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Category:Letter type:NL
MONTHYEARNL-21-034, Notification of Expected Date of Transfer of Ownership of Nuclear Units to Holtec Indian Point 2, LLC and Holtec Indian Point 3, LLC; and Notification of Receipt of All Required Regulatory Approvals2021-05-26026 May 2021 Notification of Expected Date of Transfer of Ownership of Nuclear Units to Holtec Indian Point 2, LLC and Holtec Indian Point 3, LLC; and Notification of Receipt of All Required Regulatory Approvals NL-21-039, Response to Request for Additional Information - License Amendment Request to Revise the Indian Point Nuclear Generating Unit No. 3 Licensing Basis to Incorporate the Installation and Use of a New Auxiliary2021-05-20020 May 2021 Response to Request for Additional Information - License Amendment Request to Revise the Indian Point Nuclear Generating Unit No. 3 Licensing Basis to Incorporate the Installation and Use of a New Auxiliary NL-21-033, Certifications of Permanent Cessation of Power Operations and Permanent Removal of Fuel from the Reactor Vessel2021-05-11011 May 2021 Certifications of Permanent Cessation of Power Operations and Permanent Removal of Fuel from the Reactor Vessel NL-21-032, Termination of Emergency Response Data System Feed to the U.S. Nuclear Regulatory Commission at Indian Point Energy Center2021-05-11011 May 2021 Termination of Emergency Response Data System Feed to the U.S. Nuclear Regulatory Commission at Indian Point Energy Center NL-21-005, Cancellation of Commitments Related to Beyond-Design-Basis External Events Seismic and Flooding Actions2021-05-11011 May 2021 Cancellation of Commitments Related to Beyond-Design-Basis External Events Seismic and Flooding Actions NL-21-030, Submittal of 2020 Annual Radiological Environmental Operating Report2021-05-0606 May 2021 Submittal of 2020 Annual Radiological Environmental Operating Report NL-21-027, Registration of Spent Fuel Cask Use2021-04-20020 April 2021 Registration of Spent Fuel Cask Use NL-21-021, Registration of Spent Fuel Cask Use2021-04-19019 April 2021 Registration of Spent Fuel Cask Use NL-21-017, Pre-Notice of Disbursement from Decommissioning Trusts2021-04-0808 April 2021 Pre-Notice of Disbursement from Decommissioning Trusts NL-21-010, Submittal of 2020 Annual Fitness for Duty Program Performance Data Report and Fatigue Management Program Data Report2021-02-17017 February 2021 Submittal of 2020 Annual Fitness for Duty Program Performance Data Report and Fatigue Management Program Data Report NL-21-006, Relief Request IP3-ISI-RR-16, Proposed Alternative to American Society of Mechanical Engineers Code Case N-513-4 Inspection Requirement2021-02-10010 February 2021 Relief Request IP3-ISI-RR-16, Proposed Alternative to American Society of Mechanical Engineers Code Case N-513-4 Inspection Requirement NL-21-014, Response to 2nd Round Request for Additional Information - License Amendment Request to Revise the Licensing Basis to Incorporate the Installation and Use of a New Auxiliary Lifting Device2021-01-26026 January 2021 Response to 2nd Round Request for Additional Information - License Amendment Request to Revise the Licensing Basis to Incorporate the Installation and Use of a New Auxiliary Lifting Device NL-20-082, Notice of Planned Transfer of Decommissioning Funds2020-12-14014 December 2020 Notice of Planned Transfer of Decommissioning Funds NL-20-081, Pre-Notice of Disbursement from Decommissioning Trusts2020-12-0909 December 2020 Pre-Notice of Disbursement from Decommissioning Trusts NL-20-080, Report in Accordance with 10 CFR 71.95(a) for Failure to Comply with Certificate of Compliance No. 71-93212020-11-19019 November 2020 Report in Accordance with 10 CFR 71.95(a) for Failure to Comply with Certificate of Compliance No. 71-9321 NL-20-079, (IP2 and IP3) - Request for a One-Time Exemption from 10 CFR 73, Appendix B, Section VI, Subsection C.3.(I)(1) Regarding Annual Force-on-Force (FOF) Exercises, Due to Covid 19 Pandemic2020-11-12012 November 2020 (IP2 and IP3) - Request for a One-Time Exemption from 10 CFR 73, Appendix B, Section VI, Subsection C.3.