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Issue date | Title | Topic | |
---|---|---|---|
ML20216E643 | 26 August 1999 | Rev 19 to TDB-VI, COLR for FCS Unit 1 | Boric Acid Shutdown Margin |
ML20216E636 | 21 July 1999 | Rev 18 to TDB-VI, COLR for FCS Unit 1 | Shutdown Margin |
ML20249C569 | 22 April 1998 | Rev 17 to TDB-VI, COLR for Fort Calhoun Station,Unit 1, Updating Cycle 18 Operations | Shutdown Margin |
ML20249C565 | 30 March 1998 | Rev 16 to TDB-VI, COLR for Fort Calhoun Station,Unit 1, Updating Cycle 18 Boron Concentration on Page 8 of 17 | Shutdown Margin |
ML20217G257 | 13 March 1998 | Rev 15 to Cycle 17 COLR, Updating Section 4.0 to Reduce Max Core Inlet Temp for Remainder of Cycle 17 Operations to Not Exceed 540 F | Shutdown Margin |
ML20217G249 | 28 February 1998 | Rev 14 to Cycle 17 COLR, Revising COLR Peaking Factors to Ensure Appropriate Conservatism Is Applied | Shutdown Margin |
ML20217Q542 | 13 August 1997 | Rev 13 to Colr | Shutdown Margin |
ML20135A658 | 13 November 1996 | Rev 12 to COLR, Updating Cycle 17 Operations | Shutdown Margin |
ML20135A654 | 27 August 1996 | Rev 11 to COLR, Updating COLR Figures 4,5,6,7A & 8 to Reflect New LCO & LSSS | Shutdown Margin |
ML20116B690 | 10 July 1996 | Rev 10 to Colr | Shutdown Margin |
ML20094D302 | 6 October 1995 | Rev 9 to Core Operating Limit Rept, Adding Figure, Axial Power Distribution LSSS for 4 Pump Operation | Shutdown Margin |
ML20107H628 | 6 October 1995 | Corrected Rev 9 to Core Operating Limit Rept, Adding Figure to COLR for Axial Power Distribution LSS for 4 Pump Operation | Shutdown Margin |
ML20082M497 | 4 April 1995 | Rev 8 to COLR, Updating COLR to Reflect Cycle 16 Setpoints & Restrictions Defined in EA-FC-95-009,Rev 0 Cycle 16 Setpoints & COLR | Shutdown Margin |
ML20082M479 | 20 March 1995 | Rev 7 to COLR, Revising Refueling Boron Concentration | Shutdown Margin |
ML20080F660 | 20 January 1995 | Cycle 16 Reload Evaluation Rept, for FCS Unit 1 | Shutdown Margin Anticipated operational occurrence Coast down |
ML20070P372 | 31 May 1994 | Reload Core Analysis Methodology Overview | |
ML20059H741 | 22 November 1993 | Rev 6 to COLR, Reflecting Cycle 15 Operating Conditions | Shutdown Margin |
ML20059H735 | 23 October 1993 | Rev 5 to COLR, Updating Min Boron Concentration to 1900 to Reflect Core Changes Prior to Cycle 15 Operation | Shutdown Margin |
ML20046A083 | 19 July 1993 | Omaha Public Power District Fort Calhoun Station Unit 1 Cycle 15 Reload Evaluation. | Shutdown Margin Anticipated operational occurrence |
ML20045E054 | 25 June 1993 | Nonproprietary Revised Pages of Rev 5 to Reload Core Analysis Methodology Overview. | |
ML20138D309 | 31 January 1993 | Nonproprietary OPPD Nuclear Analysis,Reload Core Analysis Methodology Overview | |
ML20128C198 | 17 December 1992 | Rev 4 to COLR, Allowing Increase in Operating Space for DNB-LCO Monitoring W/O Requiring Use of Basss | Shutdown Margin |
ML20128C194 | 16 November 1992 | Rev 3 to COLR Reflecting Increase in Allowable Peak Linear Heat Rate in COLR from 14.4 Kw/Ft to 15.5 Kw/Ft Until 7770 Mwd/Mtu | Shutdown Margin |
ML20118A393 | 17 August 1992 | Rev 2 to Fort Calhoun Station Cycle 14 Core Operating Limits Rept | Shutdown Margin |
ML20099B450 | 28 June 1992 | Rev 1 to Fort Calhoun Station Cycle 14,Core Operating Limits Rept | Shutdown Margin |
ML20096G406 | 25 April 1992 | Core Operating Limit Rept | Shutdown Margin |
ML20086F445 | 27 November 1991 | Cycle 14 Reload Evaluation | Shutdown Margin Anticipated operational occurrence |
ML20073H252 | 30 April 1991 | Rev 4 to Nuclear Analysis Reload Core Analysis Methodology Overview | |
ML20073H264 | 31 March 1991 | Rev 3 to Omaha Public Power District Nuclear Analysis Reload Core Analysis Methodology - Transient & Accident Methods & Verification | Boric Acid Shutdown Margin Anticipated operational occurrence Fuel cladding Coast down |
ML19354E695 | 26 January 1990 | Reload Evaluation Rept for Fort Calhoun Station Unit 1, Cycle 13. | Shutdown Margin Anticipated operational occurrence |
ML20154H655 | 30 April 1988 | Rev 2 to Nuclear Analysis Reload Core Analysis Methodology, Transient & Accident Methods & Verification | Shutdown Margin Anticipated operational occurrence Coast down |
ML20154H635 | 30 April 1988 | Rev 2 to Nuclear Analysis Reload Core Analysis Methodology, Neutonic Design Methods & Verification | Shutdown Margin |
ML20153E171 | 30 April 1988 | Rev 3 to Nuclear Analysis Reload Core Analysis Methodology Overview | Boric Acid Shutdown Margin Anticipated operational occurrence Coast down |
ML20149F718 | 31 January 1988 | Rev 0 to Extended Burnup Rept for Fort Calhoun Reloads XN-4 & XN-5 (Batches K & L) | Anticipated operational occurrence Hydrostatic Fuel cladding Power change |
ML20204F478 | 18 March 1987 | Errata to Rev 2 to Reload Core Analysis Methodology Overview | |
ML20204F631 | 18 March 1987 | Errata to Rev 1 to Reload Core Analysis Methodology Overview | Shutdown Margin Anticipated operational occurrence Fuel cladding |
ML20212N021 | 30 November 1986 | Rev 2 to Reload Core Analysis Methodology Overview | |
ML20212N027 | 30 November 1986 | Rev 1 to Reload Core Analysis Methodology Overview | Shutdown Margin |
ML20212N032 | 30 November 1986 | Rev 1 to Reload Core Analysis Methodology Overview | Boric Acid Shutdown Margin Anticipated operational occurrence Fuel cladding |
ML20211M527 | 30 November 1986 | Partially Withheld Nonproprietary Omaha Batch M Reload Fuel Design Rept (Ref 10CFR2.790) | Hydrostatic Earthquake Fuel cladding |
ML20082D840 | 30 November 1983 | Nonproprietary Version of Statistical Combination of Uncertainties, Parts 1,2 & 3 | Shutdown Margin |
ML20078D948 | 30 September 1983 | Reload Core Analysis Methodology Overview |