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 Entered dateEvent description
ENS 521545 August 2016 06:26:00At 2240 CDT on August 4, 2016, it was discovered that the floor between the cable spreading room and the plant administration building (PAB) basement is not a credited Appendix R fire barrier. Because the cable spreading room and the plant administration building are located in the same fire area, a fire in the PAB could spread to the cable spreading room requiring evacuation of the control room. The travel path used to access the Alternate Shutdown Panel following control room evacuation traverses the same fire area in the PAB. Therefore, this event is being reported under 10 CFR 50.72(b)(3)(ii) for Degraded or Unanalyzed Condition as a fire in the PAB could have the potential to impact Division 1 equipment as well as impede the Operators ability to access Division 2 safe shutdown equipment. Fire watches have been established. There is no impact to the health and safety of the public. The NRC Resident Inspector has been notified. The licensee will notify the State of Minnesota.
ENS 5070529 December 2014 03:40:00While the 12 Emergency Diesel Generator (EDG) was inoperable for performance of the monthly surveillance, adjustments were inadvertently made to 11 EDG which made it inoperable. As a result, Technical Specification (TS) 3.8.1 Condition E, for both EDG's inoperable was entered. Monticello has subsequently restored 12 EDG to an operable status within the 2 hour TS LCO (Limiting Condition for Operation) completion timer requirement. The station remained in a safe condition during this discovery with 12 EDG available at all times. The plant continues to operate in a normal condition with no initiating events present. The health and safety of the public was not impacted as a result of this condition. The NRC Resident Inspector has been notified. EDG 12 was restored to operable status at 2214 CST and EDG 11 will remain inoperable until a surveillance test is performed to start the EDG and restore the local governor control idle speed to the correct setting. The licensee will be notifying the Minnesota State Duty Officer.
ENS 5066310 December 2014 00:31:00

At 1830 (CST) on December 9, 2014 Door 410B, a HELB (High Energy Line Break) door between the east and west sides of the ground floor of the reactor building, was found closed. This door is one half of a pair of double doors that are normally open to provide a HELB energy and flooding release path to mitigate postulated HELB events. The closed HELB door has the potential to impact safe shutdown by exposing both divisions of safe shutdown components to unanalyzed environmental conditions. With the potential loss of both divisions of safe shutdown equipment, no safe shutdown path would exist. This condition is being reported as an unanalyzed condition as defined by (10 CFR) 50.72(b)(3)(ii)(B). The HELB door was immediately opened and returned to normal configuration. Door 410A remained open during the time that Door 410B was closed and provided an available, but not yet analyzed, release path that could have mitigated the consequences of this event. The health and safety of the general public was not impacted as a result of this condition. The NRC Resident Inspector has been notified.

  • * * RETRACTION FROM JON LAUDENBACH TO CHARLES TEAL ON 1/30/15 AT 1513 EST * * *

Further analysis has determined that the condition did not significantly degrade plant safety. Door 410B in the Reactor Building was found closed. This door is one half of a pair of double door (Doors 410A and 410B) that normally open to provide a High Energy Line Break (HELB) energy and flooding release path to mitigate postulated HELB events. The condition of one half of the double door closed was not previously analyzed. A subsequent completed engineering evaluation analyzed this condition, Door 410B being closed and Door 410A being open, for the following environmental conditions: peak compartment temperatures, block wall differential pressure, radiation dose, and flooding. The environmental conditions found the Reactor Building in response to Door 410B being closed with 410A being open does not affect the operability of safety related equipment housed within the Reactor Building or the ability to safely shut-down the plant and maintain the plant shutdown condition following a HELB event. The NRC Resident Inspector has been notified. Notified R3DO (Dickson).

ENS 503455 August 2014 20:53:00The Division 1 Control Room Emergency Filtration System (CREF) was inoperable for scheduled replacement of charcoal. During the scheduled maintenance, Division 2 CREF was placed into service. Approximately 5 minutes after startup (1446 CDT on 8/5/2014), the Division 2 CREF recirculation fan tripped off for unknown reasons. This rendered both trains of CREF inoperable. This required entry into Technical Specification TS 3.0.3. This is being reported pursuant to 10 CFR 50.72(b)(3)(v)(D) as an event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to (D) Mitigate the consequences of an accident. At 1707 CDT on 8/5/2014, the Division 1 CREF train maintenance was completed and the Division 1 CREF was declared operable. TS 3.0.3 was exited at this time. Investigation is in progress to determine the cause of the Division 2 CREF trip. The control room boundary was not challenged during this time period with any change in radiation levels as plant operation was unaffected. Thus, the health and safety of the public was not affected. The licensee notified the NRC Resident Inspector and the State of Minnesota Duty Officer.
ENS 480725 July 2012 21:24:00

At 1258 CDT on 07/05/2012, Operations was notified that both panels of Door 45 (south doors for the reactor building railroad bay airlock) were blocked by a man lift. Blocking both doors represents an unanalyzed condition as a flow path through the door is assumed for pressure relief during postulated HELB events. The man lift was immediately removed correcting the situation and all work related to Door 45 was stopped. Door 45 was blocked for approximately 20 minutes. The NRC Resident Inspector has been notified.

