URL"URL" is a <a href="/Special:Types/URL" title="Special:Types/URL">type</a> and predefined property provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a> to represent URI/URL values.
2  +