(I)(1) Regarding Annual Force-on-Force (FOF) Exercises, Due to Covid 19 Pandemic NL-20-077, Submittal of Quality Assurance Program Manual Revision 22020-11-0909 November 2020 Submittal of Quality Assurance Program Manual Revision 2 NL-20-078, Response to Requests for Additional Information - License Amendment Request to Revise the Licensing Basis to Incorporate the Installation and Use of a New Auxiliary Lifting Device2020-11-0909 November 2020 Response to Requests for Additional Information - License Amendment Request to Revise the Licensing Basis to Incorporate the Installation and Use of a New Auxiliary Lifting Device NL-20-076, Revision of Commitment Related to Nuclear Reactor Safeguards Interim Compensatory Measure - Section B.5.b Issue Regarding Spent Fuel Dispersal2020-11-0202 November 2020 Revision of Commitment Related to Nuclear Reactor Safeguards Interim Compensatory Measure - Section B.5.b Issue Regarding Spent Fuel Dispersal NL-20-069, One-time Scheduler Exemption Request from 10 CFR 50, Appendix E Biennial Emergency Preparedness Exercise Requirements Due to COVID-19 Public Health Emergency2020-10-0808 October 2020 One-time Scheduler Exemption Request from 10 CFR 50, Appendix E Biennial Emergency Preparedness Exercise Requirements Due to COVID-19 Public Health Emergency NL-20-070, Response to Requests for Additional Information, License Amendment Request to Revise the Indian Point Nuclear Generating Unit No. 3 Licensing Basis to Incorporate the Installation and Use of a New Auxiliary Lifting Device2020-10-0202 October 2020 Response to Requests for Additional Information, License Amendment Request to Revise the Indian Point Nuclear Generating Unit No. 3 Licensing Basis to Incorporate the Installation and Use of a New Auxiliary Lifting Device NL-20-067, Redacted Version of Response to U.S. Nuclear Regulatory Commission Region I Letter Regarding Algonquin Incremental Market Project Pipeline2020-09-16016 September 2020 Redacted Version of Response to U.S. Nuclear Regulatory Commission Region I Letter Regarding Algonquin Incremental Market Project Pipeline NL-20-064, 10 CFR 50.59(d)(2) Summary Report of Changes, Tests and Experiments2020-09-0101 September 2020 10 CFR 50.59(d)(2) Summary Report of Changes, Tests and Experiments NL-20-060, Status of Remaining Actions for Generic Letter 2004-022020-08-11011 August 2020 Status of Remaining Actions for Generic Letter 2004-02 NL-20-057, Cancellation of Commitment Related to Large Break LOCA Reanalysis2020-07-30030 July 2020 Cancellation of Commitment Related to Large Break LOCA Reanalysis NL-20-0851, 30-Day 10 CFR 21 Notification - Continuously Energized Eaton D26 Relays Could Fail to Deenergize Because of an Organic C3 Insulating Material2020-07-22022 July 2020 30-Day 10 CFR 21 Notification - Continuously Energized Eaton D26 Relays Could Fail to Deenergize Because of an Organic C3 Insulating Material NL-20-051, Submittal of Quality Assurance Program Manual, Revision 1 for the Indian Point Energy Center2020-07-0707 July 2020 Submittal of Quality Assurance Program Manual, Revision 1 for the Indian Point Energy Center NL-20-052, Unsatisfactory 10 CFR 26 Fitness-For-Duty Blind Performance Testing Results2020-07-0707 July 2020 Unsatisfactory 10 CFR 26 Fitness-For-Duty Blind Performance Testing Results NL-20-012, Application to Revise Provisional Operating License and Technical Specifications2020-06-30030 June 2020 Application to Revise Provisional Operating License and Technical Specifications NL-20-050, Response to U.S. Nuclear Regulatory Commission Region I Letter Regarding Algonquin Incremental Market Project Pipeline2020-06-24024 June 2020 Response to U.S. Nuclear Regulatory Commission Region I Letter Regarding Algonquin Incremental Market Project Pipeline NL-20-041, Registration of Unit 3 Spent Fuel Cask Use2020-05-13013 May 2020 Registration of Unit 3 Spent Fuel Cask Use NL-20-042, Certifications of Permanent Cessation of Power Operations and Permanent Removal of Fuel from the Reactor Vessel2020-05-12012 May 2020 Certifications of Permanent Cessation of Power Operations and Permanent Removal of Fuel from the Reactor Vessel NL-20-033, Technical Specifications Proposed Change - Permanently Defueled Technical Specifications2020-04-28028 April 2020 Technical Specifications Proposed Change - Permanently Defueled Technical Specifications NL-20-038, Response to U.S. Nuclear Regulatory Commission Region I Letter Regarding Algonquin Incremental Market Project Pipeline2020-04-23023 April 2020 Response to U.S. Nuclear Regulatory