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Category:Letter type:RBG
MONTHYEARRBG-48271, Supplement to License Amendment Request to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times RITSTF Initiative 4b and Application to Adopt 10 CFR 50.69, Risk2024-01-12012 January 2024 Supplement to License Amendment Request to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times RITSTF Initiative 4b and Application to Adopt 10 CFR 50.69, Risk RBG-48267, Reply to a Notice of Violation, NRC Inspection Report 05000458/20230032023-12-0707 December 2023 Reply to a Notice of Violation, NRC Inspection Report 05000458/2023003 RBG-48264, Core Operating Limits Report (COLR) - Cycle 23, Revision 12023-11-0606 November 2023 Core Operating Limits Report (COLR) - Cycle 23, Revision 1 RBG-48260, Notification of Readiness for Supplemental Inspection2023-10-12012 October 2023 Notification of Readiness for Supplemental Inspection RBG-48258, Notification of Readiness for Supplemental Inspection2023-10-0505 October 2023 Notification of Readiness for Supplemental Inspection RBG-48259, Revision to Reply to Notice of Violation; EA-23-0552023-10-0303 October 2023 Revision to Reply to Notice of Violation; EA-23-055 RBG-48254, Report of Changes and Errors to 10CFR50.462023-09-21021 September 2023 Report of Changes and Errors to 10CFR50.46 RBG-48249, Reply to a Notice of Violation, EA-23-0712023-09-14014 September 2023 Reply to a Notice of Violation, EA-23-071 RBG-48253, Submittal of Owner'S Activity Report Form for Cycle 222023-09-12012 September 2023 Submittal of Owner'S Activity Report Form for Cycle 22 RBG-48247, Reply to Notice of Violation; EA-23-0552023-08-21021 August 2023 Reply to Notice of Violation; EA-23-055 RBG-48226, Core Operating Limits Report (COLR) - Cycle 23, Revision 02023-05-31031 May 2023 Core Operating Limits Report (COLR) - Cycle 23, Revision 0 RBG-48237, Response to NRC Integrated Inspection Report 05000458/20230012023-05-25025 May 2023 Response to NRC Integrated Inspection Report 05000458/2023001 RBG-48220, Submittal of 2022 Annual Radioactive Effluent Release Report2023-04-25025 April 2023 Submittal of 2022 Annual Radioactive Effluent Release Report RBG-48221, 2022 Annual Radiological Environmental Operating Report2023-04-25025 April 2023 2022 Annual Radiological Environmental Operating Report RBG-48142, License Amendment Request to Revise Technical Specifications to Adopt Risk Informed Completion Times TSFT-505, Revision 2, Provide Risk-Informed Extended Completion Times - RITSTF Initiative 4b2023-02-27027 February 2023 License Amendment Request to Revise Technical Specifications to Adopt Risk Informed Completion Times TSFT-505, Revision 2, Provide Risk-Informed Extended Completion Times - RITSTF Initiative 4b RBG-48143, Application to Adopt 10 CFR 50.69, Risk-Informed Categorization and Treatment of Structures, Systems and Components for Nuclear Power Reactors2023-02-27027 February 2023 Application to Adopt 10 CFR 50.69, Risk-Informed Categorization and Treatment of Structures, Systems and Components for Nuclear Power Reactors RBG-48198, Report of Changes and Errors to 10CFR50.462022-09-22022 September 2022 Report of Changes and Errors to 10CFR50.46 RBG-48187, Notification of Spent Fuel Cask Use2022-08-15015 August 2022 Notification of Spent Fuel Cask Use RBG-48184, Notification of Spent Fuel Cask Use2022-07-18018 July 2022 Notification of Spent Fuel Cask Use RBG-48178, Notification of Spent Fuel Cask Use2022-06-29029 June 2022 Notification of Spent Fuel Cask Use RBG-48166, Supplement to Special Report for Tritium Discovered Onsite2022-05-12012 May 2022 Supplement to Special Report for Tritium Discovered Onsite RBG-48149, 2021 Annual Radioactive Effluent Release Report2022-04-27027 April 2022 2021 Annual Radioactive Effluent Release Report RBG-48148, 2021 Annual Radiological Environmental Operating Report2022-04-27027 April 2022 2021 Annual Radiological Environmental Operating Report RBG-48134, Inservice Testing Program Relief Request VRR-RBS-2021-1 Pressure Isolation Valve Testing Frequency2021-11-29029 November 2021 Inservice Testing Program Relief Request VRR-RBS-2021-1 Pressure Isolation Valve Testing Frequency RBG-48136, Additional Information for the 2020 Annual Radioactive Effluent Release Report2021-11-12012 November 2021 Additional Information for the 2020 Annual Radioactive Effluent Release Report RBG-48137, Additional Information for the 2019 Annual Radioactive Effluent Release Report2021-11-12012 November 