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Category:Letter type:NL
MONTHYEARNL-24-0031, Inservice Inspection Program Owner'S Activity Report (OAR-1) for Outage 2R232024-01-29029 January 2024 Inservice Inspection Program Owner'S Activity Report (OAR-1) for Outage 2R23 NL-24-0020, Plan, Unit 1 Responses to NRC Request for Additional Information for Refueling Outage 1R24 Steam Generator Tube Inspection Report2024-01-22022 January 2024 Plan, Unit 1 Responses to NRC Request for Additional Information for Refueling Outage 1R24 Steam Generator Tube Inspection Report NL-23-0926, Correction of Technical Specification Typographical Error2024-01-12012 January 2024 Correction of Technical Specification Typographical Error NL-23-0878, Request for Exemption from Security Event Notification Implementation2023-11-29029 November 2023 Request for Exemption from Security Event Notification Implementation NL-23-0827, Response to Requests for Additional Information for a License Amendment Request and a Proposed Alternative Related to TS 3.4.142023-11-17017 November 2023 Response to Requests for Additional Information for a License Amendment Request and a Proposed Alternative Related to TS 3.4.14 NL-23-0750, Response to Second Request for Additional Information Regarding License Amendment Request: Technical Specification Revision to Adopt TSTF-339-A, Relocate Technical Specification Parameters to the Colr2023-10-0404 October 2023 Response to Second Request for Additional Information Regarding License Amendment Request: Technical Specification Revision to Adopt TSTF-339-A, Relocate Technical Specification Parameters to the Colr NL-23-0745, Refueling Outage 1R24 Steam Generator Tube Inspection Report2023-09-22022 September 2023 Refueling Outage 1R24 Steam Generator Tube Inspection Report NL-23-0695, Response to Round 2 Request for Additional Information Regarding License Amendment Request for Technical Specification 3.8.3, Inverters Operating, Completion Time Extension (LAR-22-002S2)2023-08-31031 August 2023 Response to Round 2 Request for Additional Information Regarding License Amendment Request for Technical Specification 3.8.3, Inverters Operating, Completion Time Extension (LAR-22-002S2) NL-23-0666, License Amendment Request: Remove Combined License Appendix C (LAR 23-008)2023-08-28028 August 2023 License Amendment Request: Remove Combined License Appendix C (LAR 23-008) NL-23-0670, Response to Request for Additional Information Regarding License Amendment Request: Technical Specification Revision to Adopt TSTF-339-A, Relocate Technical Specification Parameters to the COLR Consistent with WCAP-144832023-08-11011 August 2023 Response to Request for Additional Information Regarding License Amendment Request: Technical Specification Revision to Adopt TSTF-339-A, Relocate Technical Specification Parameters to the COLR Consistent with WCAP-14483 NL-23-0658, Southern Nuclear Operating Company - Response to Request for Additional Information Regarding Quality Assurance Topical Report Submittal2023-08-11011 August 2023 Southern Nuclear Operating Company - Response to Request for Additional Information Regarding Quality Assurance Topical Report Submittal NL-23-0672, Licensee Guarantees of Payment of Deferred Premiums2023-08-10010 August 2023 Licensee Guarantees of Payment of Deferred Premiums NL-23-0542, CFR 50.46 ECCS Evaluation Model Annual Report for 20222023-08-0909 August 2023 CFR 50.46 ECCS Evaluation Model Annual Report for 2022 NL-23-0624, Report of Changes to Emergency Plan and Summary of 50.54(q) Analysis2023-08-0404 August 2023 Report of Changes to Emergency Plan and Summary of 50.54(q) Analysis NL-23-0611, Core Operating Limits Report, Cycle 11 Version 12023-07-19019 July 2023 Core Operating Limits Report, Cycle 11 Version 1 NL-23-0584, Preservice Inspection Program Owner'S Activity Report2023-07-10010 July 2023 Preservice Inspection Program Owner'S Activity Report NL-23-0555, Request for Exemption from Physical Barrier Requirement2023-07-0707 July 2023 Request for Exemption from Physical Barrier Requirement NL-23-0506, to Non-Voluntary License Amendment Request: Technical Specification Revision to Adopt WCAP-17661-P-A, Improved RAOC and CAOC Fq Surveillance Technical Specifications2023-07-0505 July 2023 to Non-Voluntary License Amendment Request: Technical Specification Revision to