Commission Region I Letter Regarding Algonquin Incremental Market Project Pipeline NL-20-035, Response to Request for Additional Information - Temporary Exemption Request from 10 CFR Appendix R, Section Iii.H Due to COVID-19 Pandemic2020-04-16016 April 2020 Response to Request for Additional Information - Temporary Exemption Request from 10 CFR Appendix R, Section Iii.H Due to COVID-19 Pandemic NL-20-034, Temporary Exemption Request from 10 CFR Appendix R, Section Iii.H Due to COVID-19 Pandemic2020-04-13013 April 2020 Temporary Exemption Request from 10 CFR Appendix R, Section Iii.H Due to COVID-19 Pandemic NL-20-021, Proposed License Amendment to Revise the Licensing Basis to Incorporate the Installation and Use of a New Auxiliary Lifting Device2020-03-24024 March 2020 Proposed License Amendment to Revise the Licensing Basis to Incorporate the Installation and Use of a New Auxiliary Lifting Device NL-20-020, Submittal of 2019 Annual Fitness for Duty Performance Data Report Update2020-02-26026 February 2020 Submittal of 2019 Annual Fitness for Duty Performance Data Report Update NL-20-015, Submittal of 2019 Annual Fitness for Duty Program Performance Data Report and Fatigue Management Program Data Report2020-02-10010 February 2020 Submittal of 2019 Annual Fitness for Duty Program Performance Data Report and Fatigue Management Program Data Report NL-20-008, Transmittal of Presentation Slides for Partially Closed Pre-Submittal Meeting to Discuss a Planned License Amendment Request to Replace the Fuel Handling Building Crane2020-01-0606 January 2020 Transmittal of Presentation Slides for Partially Closed Pre-Submittal Meeting to Discuss a Planned License Amendment Request to Replace the Fuel Handling Building Crane NL-19-094, 2018 Annual 10 CFR 50.46 Emergency Core Cooling System Evaluation Changes Report2019-12-16016 December 2019 2018 Annual 10 CFR 50.46 Emergency Core Cooling System Evaluation Changes Report NL-19-084, Application for Order Consenting to Transfers of Control of Licenses and Approving Conforming License Amendments2019-11-21021 November 2019 Application for Order Consenting to Transfers of Control of Licenses and Approving Conforming License Amendments NL-19-093, Proposed Technical Specifications (TS) Changes - Indian Point Nuclear Generating Unit 3 TS SR 3.7.7.2 and TS 3.7.6, Required Action A.12019-11-21021 November 2019 Proposed Technical Specifications (TS) Changes - Indian Point Nuclear Generating Unit 3 TS SR 3.7.7.2 and TS 3.7.6, Required Action A.1 NL-19-092, Request for Rescission of Order Modifying Licenses with Regard to Requirements for Mitigation Strategies for Beyond-Design-Basis External Events (Order Number EA-12-049)2019-11-20020 November 2019 Request for Rescission of Order Modifying Licenses with Regard to Requirements for Mitigation Strategies for Beyond-Design-Basis External Events (Order Number EA-12-049) NL-19-043, Request for Partial Exemption from Record Retention Requirements in 10 CFR 50.122019-10-22022 October 2019 Request for Partial Exemption from Record Retention Requirements in 10 CFR 50.12 NL-19-073, Request for Relaxation of Order Modifying Licenses with Regard to Requirements for Mitigation Strategies for Beyond-Design-Basis External Events (Order Number EA-12-049)2019-10-22022 October 2019 Request for Relaxation of Order Modifying Licenses with Regard to Requirements for Mitigation Strategies for Beyond-Design-Basis External Events (Order Number EA-12-049) NL-19-078, Supplement to Technical Specifications Proposed Change - Permanently Defueled Technical Specifications2019-10-22022 October 2019 Supplement to Technical Specifications Proposed Change - Permanently Defueled Technical Specifications NL-19-091, Independent Spent Fuel Storage Installation (Isfsi), Registration of Spent Fuel Cask Use2019-10-17017 October 2019 Independent Spent Fuel Storage Installation (Isfsi), Registration of Spent Fuel Cask Use NL-19-090, Registration of Unit 2 Spent Fuel Cask Use2019-10-0909 October 2019 Registration of Unit 2 Spent Fuel Cask Use NL-19-079, 50.59(d)(2) Summary Report of Changes, Tests and Experiments2019-09-26026 September 2019 50.59(d)(2) Summary Report of Changes, Tests and Experiments 2021-05-06
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Enterav Nuclear Northeast Indian Point Energy Center 295 Broadway, Suite I
