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 Entered dateEvent description
ENS 5244117 December 2016 05:43:00

At approximately 1400 CST on 12/16/16, during the performance of VEF-38A Lead Penetration Room Ventilation System (PRVS) Exhaust Fan Monthly Test, flow was found to be at 2000 SCFM with an operability limit of 1620 to 1980 SCFM. VEF-38A was declared inoperable. Unit 1 entered Technical Specification Limiting Condition for Operation (LCO) 3.7.11 Condition C for both trains of PRVS inoperable. With VEF-38A aligned as the lead fan and capable of auto-start, the operable standby fan (VEF-38B) would not have started. During the time that VEF-38A was inoperable and capable of auto-starting, the Unit 1 PRVS was in a condition that could have prevented the control of the release of radioactive material. At 1546 CST on 12/16/16, Unit 1 rendered VEF-38A incapable of auto starting by placing its hand switch in PULL-TO-LOCK. Unit 1 Entered LCO 3.7.11 condition A for one PRVS train inoperable and Exited LCO 3.7.11 Condition C. This is a notification per 10 CFR 50.72(b)(3)(v) for a condition that could have prevented the control of the release of radioactive material. The licensee has notified the NRC Resident Inspector.

  • * * UPDATE ON 2/7/17 AT 1528 EST FROM BUCHANON DICKSON TO DONG PARK * * *

EN 52441 was initiated on December 16, 2016, when the VEF-38A fan flow was found to be in excess of the procedurally defined operability limit during the monthly lead penetration room ventilation system test. The revision of the procedure in use at the time had inadvertently included acceptance criterion for fan air flow in the monthly supplements. The monthly tests demonstrate the flow paths for the two trains are functional and open, but they are not performed in the designed Engineered Safeguards (ES) configuration. The monthly tests do not secure the normal supply and exhaust ventilation within the penetration room boundaries; therefore, flow may be outside limits required during the ES configuration. The 18 month surveillance, which measures the flowrate of the system while in the ES configuration, was completed in April 2016. The surveillance verified the system's operability. The systems have not been modified or altered since this surveillance; therefore the measured flowrate remains the same. The procedure has been revised subsequent to this event to remove the flowrate as an 'acceptance criterion' for the monthly test. Because the VEF-38A flow did not result in fan inoperability, both fan trains remained operable; therefore, ANO-1 did not lose a safety function to control a radioactive release. Based on that, conclusion EN 52441 is being retracted. The licensee will notify the NRC Resident Inspector. Notified R4DO (Warnick).

ENS 5219524 August 2016 12:15:00During performance of an extent of condition evaluation of protection for Technical Specification (TS) equipment from the damaging effects of tornados, Arkansas Nuclear One, Unit 1, identified non-conforming conditions in the plant design such that specific TS equipment on Unit 1 is considered to not be adequately protected from tornado missiles. The reportable condition is postulated by tornado missiles entering the Unit 1 Cable Spreading Room through penetrating the hollow metal door or potentially from spalling of the block wall separating Room 96 and 97. A tornado could generate multiple missiles capable of striking the Unit 1 Cable Spreading Room and rendering both safety related electrical trains inoperable. This condition is reportable per 10 CFR 50.72(b)(3)(ii)(B) for any event or condition that results in the nuclear power plant being in an unanalyzed condition that significantly degrades plant safety, and per 10 CFR 50.72(b)(3)(v) for any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to (A) Shut down the reactor and maintain it in a safe shutdown condition, (B) Remove residual heat, or (D) Mitigate the consequences of an accident. This condition was identified as part of an on-going extent of condition review of potential tornado missile related site impacts. Licensee Event Report (LER) 50-313/2016-002-00 was recently submitted addressing previously identified tornado missile vulnerabilities at the Unit 1 plant. Enforcement discretion per Enforcement Guidance Memorandum EGM 15-002 has been implemented and required actions taken. Corrective actions will be documented in a follow-on licensee event report. The licensee has notified the NRC Resident Inspector.
ENS 517114 February 2016 18:50:00A non-licensed supervisor tested positive for a drugs during a random Fitness for Duty test. The individual's access to the plant has been suspended. The NRC Resident Inspector has been informed.