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 Entered dateEvent description
ENS 5429930 September 2019 01:22:00On September 29, 2019 at 2228 EDT, during a planned swap of Reactor Building HVAC trains, the exhaust fan discharge damper for the train being removed from service failed to close when the train was shutdown, which resulted in the Technical Specification (TS) for secondary containment pressure not being met for approximately 2 minutes and 15 seconds. The maximum secondary containment pressure observed during that time was approximately 0.1 inches of water gauge (positive). Secondary containment pressure was returned to within the TS operability limit of greater than or equal to 0.125 inches of vacuum water gauge (TS SR 3.6.4.1.1) by restarting the train of RBHVAC. Secondary containment pressure is currently stable. Secondary containment was declared Operable at 2235 EDT. There were no radiological releases associated with this event. Declaring secondary containment inoperable is reportable under 10 CFR 50.72(b)(3)(v)(C) as an event or condition that could have prevented the fulfillment of a safety function needed to control the release of radioactive material. The Licensee has notified the NRC Resident Inspector.
ENS 537724 December 2018 13:35:00

EN Revision Text: HPCI INOPERABLE DUE TO MECHANICAL DRAFT COOLING TOWER FAN BRAKE INVERTER FAILURE At 0935 EST on December 4, 2018, the Division 2 Mechanical Draft Cooling Tower (MDCT) fans were declared inoperable due to failure of the over speed fan brake inverter. The brakes prevent fan over speed from a design basis tornado. The MDCT fans are required to support operability of the Ultimate Heat Sink (UHS). The UHS is required to support operability of the Division 2 Emergency Equipment Cooling Water (EECW) system. The EECW system cools various safety related components, including the High Pressure Coolant Injection (HPCI) system room cooler. An unplanned HPCI inoperability occurred based on a loss of the HPCI Room Cooler. Investigation into why the Division 2 MDCT fan over speed brake inverter failed is in progress. This report is being made pursuant to 10 CFR 50.72(b)(3)(v)(D) based on an unplanned HPCI inoperability. The NRC Resident Inspector has been notified. Fermi 2 is in a 14-day LCO for inoperability of HPCI and a 72-hour LCO for UHS inoperability.

  • * * RETRACTION ON 1/30/19 AT 1605 EST FROM CHRIS ROBINSON TO BETHANY CECERE * * *

The purpose of this notification is to retract EN 53772 made on December 4, 2018. Subsequent to the initial notification, the event and site Technical Specifications (TS) were reviewed further. An evaluation determined that TS Limiting Condition for Operation (LCO) 3.0.9 for barriers could be applied to the MDCT fan brakes. As a result of applying TS LCO 3.0.9 to the MDCT fan brakes, it was not necessary to declare the UHS inoperable. With the Division 2 UHS operable on December 4, 2018, the HPCI system was also operable. With HPCI operable, there was no event or condition that could have prevented the fulfillment of a safety function needed to mitigate the consequences of an accident under 10 CFR 50.72(b)(3)(v)(D). Therefore, EN 53772 is retracted and no Licensee Event Report (LER) under 10 CFR 50.73(a)(2)(v)(D) is required to be submitted. The licensee has notified the NRC Resident Inspector. Notified R3DO (Cameron).

ENS 5355421 August 2018 12:25:00At 08/20/2018 at 1856 (EDT), it was determined that a contract supervisor failed a test specified by the FFD (fitness for duty) testing program. The individual's authorization for site access has been terminated. The NRC Resident Inspector has been notified.
ENS 5317822 January 2018 15:09:00At 1115 EST, on 1/22/18, Fermi 2 determined that the site was in violation of its National Pollutant Discharge Elimination System (NPDES) permit due to an oil sheen being observed in a overflow canal that had breached the installed oil booms and entered navigable waterways. Approximately 5-10 gallons of oil has reached navigable water, which resulted in exceeding State limits. The oil is currently contained with no additional leakage to navigable waters and cleanup is in progress. The cause of the oil entering the overflow canal is under investigation. Reports will be made to the Michigan Department of Environmental Quality (MDEQ) and other local agencies. Since these reports are in the process of being made, this is considered a News Release or Notification to Other Government Agencies, therefore this event is reportable under 10 CFR 50.72(b)(2)(xi). The NRC Resident Inspector has been notified. The Licensee has notified the National Response Center.