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 Entered dateEvent description
ENS 4471914 December 2008 20:38:00Callaway Plant was at 98% power with two condensate pumps in service. At 1714 on 12-14-08, the reactor was manually tripped due to a motor ground fault on the 'B' condensate pump. The 'C' condensate pump was not available for service (See EN #44714). This left only one condensate pump available so the reactor was manually tripped. The plant is in mode 3 and stable. Reactor trip procedures have been implemented and exited and normal operating procedures are in progress at this time. All safety systems actuated as designed. All control rods inserted during the trip. Offsite power is available and powering safety loads. There is no primary to secondary leakage. Decay heat is being removed via steam dumps to the condenser with makeup provided by Auxiliary Feedwater to the steam generators. The standby diesel generators and safety systems are available. The NRC Senior Resident Inspector has been notified.
ENS 443814 August 2008 11:07:00The Callaway Plant Process Computer is being upgraded to a newer system. This implementation period is expected to start on August 4, 2008 and last approximately 14 days. During the implementation time for this upgrade, the Emergency Response Data System (ERDS) system will be out of service. Compensatory actions for emergency situations have been established. This event is reportable per 10 CFR50.72(b)(3)(xiii) since this constitutes a loss of ERDS for the duration of the evolution. The licensee has notified the NRC Resident Inspector.