-- er P.O. Box 249 Buchanan, NY 10511-0249 Fred Dacimo Site Vice President Tel 914 734 6700 May 31, 2005 Re: Indian Point Unit 3 Docket No. 50-286 NL-05-063 Document Control Desk U.S. Nuclear Regulatory Commission Mail Stop O-Pl-17 Washington, DC 20555-0001
Subject:
Reactor Vessel Lower Head Inspection Results; Indian Point Unit 3. Spring 2005 Refuelina Outage (3R13)
Reference:
- 1) NRC Bulletin 2003-02, "Leakage from Reactor Pressure Vessel Lower Head Penetrations and Reactor Coolant Pressure Boundary Integrity", dated August 21, 2003
- 2) Entergy letter to NRC (NL-03-178); "90-Day Response to NRC Bulletin 2003-02 Regarding Leakage from Reactor Pressure Vessel Lower Head Penetrations and Reactor Coolant Pressure Boundary Integrity", dated November 13, 2003
Dear Sir:
This letter provides the Reactor Vessel Lower Head Inspection Report (Attachment 1) for Indian Point Unit 3 (IP3), in accordance with Requested Information Item (2) (Reference 1). The inspection was performed during refueling outage 3R13 that was completed on April 7, 2005.
The inspection was performed in accordance with the plan provided in Reference 2.
The inspection consisted of a visual examination of the lower head region adjacent to each bottom mounted instrumentation (BMI) penetration including the annulus region between the penetration and the Alloy 600 weld pad. Cleaning of the lower head penetrations annulus regions to remove this boron residue was also implemented during 3R13.
Based on the results of this inspection, Entergy concludes that there is no evidence of leakage resulting from a breach of the lower head penetrations or the attaching j-groove weld (i.e. no "popcorn-like" evidence of boron deposits at the annulus between the penetration and the weld pad). Although there were minor boron streaks and boron residue in regions of the lower head, the annulus region of each penetration was relatively free of boron residue. In those instances where boron residue was present in the annulus region, this residue was clearly traceable to Aioq
NL-05-063 Docket 50-286 Page 2 of 3 sources above the penetration by following the boron streaks. In addition, residue identified in these regions, did not show any 'popcorn-like' characteristics which would be expected from a pressure boundary leak. The source of boron residue was concluded to be leakage from sources located above the lower head region Residue in the lower head annulus regions were subsequently steam cleaned after completion of the inspection with an additional as-left, baseline inspection performed prior to exiting the refueling outage.
There are no new commitments made by Entergy contained in this letter. If you have any questions, please contact Mr. Patric W. Conroy, Manager, Licensing at (914) 734-6668.
Very truly yours, FeR. Dacimo Site Vice President Indian Point Energy Center (Reactor Vessel Lower Head Inspection Results; Indian Point Unit 3, Spring 2005 Refueling Outage (3R13))
cc: see next page
NL-05-063 Docket 50-286 Page 3 of 3 cc: Mr. John P. Boska, Senior Project Manager, Section 2 Project Directorate I Division of Licensing Project Management U.S. Nuclear Regulatory Commission Mr. Samuel J. Collins Regional Administrator, Region 1 U.S. Nuclear Regulatory Commission Resident Inspector's Office Indian Point Unit 3 Nuclear Power Plant U.S. Nuclear Regulatory Commission Mr. Paul Eddy New York State Dept. of Public Service
ATTACHMENT 1 TO NL-05-063 REACTOR VESSEL LOWER HEAD INSPECTION RESULTS; INDIAN POINT UNIT 3, SPRING 2005 REFUELING OUTAGE (3R13)
ENTERGY NUCLEAR OPERATIONS, INC.
INDIAN POINT NUCLEAR GENERATING UNIT NO. 3 DOCKET NO. 50-286
NL-05-063 Docket No. 50-286 Attachment 1 Page 1 of 2 REACTOR VESSEL LOWER HEAD INSPECTION RESULTS; INDIAN POINT UNIT 3, SPRING 2005 REFUELING OUTAGE (3R13)
Item (2) of Bulletin 2003-02 requested that, within 60 days of plant restart following the next inspection of the RPV lower head penetrations, Licensees should submit to the NRC (1) a summary of the inspections performed, (2) the extent of the inspections, (3) the method used, (4) a description of the as-found condition of the lower head, (5) any findings of relevant indications of through wall leakage and (6) a summary of the disposition of any findings of boric acid deposits and any corrective actions taken as a result of indications found.