Adopt WCAP-17661-P-A, Improved RAOC and CAOC Fq Surveillance Technical Specifications NL-23-0541, Inservice Inspection Program Owners Activity Report for Outage 1R242023-06-28028 June 2023 Inservice Inspection Program Owners Activity Report for Outage 1R24 NL-23-0444, Quality Assurance Topical Report Submittal2023-06-15015 June 2023 Quality Assurance Topical Report Submittal NL-23-0339, Response to Request for Additional Information Regarding License Amendment Request for Technical Specification 3.8.3, Inverters - Operating, Completion Time Extension (LAR-22-002S1)2023-06-13013 June 2023 Response to Request for Additional Information Regarding License Amendment Request for Technical Specification 3.8.3, Inverters - Operating, Completion Time Extension (LAR-22-002S1) NL-23-0455, Report of 10 CFR 50.59 Changes, Tests, and Experiments and 10 CFR 52 Appendix D Departure Report2023-06-12012 June 2023 Report of 10 CFR 50.59 Changes, Tests, and Experiments and 10 CFR 52 Appendix D Departure Report NL-23-0467, Response to Request for Additional Information Regarding License Amendment Request: Timing of Unit 4 Technical Specifications Effectiveness Prior to Initial Criticality (LAR-23-005S1)2023-06-0909 June 2023 Response to Request for Additional Information Regarding License Amendment Request: Timing of Unit 4 Technical Specifications Effectiveness Prior to Initial Criticality (LAR-23-005S1) NL-23-0346, License Amendment Request for Exception to Regulatory Guide 1.163 (LAR 23-007)2023-05-25025 May 2023 License Amendment Request for Exception to Regulatory Guide 1.163 (LAR 23-007) NL-23-0383, SNC Response to Regulatory Issue Summary 2023-01:Preparation And.2023-05-19019 May 2023 SNC Response to Regulatory Issue Summary 2023-01:Preparation And. NL-23-0385, License Amendment Request: More Restrictive Action for Technical Specification 3.1.9 (LAR-23-006R1)2023-05-17017 May 2023 License Amendment Request: More Restrictive Action for Technical Specification 3.1.9 (LAR-23-006R1) NL-23-0398, Withdrawal of Request of License Amendment Request Regarding More Restrictive Action for Technical Specification 3.1.9 (LAR-23-006)2023-05-16016 May 2023 Withdrawal of Request of License Amendment Request Regarding More Restrictive Action for Technical Specification 3.1.9 (LAR-23-006) NL-23-0372, Units 1 & 2, Joseph M. Farley Nuclear Plant - Units 1 & 2, Vogtle Electric Generating Plant - Units 1 & 2, Annual Radiological Environmental Operating Reports for 20222023-05-10010 May 2023 Units 1 & 2, Joseph M. Farley Nuclear Plant - Units 1 & 2, Vogtle Electric Generating Plant - Units 1 & 2, Annual Radiological Environmental Operating Reports for 2022 NL-23-0360, Supplement to License Amendment Request and Exemptions to Allow Use of Lead Test Assemblies for Accident-Tolerant Fuel2023-05-0505 May 2023 Supplement to License Amendment Request and Exemptions to Allow Use of Lead Test Assemblies for Accident-Tolerant Fuel NL-23-0326, Response to Apparent Violation in NRC Inspection Report 05000424, 425/2023090; EA-22-1082023-05-0101 May 2023 Response to Apparent Violation in NRC Inspection Report 05000424, 425/2023090; EA-22-108 NL-23-0217, License Amendment Request to Revise Technical Specification Surveillance Requirement 3.4.14.1 and Proposed Inservice Testing Alternative ALT-VR-022023-05-0101 May 2023 License Amendment Request to Revise Technical Specification Surveillance Requirement 3.4.14.1 and Proposed Inservice Testing Alternative ALT-VR-02 NL-23-0330, Core Operating Limits Report, Cycle 25, Version 12023-04-26026 April 2023 Core Operating Limits Report, Cycle 25, Version 1 NL-23-0310, Annual Non-Radiological Environmental Operating Reports and Annual Radioactive Effluent Release Reports for 20222023-04-25025 April 2023 Annual Non-Radiological Environmental Operating Reports and Annual Radioactive Effluent Release Reports for 2022 NL-23-0135, License Amendment Request: Timing of Technical Specifications Effectiveness Prior to Initial Criticality (LAR-23-005)2023-04-17017 April 2023 License Amendment Request: Timing of Technical Specifications Effectiveness Prior to Initial Criticality (LAR-23-005) NL-23-0019, GEN-ISI-ALT-2023-01, Request to Use Provision of a Later Edition of the ASME Boiler and Pressure Vessel Code, Section XI2023-04-12012 April 2023 GEN-ISI-ALT-2023-01, Request to Use Provision of a Later