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 Entered dateEvent description
ENS 5722110 July 2024 11:15:00The following information was provided by the licensee via phone and email: At 0728 EDT on July 10, 2024, with Unit 2 in Mode 1 at 24 percent power, the reactor automatically scrammed due to a manual turbine trip. The (reactor) scram was not complex with all systems responding normally. Reactor vessel level reached the low-level set-point following the scram, resulting in valid Group 2 and Group 3 containment isolation signals. Due to the reactor protection system actuation while critical, this event is being reported as a four hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B) and an eight hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A) for the Group 2 and Group 3 isolations. Operations responded using emergency operating procedures and stabilized the plant in Mode 3. Decay heat is being removed by discharging steam to the main condenser using the turbine bypass valves. Unit 3 was not affected. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.