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 Entered dateEvent description
ENS 5393715 March 2019 13:39:00On March 15, 2019 at 1300 EDT, Indian Point Unit 2 automatically tripped offline from mode 1 - 100% power operations. Reactor Operators verified the reactor trip and the plant is currently stable in mode 3. All automatic systems functioned as required. The auxiliary feedwater system actuated following the trip, as expected. All control rods fully inserted upon the trip, as expected. This event is reportable under 10 CFR 50.72(b)(3)(iv)(A) and 10 CFR 50.72(b)(2)(iv)(B). The unit remains on offsite power in hot standby at normal operating temperature and pressure. Decay heat is being removed from the steam generators via the auxiliary feedwater system and the condensate steam dump valves. Unit 3 remains in mode 6 for a scheduled refueling outage. The licensee notified the NRC Resident Inspector, the local transmission company, and New York State Independent System Operator. The Indian Point Unit 2 automatic trip was caused by the trip of the main generator. The cause of the generator trip is unknown at this time.