Edition of the ASME Boiler and Pressure Vessel Code, Section XI NL-23-0152, License Amendment Request: Technical Specification Revision to Adopt TSTF-339-A, Relocate Technical Specification Parameters to the COLR Consistent with WCAP-144832023-04-11011 April 2023 License Amendment Request: Technical Specification Revision to Adopt TSTF-339-A, Relocate Technical Specification Parameters to the COLR Consistent with WCAP-14483 NL-23-0263, Southern Nuclear Company Submittal of Drug and Alcohol Testing Errors Identified 10 CFR 26.719(c) 30-Day Report2023-04-0505 April 2023 Southern Nuclear Company Submittal of Drug and Alcohol Testing Errors Identified 10 CFR 26.719(c) 30-Day Report NL-23-0136, License Amendment Request: More Restrictive Action for Technical Specification 3.1.9 (LAR-23-006)2023-04-0505 April 2023 License Amendment Request: More Restrictive Action for Technical Specification 3.1.9 (LAR-23-006) NL-23-0132, License Amendment Request: Remove Combined License Appendix C (LAR 23-001)2023-04-0404 April 2023 License Amendment Request: Remove Combined License Appendix C (LAR 23-001) NL-23-0014, Southern Nuclear Operating Co Submittal of Report on Status of Decommissioning Funding2023-03-29029 March 2023 Southern Nuclear Operating Co Submittal of Report on Status of Decommissioning Funding NL-23-0208, Independent Spent Fuel Storage Installation ISFSI, Decommissioning Funding Plan Triennial Update2023-03-29029 March 2023 Independent Spent Fuel Storage Installation ISFSI, Decommissioning Funding Plan Triennial Update NL-23-0193, Request for License Amendment: Relocation of TS 3.7.9, Spent Fuel Pool Makeup Water Sources (LAR-23-003)2023-03-24024 March 2023 Request for License Amendment: Relocation of TS 3.7.9, Spent Fuel Pool Makeup Water Sources (LAR-23-003) NL-23-0196, Response to Request for Additional Information Regarding License Amendment Request for Alternative Source Term, TSTF-51, TSTF-471, and TSTF-4902023-03-24024 March 2023 Response to Request for Additional Information Regarding License Amendment Request for Alternative Source Term, TSTF-51, TSTF-471, and TSTF-490 NL-23-0228, Nuclear Property Insurance Coverage as of April 1, 2023 and Licensee Guarantees of Payment of Deferred Premiums (10 CFR 140.21)2023-03-20020 March 2023 Nuclear Property Insurance Coverage as of April 1, 2023 and Licensee Guarantees of Payment of Deferred Premiums (10 CFR 140.21) NL-22-0977, License Amendment Request to Modify Technical Specification 5.5.11.c Acceptance Criteria for Charcoal Filter Testing2023-02-0909 February 2023 License Amendment Request to Modify Technical Specification 5.5.11.c Acceptance Criteria for Charcoal Filter Testing NL-23-0010, Response to Request for Additional Information Regarding License Amendment Request for Alternative Source Term, TSTF-51, TSTF-471, and TSTF-4902023-02-0606 February 2023 Response to Request for Additional Information Regarding License Amendment Request for Alternative Source Term, TSTF-51, TSTF-471, and TSTF-490 NL-23-0076, Exigent License Amendment Request: Technical Specification Exceptions for In-containment Refueling Water Storage Tank Operability Prior to Initial Criticality (LAR-23-004)2023-01-31031 January 2023 Exigent License Amendment Request: Technical Specification Exceptions for In-containment Refueling Water Storage Tank Operability Prior to Initial Criticality (LAR-23-004) NL-23-0013, Response to Request for Additional Information Related to 10CFR 50.75 Decommissioning Funding Assurance Requirements2023-01-30030 January 2023 Response to Request for Additional Information Related to 10CFR 50.75 Decommissioning Funding Assurance Requirements NL-23-0068, Responses to NRC Request for Additional Information Related to the Refueling Outage 2R22 Steam Generator Tube Inspection Report2023-01-27027 January 2023 Responses to NRC Request for Additional Information Related to the Refueling Outage 2R22 Steam Generator Tube Inspection Report NL-23-0012, Post-Audit Supplement to License Amendment Request and Exemptions to Allow Use of Lead Test Assemblies for Accident-Tolerant Fuel2023-01-20020 January 2023 Post-Audit Supplement to License Amendment Request and Exemptions to Allow Use of Lead Test Assemblies for Accident-Tolerant Fuel 2024-01-29
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Text
Southern Nuclear Operating Company, Inc.
