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 Entered dateEvent description
ENS 452455 August 2009 12:00:00

At 0750 PDT the licensee experienced a turbine trip and reactor scram. At approximately the same time, a fire was detected in the non-safety related 6.9 kV feed bus to switchgear SH-5 and SH-6 in the turbine building. The fire and associated fault to the switchgear feed bus caused a loss of power to both reactor recirculation pumps and the automatic reactor scram. The fire produced smoke and potentially toxic gases. Due to the presence of potentially toxic gas in the power plant, an Unusual Event was declared at 0812 PDT based on EAL 9.3.U.3. At the present time, the fire is out and the smoke is being cleared from the plant. All rods fully inserted upon the reactor scram. Systems functioned as expected except for problems with the EHC system which resulted in the bypass valves remaining open which caused the reactor to depressurize to approximately 390 psi. MSIVs were manually shut to halt the reactor depressurization and cooldown. Decay heat is being removed via relief valves to the suppression pool with reactor pressure being maintained between 500 and 600 psi. Suppression pool cooling is via RHR. Makeup water to the reactor is via normal feed. Licensee is on natural circulation at the time of this report. Normal shutdown electrical alignment is established with the exception of Division II emergency switchgear which is aligned to the backup transformer. A request for assistance was made to the Hanford fire department, however, the fire was out prior to their arrival on site. The licensee has notified State, local agencies and the NRC Resident Inspector.

  • * * UPDATE FROM JOHN SLACK TO DONALD NORWOOD AT 1332 ON 08/05/09 * * *

The Unusual Event has been terminated as of 1006 PDT. The licensee is taking the unit to cold shutdown. The licensee will notify the NRC Resident Inspector. Notified NRR EO (Ross-Lee), R4DO (Walker), DHS (Enzer), and FEMA (Eaches).

  • * * UPDATE FROM NICK RULLMAN TO PETE SNYDER AT 1827 ON 08/05/09 * * *

Following the reactor scram, with the turbine bypass valves failed fully open, the inboard main steam isolation valves had to be manually closed to prevent excessive cool down. The outboard main steam isolation valves automatically closed from the inability to maintain condenser vacuum. The inability to maintain condenser vacuum was due to limited equipment access in the Turbine Building from heavy smoke. This is reportable under Part 50.72(b)(3)(iv)(A) as a valid actuation of one of the systems listed in Part 50.72(b)(3)(iv)(B)(2). The licensee notified the NRC Resident Inspector. Notified R4DO (Walker).