Semantic search

Jump to navigation Jump to search
 Entered dateEvent description
ENS 533824 May 2018 13:50:00During performance of an extent of condition evaluation of protection for Technical Specification (TS) equipment from the damaging effects of tornados, River Bend Station identified non-conforming conditions in the plant design such that specific TS equipment is considered to not be adequately protected from tornado missiles. The reportable condition is postulated by tornado missiles entering the Diesel Generator Building through conduit and pipe penetrations. A tornado could generate multiple missiles capable of striking Division 1, Division 2, and Division 3 Diesel Generator support equipment rendering all Safety Related Diesel Generators inoperable. This condition is reportable per 10 CFR 50.72(b)(3)(ii)(B) for any event or condition that results in the nuclear power plant being in an unanalyzed condition that significantly degrades plant safety, and per 10 CFR 50.72(b)(3)(v) for any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to (A) Shut down the reactor and maintain it in a safe shutdown condition, (B) Remove residual heat, or (D) Mitigate the consequences of an accident. This condition was identified as part of an on-going extent of condition review of potential tornado missile related site impacts. Enforcement discretion per Enforcement Guidance Memorandum EGM 15-002 has been implemented and required actions taken. Corrective actions will be documented in a follow-on licensee event report. The licensee has notified the NRC Resident Inspector.
ENS 5336526 April 2018 18:50:00River Bend Station experienced an inadvertent initiation and injection of High Pressure Core Spray (HPCS) at 1531 (CDT) on 4/26/2018 while operating at 100 percent power. During replacement of Level Transmitter B21-LTN081C 'Reactor Vessel Low Water Level 1', Main Control Room received an inadvertent initiation and injection of High Pressure Core Spray. The HPCS injection valve was open for approximately 40 seconds before the operators manually closed the valve. Feedwater Level Control responded per design and maintained Reactor Water Level nominal values. The Division 3 Diesel Generator (DG) also automatically started in response to the actuation signal. The DG did not automatically connect to the Division 3 switchgear since there was not a low voltage condition on the bus. The manual closure of the injection isolation valve caused the system to be incapable of responding to an automatic actuation signal. The manual override of the injection isolation valve was reset approximately 16 minutes after the event, restoring the system to its standby condition. This event is being reported in accordance with 10 CFR 50.72(b)(2)(iv)(A) as a condition that caused ECCS (Emergency Core Cooling System) discharge to RCS (Reactor Coolant System) and 10 CFR 50.72(b)(3)(v)(D) as a condition that caused the loss of function of the HPCS System. The Senior NRC Resident inspector has been notified.