2021 Additional Information for the 2019 Annual Radioactive Effluent Release Report RBG-48128, Reply to a Notice of Violation; EA-21-017, 030 and 0502021-10-29029 October 2021 Reply to a Notice of Violation; EA-21-017, 030 and 050 RBG-48129, Payment of a Civil Penalty2021-10-21021 October 2021 Payment of a Civil Penalty RBG-48112, Report of Changes and Errors to 10CFR50.462021-09-16016 September 2021 Report of Changes and Errors to 10CFR50.46 RBG-48110, Core Operating Limits Report (COLR) - Cycle 22, Revision 12021-08-19019 August 2021 Core Operating Limits Report (COLR) - Cycle 22, Revision 1 RBG-48104, Fitness for Duty Blind Quality Assurance Specimen Testing Error2021-06-30030 June 2021 Fitness for Duty Blind Quality Assurance Specimen Testing Error RBG-48099, Submittal of Owner'S Activity Report Form for Cycle 212021-06-16016 June 2021 Submittal of Owner'S Activity Report Form for Cycle 21 RBG-48083, Application to Add License Condition Concerning Receipt, Possession, and Use of Byproduct Materials2021-06-15015 June 2021 Application to Add License Condition Concerning Receipt, Possession, and Use of Byproduct Materials RBG-48093, Corrected 2020 Annual Radiological Environmental Operating Report2021-05-20020 May 2021 Corrected 2020 Annual Radiological Environmental Operating Report RBG-48082, 2020 Annual Radiological Environmental Operating Report2021-04-20020 April 2021 2020 Annual Radiological Environmental Operating Report RBG-48081, 2020 Annual Radioactive Effluent Release Report2021-04-20020 April 2021 2020 Annual Radioactive Effluent Release Report RBG-48078, Core Operating Limits Report (COLR) - Cycle 22, Revision 02021-03-14014 March 2021 Core Operating Limits Report (COLR) - Cycle 22, Revision 0 RBG-48075, Notification of Deviation from BWRVIP Guidelines2021-02-24024 February 2021 Notification of Deviation from BWRVIP Guidelines RBG-48074, Spent Fuel Storage Radioactive Effluent Release Report for 20202021-02-22022 February 2021 Spent Fuel Storage Radioactive Effluent Release Report for 2020 RBG-48061, One-Time Schedular Exemption Request from 10 CFR 50, Appendix E Biennial Emergency Preparedness Exercise Requirements Due to COVID-19 Public Health Emergency2020-12-0303 December 2020 One-Time Schedular Exemption Request from 10 CFR 50, Appendix E Biennial Emergency Preparedness Exercise Requirements Due to COVID-19 Public Health Emergency RBG-48054, Application to Adopt GL 86-10 Standard License Condition for Fire Protection Program2020-11-0202 November 2020 Application to Adopt GL 86-10 Standard License Condition for Fire Protection Program RBG-48049, Reply to a Notice of Violation; EA-20-0582020-10-26026 October 2020 Reply to a Notice of Violation; EA-20-058 RBG-48038, Request for One-Time Exemption from 10 CFR 50, Appendix E Biennial Emergency Preparedness Evaluated Offsite Exercise Requirements Due to Covid 19 Pandemic2020-10-0606 October 2020 Request for One-Time Exemption from 10 CFR 50, Appendix E Biennial Emergency Preparedness Evaluated Offsite Exercise Requirements Due to Covid 19 Pandemic RBG-48042, Submittal of Rev. 48 to Emergency Plan2020-09-22022 September 2020 Submittal of Rev. 48 to Emergency Plan RBG-48039, Report of Changes and Errors to 10CFR50.462020-09-16016 September 2020 Report of Changes and Errors to 10CFR50.46 RBG-48033, Application to Revise Technical Specifications to Adopt TSTF-582, Reactor Pressure Vessel Water Inventory Control (RPV WIC) Enhancements2020-09-0404 September 2020 Application to Revise Technical Specifications to Adopt TSTF-582, Reactor Pressure Vessel Water Inventory Control (RPV WIC) Enhancements RBG-48023, Submittal of Revs. 46 and 47 to Emergency Plan and Revised Emergency Implementing Procedures2020-06-0909 June 2020 Submittal of Revs. 46 and 47 to Emergency Plan and Revised Emergency Implementing Procedures RBG-48019, 2019 Annual Radioactive Effluent Release Report2020-04-30030 April 2020 2019 Annual Radioactive Effluent Release Report RBG-48020, Annual Radiological Environmental Operating Report2020-04-30030 April 2020 Annual Radiological Environmental Operating Report RBG-48018, Withdrawal of License Amendment Request to Extend the RBS Emergency Plan Implementation Date2020-04-24024 April 2020 Withdrawal of License Amendment Request to Extend the RBS Emergency Plan Implementation Date 2024-01-12
[Table view] Category:Licensee Response to Notice of Violation