(1) Summary of Inspections Performed During the recently completed 3R13 refueling outage, Indian Point Unit 3 (1P3) removed the individual insulation half-moon plates adjacent to each of the 58 lower head penetrations and performed a bare metal visual (BMV) examination of the lower head region adjacent to each penetration including 3600 of the annulus region between the penetration and the Alloy 600 weld pad.
(2) Extent of the Inspections As discussed in item (1) above, each of the 58 lower RPV head penetrations were inspected including the Alloy 600 penetration, the Alloy 600 weld pad and 3600 of the annulus between the penetration and the weld pad.
(3) Method Used This inspection was a visual examination performed with remote video equipment and provided a resolution equivalent to the ASME Section Xl VT-2 requirements as a minimum. The inspection results were reviewed by certified VT-2 personnel meeting the requirements of ASME Section XI.
(4) DescriDtion of the As-Found Condition of the Lower Head The inspections required by Bulletin 2003-02 were performed in the beginning of the refueling outage (i.e. prior to refueling operations) and identified no evidence of leakage resulting from a breach of the lower head penetrations or the attaching j-groove weld (i.e. no "popcorn-like" evidence of boron deposits at the annulus between the penetration and the weld pad). Although this inspection identified no evidence of RCS leakage resulting from a through wall defect, it identified some minor boron residue and streaking in localized regions of the lower head including some annuli regions. This residue was characterized primarily as two-dimensional (i.e. streaks) resulting from flow of borated water from sources located above the outer most penetrations. Nine locations were identified with some minor boron residue either on or adjacent to the annulus region. In all instances where boron residue was detected in the annulus region, the residue could be traced to sources above the penetration by following the streaks. The source of these streaks and residue was identified as previous leaks from sources above the lower head.
NL-05-063 Docket No. 50-286 Attachment 1 Page 2 of 2 Following refueling operations, additional boron streaks and residue were identified on the outside surface of the lower head insulation. As a result of this additional residue, sixteen penetrations (i.e. the penetrations located in the regions of the new boron streaks) were re-examined to determine if the new leakage introduced during refueling operations, had resulted in additional boron residue at the annuli of additional penetrations, which could impact the effectiveness of future BMV examinations. As a result of this re-inspection, four additional penetrations were identified with some boron residue at or adjacent to the annulus region resulting in a total of thirteen penetrations with some boron residue (nine identified prior to refueling operations plus the additional four identified as having boron residue as a result of and subsequent to refueling operations). All thirteen of these penetrations were steam cleaned during the refueling outage and a post cleaning inspection was also performed of all thirteen penetrations to verify the effectiveness of the cleaning.
(5) Findings of Relevant Indications of Through Wall Leakage The inspections performed during 3R13 identified no evidence of leakage resulting from a breach of the lower head penetrations or the attaching j-groove weld (i.e. no popcorn-like evidence of boron deposits at the annulus between the penetration and the weld pad). The boron residue detected during the pre-refueling inspection was attributed to leakage from components located in the upper vessel head region while residue detected during the post-refueling inspection was attributed to reactor cavity leakage.
This resulted in thirteen penetrations which required subsequent cleaning to ensure that future BMV inspections can be performed in an effective manner.
(6) Summary of the Disposition of any Findings of Boric Acid Deposits and any Corrective Actions taken as a Result of Indications Found As discussed above, the residue detected on the lower head surface was a result of either leakage from components in the upper head region or from refueling cavity leakage during 3R13. This resulted in thirteen penetrations which required steam cleaning to remove the residue from the annulus regions. A post cleaning inspection confirmed the effectiveness of the cleaning in removing the boron residue.
References
- 1. NRC Bulletin 2003-02, "Leakage from Reactor Pressure Vessel Lower Head Penetrations and Reactor Coolant Pressure Boundary Integrity", dated August 21, 2003
- 2. Entergy letter to NRC (NL-03-178); "90-Day Response to NRC Bulletin 2003-02 Regarding Leakage from Reactor Pressure Vessel Lower Head Penetrations and Reactor Coolant Pressure Boundary Integrity", dated November 13, 2003