Post Off ice Box 1295 Birmingham, Alabama 35201-1295 June 21, 2007 Energy to Serve Your World '"
Docket No.: 50-425 U. S. Nuclear Regulatory Commission A m : Document Control Desk Washington, D. C. 20555-0001 Vogtle Electric Generating Plant - Unit 2 Results of Reactor Pressure Vessel Head Inspections Required by First Revised Order EA-03-009 Ladies and Gentlemen:
On February 20,2004, the NRC issued the First.Revised NRC Order EA-03-009 (Order) to establish interim inspection requirements for reactor pressure vessel (RPV) heads at pressurized water reactors. On March 8,2004, Southern Nuclear Operating Company (SNC) submitted an answer to the Order which included a request for relaxation of the Order pursuant to the provisions of paragraph IV.F. The relaxation request was in regard to inspections performed under paragraph IV.C.(S)(a) of the Order. The relaxation request was supplemented by SNC letter dated July 1,2005 and was granted by NRC letter dated September 13,2005 (TAC Nos. MC7019 and MC7020). In addition, by SNC letter dated May 18,2006, and supplemented by SNC letter dated June 2,2006, SNC requested a relaxation of the Order pursuant to the provisions of paragraph IV.F in regard to inspections performed under paragraph IV.C.(S)(b) of the Order. This relaxation request was granted by NRC letter dated August 30,2006 (TAC Nos. MD1805 and MD1806).
As reported by SNC's June 28, 2004 letter, SNC completed a bare metal visual (BMV) examination of >99% of the RPV top head surface including 360' around each RPV head penetration nozzle during the spring 2004 reheling outage (2R10) at Vogtle Electric Generating Plant Unit 2 (VEGP-2). This examination satisfied the portion of paragraph IV.C.(3) of the Order which specified an inspection meeting the requirements of paragraph IV.C.(S)(a), consistent with the relaxation granted by the NRC (TAC Nos.
MC70 19 and MC7020).
During the recent spring reheling outage at VEGP-2, SNC completed inspections as required to be performed under paragraph IV.C.(S)(b) of the Order, consistent with the relaxation granted by the NRC (TAC Nos. MD 1805 and MD 1806). SNC hereby reports the results of those inspections as required by paragraph 1V.E of the Order. In addition, this letter reports the results of a visual inspection performed under paragraph IV.D of the Order.
U. S. Nuclear Regulatory Commission NL 1260 Page 2 Examinations Required by the First Revised,NRCOrder EA-03-009, Establishing Interim Inspection Requirements for Reactor Pressure Vessel Heads at Pressurized Water Reactors:
As required by paragraph IV.A of the Order, SNC calculated the Effective Degradation Year (EDY) value at the end of the last operating cycle (2R12) for VEGP-2. The EDY value is 3.06 years which places VEGP-2 into the Low (EDY c8) category for susceptibility to primary water stress corrosion cracking (PWSCC) established by Paragraph IV.B. The susceptibility category determines the required examinations and timing of those examinations. An examination was completed during 2R12, satisfying the portion of paragraph IV.C.(3) of the Order which specified an inspection meeting the requirements of paragraph IV.C.(S)(b) consistent with the relaxation request granted by the NRC (TAC Nos. MD 1805 and MD 1806). Full inspection coverage is not achievable at VEGP for all RPV head nozzles, because of nozzle end geometry. Specifically, the bottom end of these nozzles are externally threaded or internally tapered, or both. The relaxation request granted by the NRC consisted of volumetric examination of each nozzle from 2 inches above the J-groove weld down to the maximum extent possible, with a minimum required inspection distance below the J-groove weld to exceed the 6 effective full power years (EFPY) crack growth evaluation limit. The inspection requirement of paragraph IV.D was also performed on the RPV top head during 2R12.