MONTHYEARRBG-48267, Reply to a Notice of Violation, NRC Inspection Report 05000458/20230032023-12-0707 December 2023 Reply to a Notice of Violation, NRC Inspection Report 05000458/2023003 RBG-48259, Revision to Reply to Notice of Violation; EA-23-0552023-10-0303 October 2023 Revision to Reply to Notice of Violation; EA-23-055 RBG-48249, Reply to a Notice of Violation, EA-23-0712023-09-14014 September 2023 Reply to a Notice of Violation, EA-23-071 RBG-48237, Response to NRC Integrated Inspection Report 05000458/20230012023-05-25025 May 2023 Response to NRC Integrated Inspection Report 05000458/2023001 RBG-48128, Reply to a Notice of Violation; EA-21-017, 030 and 0502021-10-29029 October 2021 Reply to a Notice of Violation; EA-21-017, 030 and 050 RBG-48129, Payment of a Civil Penalty2021-10-21021 October 2021 Payment of a Civil Penalty ML21105A4192021-04-15015 April 2021 Reply to Notice of Violation RBG-48049, Reply to a Notice of Violation; EA-20-0582020-10-26026 October 2020 Reply to a Notice of Violation; EA-20-058 RBG-47771, Submittal of Rely to Notice of Violation 05000458/2017-009-012017-07-0606 July 2017 Submittal of Rely to Notice of Violation 05000458/2017-009-01 IR 05000458/20170092017-07-0606 July 2017 Submittal of Rely to Notice of Violation 05000458/2017-009-01 ML15293A4942015-09-30030 September 2015 Supplement to Reply to Notice of Violation EA-15-043 RBG-47615, Reply to a Notice of Violation; EA-15-0432015-09-25025 September 2015 Reply to a Notice of Violation; EA-15-043 RBG-47428, Reply to Notice of Violation: EA-13-1102014-02-0303 February 2014 Reply to Notice of Violation: EA-13-110 RBG-47061, Supplement - Reply to a Notice of Violation: EA-10-0952010-08-30030 August 2010 Supplement - Reply to a Notice of Violation: EA-10-095 RBG-47046, Reply to a Notice of Violation: EA-10-0952010-07-19019 July 2010 Reply to a Notice of Violation: EA-10-095 RBG-46213, Reply to a Notice of Violation in Inspection Report 05000458/02-07, River Bend Station, Unit 12004-01-28028 January 2004 Reply to a Notice of Violation in Inspection Report 05000458/02-07, River Bend Station, Unit 1 RBG-46009, Owner Controlled Area Public Information2002-08-30030 August 2002 Owner Controlled Area Public Information 2023-09-14
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- ) entergy Phil Hansett Site Vice President River Bend Station 225-381-437 4 RBG-48267 10 CFR 2.201 December 7, 2023 ATTN: Document Control Desk U.S. Nuclear Regulatory Commission Washington, DC 20555-0001
Subject:
Reply to a Notice of Violation, NRC Inspection Report 05000458/2023003 River Bend Station, Unit 1 NRC Docket No. 50-458 Renewed Facility Operating License No. NPF-47
Reference:
NRC letter to Entergy, "River Bend Station - Integrated Inspection Report 05000458/2023003 and Notice of Violation," (ADAMS Accession No. ML23310A032), dated November 13, 2023.
In accordance with 10 CFR 2.201, Entergy Operations, Inc. (Entergy) hereby submits the Reply to Notice of Violation, EA-23-065, for River Bend Station. As requested, the Enclosure contains the following: (1) the reason for the violation; (2) the corrective steps that have been taken and the results achieved; (3) the corrective steps that will be taken; and (4) the date when full compliance will be achieved.
Should you have any questions concerning this issue, please contact Randy Crawford, Manager, Regulatory Assurance, at 225-381-4177.
Respectfully, Phil Hansett PH/twf Entergy Operations, Inc., 5485 U.S. Highway 61 N. St. Francisville, LA 70775
RBG-48267 Page 2 of 2
Enclosure:
Reply to Notice of Violation; EA-23-065 cc: NRC Regional Administrator - Region IV NRC Senior Resident Inspector - River Bend Station NRC Document Control Desk R4Enforcement@nrc.gov
Enclosure RBG-48267 Reply to Notice of Violation; EA-23-065
RBG-48267 Enclosure Page 1 of 3 Reply to Notice of Violation EA-23-065 In the U.S. Nuclear Regulatory Commission (NRC) letter to Entergy Operations, Inc. (Entergy),
"River Bend Station - Integrated Inspection Report 05000458/2023003 and Notice of Violation,"
(ADAMS Accession No. ML23310A032), dated November 13, 2023, the NRC issued Notice of Violation EA-23-065 to Entergy's River Bend Station (RBS) as restated below:
1 O CFR 50.59(c)(2)(ii) requires, in part, that a licensee shall obtain a license amendment pursuant to 1 O CFR 50.90 prior to implementing a proposed change if the change would result in more than a minimal increase in the likelihood of occurrence of a malfunction of a structure, system, or component (SSC) important-to-safety previously evaluated in the final safety analysis report (as updated).
