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On February 11, 2015, at 0820 Central StanOn February 11, 2015, at 0820 Central Standard Time, Brown's Ferry Nuclear Plant (BFN), Unit 3, declared the High Pressure Coolant Injection (HPCI) and Reactor Core Isolation Cooling (RCIC) systems inoperable due to no suction source aligned. During surveillance testing, the Condensate Storage Tank (CST) emergency discharge isolation valve energized and closed when the breaker was closed, isolating both systems from their suction source. It was subsequently determined that maintenance task. Operations personnel re-opened the isolation valve using the hand switch in the Control Room, restoring operability to the HPCI and RCIC systems.</br></br>The apparent cause of this event was inadequate design review of a 2010 plant modification which allowed latent design vulnerabilities to be introduced into the plant.</br></br>The corrective actions to reduce the probability of a similar event occurring in the future were to remove thermal overload heaters from the affected breakers, preventing valve closure when these breakers are closed; to review a sample of recent engineering change packages for quality of Design Review; to repair a faulty hand switch; and to implement a design change for the CST isolation valves for all three BFN units to prevent spurious operation of the isolation valve when the associated breaker is closed.lve when the associated breaker is closed.  +
April 13, 2015  +
February 11, 2015  +
On February 11, 2015, at 0820 Central StanOn February 11, 2015, at 0820 Central Standard Time, Brown's Ferry Nuclear Plant (BFN), Unit 3, declared the High Pressure Coolant Injection (HPCI) and Reactor Core Isolation Cooling (RCIC) systems inoperable due to no suction source aligned. During surveillance testing, the Condensate Storage Tank (CST) emergency discharge isolation valve energized and closed when the breaker was closed, isolating both systems from their suction source. It was subsequently determined that maintenance task. Operations personnel re-opened the isolation valve using the hand switch in the Control Room, restoring operability to the HPCI and RCIC systems.</br></br>The apparent cause of this event was inadequate design review of a 2010 plant modification which allowed latent design vulnerabilities to be introduced into the plant.</br></br>The corrective actions to reduce the probability of a similar event occurring in the future were to remove thermal overload heaters from the affected breakers, preventing valve closure when these breakers are closed; to review a sample of recent engineering change packages for quality of Design Review; to repair a faulty hand switch; and to implement a design change for the CST isolation valves for all three BFN units to prevent spurious operation of the isolation valve when the associated breaker is closed.lve when the associated breaker is closed.  +
2,015  +
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12:43:29, 23 July 2016  +
April 13, 2015  +
February 11, 2015  +
High Pressure Coolant Injection and Reactor Core Isolation Cooling Inoperable Due To No Suction Source Aligned  +
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