  • * * RETRACTION FROM BART BLAKESLEY TO DONALD NORWOOD AT 1605 EDT ON 8/31/2012 * * *

The purpose of this notification is to retract the previous Event Notification Report (#48072) made by the Monticello Nuclear Generating Plant on 7/5/2012. The initial report indicated that blocking both panels of the railroad bay doors by a man lift represented an unanalyzed condition, as a flow path through the door is assumed for pressure relief during postulated HELB events, and was reported in accordance with 10CFR50.72(b)(3)(ii)(B), Unanalyzed Condition. Since the initial report, Engineering has completed an evaluation that demonstrates equipment supporting safe shutdown would have been capable of performing their specified design function during postulated HELB events. Based on this analysis, the condition initially reported in EN #48072 did not result in an unanalyzed condition that significantly degraded plant safety and is therefore retracted. The NRC Resident Inspector has been informed of this retraction. Notified R3DO (Cameron).

ENS 4533810 September 2009 13:06:00

The Minnesota State Pollution Control Agency and State Department of Emergency Management were notified today, September 10, 2009, that Monticello did not meet the National Pollutant Discharge Elimination System (NPDES) Permit. Samples from a new monitoring well near the reactor building showed low levels of tritium greater than normal background but below Environmental Protection Agency drinking water standards. The concentration of tritium is below any radiological reporting levels established in station procedures. No elevated levels have been detected in any of the other permanent plant monitoring wells. Therefore, we have no indications that there has been a release of tritium beyond the site from this source. The station will continue to monitor, sample and investigate the source of the tritium. The licensee notified the NRC Resident Inspector.

  • * * UPDATE FROM B. CALLSTROM TO V. KLCO AT 1201 ON 9/12/2009 * * *

A subsequent water sample from a new monitoring well near the reactor building indicated a level of 21,300 picocuries/liter of tritium which is slightly above the Environmental Protection Agency drinking water standard for tritium of 20,000 picocuries/liter. No elevated levels have been detected in any of the other permanent plant monitoring wells. Therefore, (the licensee has) no indication that there has been a release of tritium beyond the site from this source. The station will continue to monitor, sample and investigate the source of the tritium. This poses no immediate safety concern for plant employees or the general public. The licensee notified the NRC Resident Inspector. Notified the R3DO (Ring).

ENS 452475 August 2009 15:34:00

On 8/6/09 at 0600 hours CDT the Monticello Nuclear Generating Plant's Technical Support Center uninterruptable power supply will be isolated to perform a planned maintenance activity. The maintenance activity requires implementation of compensatory measures to maintain TSC functions during the activity. The compensatory measures include having the Emergency Director report to the Control Room and co-locating the remaining TSC staff at the EOF should an event be declared requiring ERO activation. The ERO has previously successfully demonstrated the ability to implement these compensatory measures. The maintenance activity is scheduled to be completed with the TSC returned to full functionality by the end of the dayshift on 8/6/09. The Site Emergency Response Organization has been notified of the maintenance activity and instructed on the planned compensatory measures to be implemented during the activity. MNGP will notify the NRC upon completion of the activity restoring full TSC operability. This event is considered reportable per 10CFR50.72(b)(3)(iii). The licensee has notified the NRC Resident Inspector.

* * * UPDATE FROM D. BARNETT TO P. SNYDER AT 1943 ON 8/6/09 * * * 

On 8/6/09 at 1700 CDT the Monticello Nuclear Generating Plant's Technical Support Center was returned to service and declared functional. The Monticello Emergency Response Organization has been notified and the compensatory measures that were in effect have been terminated. The licensee has notified the NRC Resident Inspector. Notified R3DO (Skokowski).

ENS 4506013 May 2009 02:36:00The equalizing valve for one of the four Main Steam Line (MSL) Flow - High differential pressure switches on the 'B' MSL was leaking through. The leak effectively reduced the differential pressure across all four MSL Flow - High valves on the 'B' MSL. This reduction in differential pressure thus potentially would not allow the switches to isolate the 'B' MSL at the required setpoint. This switch was for group 1 isolation. This loss of safety function was restored by isolating the faulty valve block for DPIS-2-117A. All other switches are now reading normally. The repairs for the faulty valve are in progress. The licensee will notify NRC Resident Inspector, State, and local authorities.
ENS 4472315 December 2008 22:47:00

At 1616 on 12/15/08, a plant heating boiler trip resulted in a loss of a reactor building ventilation. The loss of reactor building ventilation resulted in maximum average main steam chase temperatures greater than or equal to 165F. High energy line break (HELB) analysis of piping in the steam chase assumes an initial average temperature prior to the break of 165F. Temperature greater than or equal to 165F in the steam chase challenges EQ qualification of the piping analysis. Abnormal procedures for loss heating boiler and ventilation system failure were entered. C.3 (Shutdown) and C.5-1300 (secondary containment control) were also entered. The plant heating boiler was restarted and ventilation restored prior to power reduction. All systems have been returned to normal. The licensee notified the NRC Resident Inspector.

