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 Entered dateEvent description
ENS 4843624 October 2012 02:40:00

On 10/24/12 at 0147, North Anna Unit 2 reactor tripped automatically. The reactor first out is the 'C' steam generator lo-lo level. The turbine first out is reactor tripped, turbine trip. The event was apparently initiated by a loss of load on the secondary side. The cause of the loss of load is still being investigated. All systems responded as expected. This event is reportable per 10 CFR 50.72(b)(2)(iv)(B) due to actuation of the Reactor Protection System. The Auxiliary Feedwater pumps received an automatic start signal due to low-low level in all steam generators at the time of the trip, Steam generator levels have been restored to normal operating level. The Auxiliary Feedwater System operated as designed with no abnormalities noted. This event is reportable per 10 CFR 50.72(b)(3)(iv)(A) due to actuation of an ESF system. All control rods inserted into the core at the time of the trip and decay heat is being removed via the main condenser steam dumps. Several secondary (feedwater) relief valves lifted and reseated during the event. North Anna Unit 2 is currently stable at no load temperature and pressure in mode 3. At 0147 EDT, the Unit 2 Pressurizer Power Operated Relief Valve (PORV) , 2-RC-PCV-2455C, opened during an automatic reactor trip of Unit 2. The valve indicated open for less than 1 second. During this time, the identified leakage threshold for EAL SU6.1 (25 gpm) was exceeded. The cause of the loss of secondary load, which is believed to have caused the low steam generator water level and the lifting of the pressurizer PORV, is still under investigation. The licensee is focusing on the high pressure to low pressure turbine intercept valves or reheat valves going shut for reasons unknown at this time. The licensee's data shows that a pressurizer PORV opened momentarily. The instantaneous leak rate exceeded the unusual event threshold leak rate of 25 gpm. The PORV reseated and no ongoing leakage occurred during the transient. The rest of the transient was characterized as uncomplicated. The unit is in a normal post-trip electrical configuration. All systems functioned as required. There was no impact on Unit 1. The licensee has notified the NRC Resident Inspector.

  • * * UPDATE AT 1346 EDT ON 10/24/12 FROM PAGE KEMP TO S. SANDIN * * *

The licensee is updating their report to RETRACT the portion related to the after-the-fact entry into EAL SU6. At 0147 hours EDT on 10-24-12, a Unit 2 Pressurizer Power Operated Relief Valve, 2-RC-PCV-2455C, opened during automatic reactor trip. The valve indicated open for less than 1 second. 2-RC-PCV-2455C opened as designed in response to the plant trip and allowed a small amount of water to transfer to the Pressurizer Relief Tank, as designed. The Pressurizer Power Operated Relief Valve subsequently re-closed and remains available for automatic operation, if needed. Initially, this issue was reported to the NRC at 0240 hours on 10-24-12 as an After-The-Fact Unusual Event for EAL SU6.1. Subsequent review has determined that the Pressurizer Power Operated Relief Valve functioned as designed and the small amount of inventory was transferred to the Pressurizer Relief Tank as designed and therefore does not meet the criteria for an Unusual Event and this notification is being retracted. NEI 99-01, Rev. 5 provides additional guidance that relief valve normal operation should be excluded from this Initiating Condition. However, a relief valve that operates and fails to close per design should be considered applicable to this Initiating Condition if the relief valve cannot be isolated. In this case, the Pressurizer Power Operated Relief Valve operated as designed and returned to automatic operation. The licensee informed state and local agencies and the NRC Resident Inspector. Notified R2DO (Musser).