PNO-II-80-161, on 801119,w/reactor at 50% power,2-inch Steam Generator Recirculation Pump Line Sheared at Connection to Steam Generator B Feed Regulator Valve Bypass Line,After Earlier Reactor Trip

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PNO-II-80-161:on 801119,w/reactor at 50% power,2-inch Steam Generator Recirculation Pump Line Sheared at Connection to Steam Generator B Feed Regulator Valve Bypass Line,After Earlier Reactor Trip
ML17340A769
Person / Time
Site: Turkey Point NextEra Energy icon.png
Issue date: 11/19/1980
From: Martin R, Price D
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
References
PNO-II-80-161, NUDOCS 8102280226
Download: ML17340A769 (2)


HKLIHDQRY SOTIEZCATIQH ENCLOSURE Nav~r 2~9+0 PP~ZKDQLRV ROTZFICATXON'OF OR GKGSQAL OCCJRBZHCE

" Papal-80-l61 This rcliminarv notification constitutes ZQ v notice of an event af POSSIBLE ff'.t or public interest siniEicance.

The infcri"ation yresentea zs as initially

= rccoived sit.haut verification or evalu"tion and -'s basicallv all that is hewn bv TK sta f as af this date 7'AC&~~

H.orida Power and Light Company Tu"rey Point 3 Docket Ho. 50"250 Eon stead)

F'larida SOBJBH':i PSZDWATSB SYSiiH PZPB BBBSR

~

ss At 1:30 p.m.) a 2-inch steam generator recirculation pump line sheared at its connectio:.

tc th 8 s~ generator feed regulator valve

{FPV) bypass line with the reactor at 5'~;:

power.

A reacto trip from 100>o power had occurred earlier, at %0:l6 a.m., following

=.

turbin trip on low level in steam generator A. Initial investigation af the earlier =:

a"t"iouted the problem to a HP control failure caused by a loose wire in the valve's controller.

Mao wire was tightened anc thc plan restarted.

A ~zozimately 50~ power, water leve1 oscillations were observed in all 3 steam generators.

Bnc FRVs were shifted to manu=i con-rol and a second feed pump started.

- s'ezz gcncrator oscillations increased and a rumbling sound was heard in the control o.

Investigalion revealed water and steam D.ca~ from.

he vicinity of a nortion of the az:

fcedwater pipe which is located outside a

con'~inment.

The operators..initiated a re""

si.~edge but th reactor tri@ecl autor" ically due to

  • Low stcam ~energy.t.or level.

Auxiliary fee@uter pumps wer= started and the s=eam generator level iestnred.

Further

=nvestigation revealed the leak t.o be fran the break of the 2 inch recirculation pump inc,.

This break was isolated..Ho radioac:ve contaminate.an or persouneg injury'c~~cd

~

licensee is investigating the event

'-e -ei oscillations and the pipe break.

=h tim of the event and is continuing to determine the cause of the st.earn generator Ti resid nt inspector was in the control zoo~

La mon tor licensee act.ivim~s hfcdia interest m"v occur.

The licensee is considering a news relezse.

Thc EC does no plan to issue a news release.

The State of Florida has been informed.

A

~

ss Re-ian II (At.lant') receivecl notifica"ion of this occurrence by telephone from the resiflent inspector at. 2:45 on November 19, 1980.

J - Ch>lk)

SvCY C. Eammerer, CA

{ r Distr'bution)

XB:XOOS~~~ (W:Bq Diss.)

P.

B}dg.

E. R. Qentan, lsd R.

H. Voila:er, "P3'

. S~oeder, V~~

D. F. Ross, h."Z L. Rx enhr t) RP, S

E. nanauer) hYR Transmitted:

tSBB V. J. Dirchs)

ZDO C. hichelson, A=OD

'. Foucha"d PA

h. 1lalfer)

GAPA

F.

G. Ryan)

SP Z. Shapar, ELD 1andow

{6 ~/page-J. J. Cux~gs)

QIA HAEL R. Ninogne, SD IE:XO05 D>ocument~t.

Br. g'or PD";

Villste Je Ce Ga~t.~ s ss.>s)S T. E. Hmley, RES.

PRELIMlHARV E:0~

ATION Appliable President Site P siessl Offices Ccntac:

D. S.

P ice, PZI 242-5569; R. D. Ear ir, Rll'42-5534 llist.rihution:

Transmitted H. St Chairman Ahearnc C~sioner nendrie S.

Comissione Gilinsky Co~sioner Bradford C.

ACES Fa