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 Entered dateEvent description
ENS 5482710 August 2020 17:05:00The following was received from the licensee: On August 3, 2020, Entergy Operations, Inc. (Entergy) completed an evaluation of a deviation at Waterford 3 which concluded the condition constitutes a defect pursuant to 10 CFR 21. The Waterford 3 Site Vice President was notified of the result of this evaluation on August 10, 2020. The Masoneilan 8012N-3C electropneumatic positioner installed on Emergency Feedwater Valve EFW-223A locked during as-found diagnostic testing. Failure analysis concluded that the condition was due to an internal failure of the magnet-coil assembly due to the magnet base had poor solder joints. This has been attributed to a manufacturing defect. Entergy concluded that this condition could affect the ability to properly respond to an Emergency Feedwater Actuation Signal / Main Steam Isolation Signal if present on any of the four air operated Emergency Feedwater to Steam Generator flow control valves; therefore, it could have created a substantial safety hazard. Licensees affected: Waterford. The licensee notified the NRC Resident Inspector. Notified R4DO and the Part 21 group via email.
ENS 5406816 May 2019 18:07:00This is a non-emergency notification from Waterford 3. On May 16, 2019, at 1348 CDT, Waterford 3 experienced an automatic reactor trip due to Steam Generator number 1 high level, which was the result of a Main Turbine trip and subsequent reactor power cutback which had occurred at 1345 CDT. The cause of the Main Turbine trip is currently under investigation. Subsequent to the Reactor trip, Main Feedwater Isolation Valves number 1 and number 2 closed on high Steam Generator levels. Emergency Feedwater automatically actuated for Steam Generator number 2 at 1419 CDT and Steam Generator number 1 at 1425 CDT. Main Feedwater was restored to both Steam Generators by 1629 CDT. The plant entered the Emergency Operating Procedure for an uncomplicated reactor trip and is in the process of transitioning to the normal operating shutdown procedure. The plant is currently in Mode 3 and stable with Main Feedwater feeding and maintaining both Steam Generators. The NRC Senior Resident Inspector has been notified. All control rods fully inserted. Decay heat is being removed through the main condenser. The plant is in a normal shutdown electrical lineup.
ENS 5217915 August 2016 14:10:00This is a non-emergency notification from Waterford 3. On August 12, 2016, at 1704 CDT, the shift operating crew entered Technical Specification (TS) 3.0.3 due to both trains of Essential Services Chilled Water being inoperable. Essential Services Chilled Water Loop A had previously been declared inoperable for maintenance on August 11, 2016. On August 12, 2016, at 1704, the shift operating crew noted that Loop B Essential Services Chilled Water outlet temperature exceeded the allowed TS limit of 42 degrees Fahrenheit. Essential Chiller AB was subsequently aligned to Loop B and TS 3.0.3 was exited on August 12, 2016 at 1802 when outlet temperature was verified less than or equal to 42 degrees Fahrenheit. On August 15, 2016, subsequent review of this event determined that this event was reportable under 10 CFR 50.72(b)(3)(v)(D), 'event or condition that could have prevented fulfillment of a safety function of structures or systems that are needed to (D) mitigate the consequences of an accident' due to both Essential Services Chilled Water Loops being inoperable. The NRC Resident Inspector has been notified.
ENS 5134826 August 2015 15:47:00

This is a non-emergency notification from Waterford 3. On August 26, 2015, at 0111 CDT, Emergency Diesel Generator (EDG) 'A' was declared inoperable following a trip of EDG 'A' on Generator Differential. Technical Specification (TS) 3.8.1.1 actions b. and d. were entered. EDG 'A' was being routinely run in accordance with OP-903-115, 'Train A Integrated Emergency Diesel Generator/Engineering Safety Features Test', Section 7.4, '24 hr EDG A Run with Subsequent Diesel Start' to satisfy Technical Specification Surveillance Requirement 4.8.1.1.2 6. EDG 'B' was subsequently started per TS 3.8.1.1 action b. (1). At 0740 CDT, EDG 'B' was declared inoperable and TS 3.8.1.1 f. was entered due to the exhaust fan not starting when the diesel engine was started. Troubleshooting determined that the EDG B exhaust fan did not start due to HVR-501B (EG B ROOM OUTSIDE AIR INTAKE DAMPER) not opening. Action was taken to isolate air and fail HVR-501B to its open safety position. At 1001 CDT, EDG 'B' was declared operable and TS 3.8.1.1.f. was exited following verification of proper operation of the EDG 'B' exhaust fan. Waterford 3 is currently in TS 3.8.1.1 actions b. and d. Actions to verify a temporary EDG is available and restore EDG 'A' to operable status are in progress. This event is reportable pursuant to 10 CFR 50.72(b)(3)(v) (A) and 10 CFR 50.72 (b)(3)(v) (D), 'event or condition that could have prevented fulfillment of a safety function of structures or systems that are needed to (A) shut down the reactor and maintain it in a safe shutdown condition' and (D) 'mitigate the consequences of an accident due to both emergency diesel generators being inoperable.' The NRC Resident Inspector has been notified.

  • * * UPDATE FROM SCOTT MEIKLEJOHN TO DONALD NORWOOD AT 1328 EDT ON 8/31/2015 * * *

The following is a correction to a non-emergency event notification from Waterford 3 originally made on 8/26/2015: On August 26, 2015, at 0111 CDT, Emergency Diesel Generator (EDG) 'A' was declared inoperable following a trip of EDG 'A' on Generator Differential. Technical Specification (TS) 3.8.1.1 actions b and d were entered. EDG 'A' was being routinely run in accordance with OP-903-115, 'Train A Integrated Emergency Diesel Generator/Engineering Safety Features Test,' Section 7.4, '24 hr EDG A Run with Subsequent Diesel Start' to satisfy Technical Specification Surveillance Requirement 4.8.1.1.2(e)6. EDG 'B' was subsequently started per TS 3.8.1.1 action b.(1). At 0740 CDT, EDG 'B' was declared inoperable and TS 3.8.1.1 f was entered due to the room exhaust fan not starting when the diesel engine was started. Troubleshooting determined that the EDG B room exhaust fan did not start due to HVR-501B (EDG B ROOM OUTSIDE AIR INTAKE DAMPER) not opening. Action was taken to isolate air and fail HVR-501B to its open safety position. At 1001 CDT, EDG 'B' was declared operable and TS 3.8.1.1.f was exited following verification of proper operation of the EDG 'B' room exhaust fan. Waterford 3 is currently in TS 3.8.1.1 actions b and d. Actions to verify a temporary EDG is available and restore EDG 'A' to operable status are in progress. This event is reportable pursuant to 10 CFR 50.72(b)(3)(v)(A) and 10 CFR 50.72(b)(3)(v)(D), Event or Condition that Could Have Prevented Fulfillment of a Safety Function of structures or systems that are needed to (A) shut down the reactor and maintain it in a safe shutdown condition and (D) mitigate the consequences of an accident due to both emergency diesel generators being inoperable. The NRC Resident Inspector has been notified. Notified R4DO (Warnick)