Paragra~hIV.C.(SMb) Insvection Results:
The examination scope satisfying the portion of paragraph IV.C.(3) of the Order, which specified an inspection meeting the requirements of paragraph IV.C.(S)(b)(i) for VEGP-2, included ultrasonic, eddy current, and leakage assessment of the 78 CRDM penetration nozzles. The scope also included a manual eddy current examination of the RPV head vent line penetration.
Of the 78 CRDM penetration nozzles inspected, none showed detectable degradation.
There were no indications of leak paths identified in the shrink fit areas. All penetrations were inspected from 2 inches above the highest point of the root of the J-groove weld (on a horizontal plane perpendicular to the nozzle axis), and 77 penetrations were inspected 1 inch or greater below the toe of the J-groove weld. Penetration number 77 had data collected from less than 1 inch below the lowest point at the toe of the J-groove weld, but in all cases coverage was achieved in accordance with the relaxed scope requirement.
There was one surface geometry indication identified during the eddy current reactor vessel head vent line penetration examination.
U. S. Nuclear Regulatory Commission NL 1260 Page 3 Thermal Sleeve Examinations:
Thermal sleeves were examined for wear and measurements taken at locations where wear was found. Wear of varying magnitudes was found, with more significant wear at nine locations and minimal wear at 23 locations. The wear areas extend, at most, 360-degrees around the thermal sleeves, but at many locations only partially around the thermal sleeve tube. Wear has been found only at penetrations located toward the periphery of the reactor head.
The wear is attributed to the thermal sleeve contacting the inside diameter of the CRDM head adapter tube due to a flow-induced whirling motion of the thermal sleeve. The sleeve-to-adapter contact resulted in wear of material on the outside diameter of the sleeve. The most extensive wear (at 4 unrodded locations, penetrations 62,63,64, and
- 65) thinned the sleeve wall to less than a minimum acceptable thickness when very conservative assumptions were made as to the wear rate for the next cycle of operation, e.g. all wear occurred in the last cycle. Based on the amount of wear found and the probability that the wear will continue, the lower 40 inches of the thermal sleeves (to bottom of funnel) at the 4 unrodded penetration locations have been removed.
An analysis CN-RIDA-07-40, 'Thermal Sleeve Wear Criteria Analysis, March 30,2007,"
has been performed to determine a minimum wall thickness criterion that would allow continued operation with the thermal sleeves that have exhibited wear. The analysis examined wear, fatigue, and stress intensity for two groups of the highest wearing rodded penetrations. The analysis established a minimum wall thickness and maximum predicted wear depth for the next cycle. Based on eddy-current wear depth measurements and video scans, it was determined that the minimum wall thickness and maximum wear depth limits will not be exceeded for an additional cycle. Prior to the start of the next operating cycle, this condition will be re-evaluated.
Paragraph IV.D Insvection Results:
Visual inspections were performed to identify potential boric acid leaks from pressure-retaining components above the RPV head as required by paragraph IV.D of the Order.
No new boric acid residue or evidence attributed to active leakage was found.
The examinations performed were documented by a written report.
U. S. Nuclear Regulatory Commission NL 1260 Page 4 This letter contains no NRC commitments. If you have any questions, please advise.
Sincerely, Manager, Nuclear Licensing cc: Southern Nuclear Overatinrr Comvanv Mr. J. T. Gasser, Executive Vice President Mr. T. E. Tynan, Vice President - Vogtle Mr. D. H. Jones, Vice President -Engineering RType: CVC7000 U. S. Nuclear Rermlatorv Commission Dr. W. D. Travers, Regional Administrator Mr. B. K. Singal, NRR Project Manager - Vogtle Mr. G. J. McCoy, Senior Resident Inspector - Vogtle