  • * * RETRACTION PROVIDED FROM DAVID BARNETT TO JOE O'HARA AT 1158 ON 2/6/09 * * *

The licensee is retracting this report based on the following: Monticello is retracting the event reported based on further evaluation, which found that the issue was not an unanalyzed condition that seriously degraded plant safety. The investigation of the event found the peak temperature achieved was 167.2 degrees F and the condition lasted for approximately 11 minutes. Engineering review of Safety System Components found no impact on the equipment for the temperature reached, Additionally, revised High Energy Line Break (HELB) calculations performed with an initial average Steam Chase Room temperature of 180 degrees F before a HELB determined that Safety System components could perform their safety functions. The station has identified the cause for the event and corrective actions will be tracked in the station's corrective action program. Since there was no impact on the equipment in either Environmental Qualification (EQ) or safety function, the temperature of the event was less than the revised calculation temperature, and the unanalyzed condition that existed in the initial event notification report no longer exists and did not result in a condition that seriously degraded plant safety, this event can be retracted. The licensee informed the NRC Resident Inspector. Notified R3DO (Ring).

ENS 446336 November 2008 14:47:00On November 6, 2008 at 11:15, Operations was notified that results of an October 20, 2008 oil and grease weekly sample from a plant sump discharge to the Mississippi River exceeded the National Pollution Discharge Elimination System (NPDES) daily maximum allowable value of 15ppm. The October monthly average oil and grease NPDES of 10ppm was also exceeded. The Minnesota Pollution Control Agency is being notified. The licensee notified the NRC Resident Inspector.
ENS 4421113 May 2008 19:13:00Monticello Nuclear Generating Plant is making a telephone report in accordance with 10 CFR 50.73(a)(2)(iv)(A) Invalid Partial Actuation of the Standby Gas Treatment and Secondary Containment Isolation Systems due to an inappropriate operator action. This report is being made in lieu of a written Licensee Event Report. At 0825 on 04/03/2008, an operator was performing an annunciator test of the Control Room panels and inappropriately pushed the 'A' Standby Gas Treatment system 'Test' pushbutton instead of the 'Lamp Test' pushbutton. He then immediately pushed the 'Reset' pushbutton which reset the Standby Gas Treatment train. The inappropriate actuation of the 'A' Standby Gas Treatment System resulted in the 'A' train momentarily starting, causing ventilation fans V-EF-10 and V-MZ-6 to trip. The immediate resetting of the system by depressing the 'Reset' pushbutton prevented a full secondary containment isolation. All systems started and functioned successfully. The cause of the invalid signal was the operator actuating the system by depressing the 'Test' pushbutton instead of the 'Lamp Test' pushbutton. The NRC Resident Inspector was notified of this event report. After the invalid actuation was completed, all systems affected were reset and returned to normal lineup.
ENS 4143623 February 2005 19:20:00

The licensee provided via facsimile the following report:

During an extent of condition review of the corrective actions associated (with) Event Notification #41374, the Monticello Nuclear Generating Plant (MNGP) engineering staff made the following discovery.  On February 22, 2005 at 12:00 hours, MNGP discovered a potential vulnerability with Alternate Shutdown System (ASDS) isolation design which could result in Bus 16 being locked out in the event of a Control Room or Cable Spreading Room fire.  The Monticello Appendix R Safe Shutdown Analysis for Control Room/Cable Spreading Room fire assumes a loss of control of Division I and II equipment from the Control Room, however, safe shutdown is achieved remotely from the ASDS panel.  ASDS design is such that a Control Room/Cable Spreading Room fire would not impede the ability to safely shutdown and maintain the plant in a shutdown condition.  

Contrary to the ASDS design, it was discovered that an un-isolated metering circuit from the 1AR transformer could result in Bus 16 being locked out in the event of a Control Room or Cable Spreading Room fire. The bus lockout relay from the 1AR transformer is not isolated by the ASDS transfer switches, therefore, this condition could result in failure of Bus 16 to re-energize during the implementation of the Shutdown Outside Control Room procedure. Since the Bus 16 feeder breaker from the 1AR transformer is not required at this time, it has been isolated from the safeguards bus to preclude occurrences of this event. The event is being reported as a potential loss of safety function (10CFR50.72(b)(v)(A,B and D) and as a degraded or unanalyzed condition (10CFR50.72(b)(3)(ii)(B)). The licensee informed NRC Resident Inspector.