Contrary to the above, from October 27, 2011, to September 30, 2023, the licensee failed to obtain a license amendment pursuant to 1 O CFR 50.90 prior to implementing a proposed change, test, or experiment if this activity would result in more than a minimal increase in the likelihood of occurrence of a malfunction of an SSC important-to-safety previously evaluated in the final safety analysis report (as updated). Specifically, the licensee changed the design basis of the ultimate heat sink inventory requirements from providing a 30-day cooling water supply without the need for makeup to providing a less than 30-day cooling water supply with makeup capability, without obtaining a license amendment. The licensee implemented temporary compensatory measures that would ensure a 30-day ultimate heat sink cooling water supply.
Pursuant to the provisions of 10 CFR 2.201, this Enclosure provides Entergy's Reply to Notice of Violation, EA-23-065.
- 1) Reason for the Violation RBS failed to restore compliance to NCV 05000458/2011008-06 because a License Amendment Request was not submitted for a change to the licensing basis for the Ultimate Heat Sink (UHS) that required prior NRC approval.
In the NRC letter to Entergy, "River Bend Station - NRC Component Design Bases Inspection -
Inspection Report 05000458/2011008," (ADAMS Accession No. ML113400127), dated December 6, 2011, the NRC issued Non-Cited Violation 05000458/2011008-06 to RBS as restated below:
The team identified a Severity Level IV, noncited violation of 1 O CFR 50.59, "Changes, Tests, and Experiments," because the licensee failed to obtain a license amendment, pursuant to 1 O CFR 50.90, prior to implementing a change to the ultimate heat sink inventory requirements. Specificality, the licensee changed the design basis of the ultimate heat sink inventory requirements from providing a 30-day cooling water supply without makeup capability to providing a less than 30-day cooling water supply with makeup capability without obtaining a license amendment.
Following the issuance of NCV 05000458/2011008-06 in 2011, RBS intended to correct the condition by submitting a License Amendment Request that would credit makeup to the UHS in less than 30 days to account for system leakage and operation with more than one division of
RBG-48267 Enclosure Page 2 of 3 standby service water in operation; however, the request was later withdrawn on July 7, 2014, due to NRG concerns.
The 2014 Component Design Basis NRG inspection reviewed the corrective actions to address NCV 05000458/2011008-06 and issued another NCV against 1 O CFR 50, Appendix B, Criterion XVI, "Corrective Actions," for failure to take prompt corrective actions to restore compliance following the 2011 violation.
As part of corrective actions from the 2011 and 2014 NCVs, RBS revised the Updated Safety Analysis Report (USAR), Section 9.2.5, to remove the following sentence describing the licensing basis of the UHS:
"Additional makeup is required for system leakage under licensing basis condition and when operating two divisions with system leakage."
While removal of this sentence addressed a portion of the USAR changes that caused the 1 O CFR 50.59 NCV issued in 2011, the NRG determined that additional portions of the RBS licensing basis still rely on the use of make-up to meet the 30-day requirement for the UHS and that RBS had still not received NRG approval for this change. Specifically, USAR Section 9.2.5.1.2 states that, "the capacity of the UHS water storage basin is designed to provide necessary cooling for the period of time (30 days) needed to evaluate the situation, to take corrective action to mitigate the consequences of an accident, and if required to take any necessary measures to permit water replenishment." This is different than the approved section from the Safety Evaluation Report that stated the UHS had more than a 30-day supply with no makeup required.
The original RBS license basis stated that the UHS will last 30 days assuming a single active failure with no makeup required. The allowance for makeup to the UHS was done without prior NRG approval, contrary to 1 O CFR 50.59.
The License Amendment Request was not submitted to the NRG because RBS understood the original UHS licensing basis for the active single failure to be considered was that of the Division II Emergency Diesel Generator. This understanding was based on the originally submitted FSAR. From a plant response perspective, that continues to be the case and, assuming the failure of one Emergency Diesel Generator, the heat load on the UHS continues to allow the UHS to meet the 30-day supply with no makeup requirement. However, considering the heat load on the UHS without the failure of an Emergency Diesel Generator, the UHS would not be able to meet the 30-day supply with no makeup. As a result of this recognition, compensatory measures have been established to ensure a 30-day UHS cooling water supply and a License Amendment Request will be submitted to change the licensing basis. As of the date of this letter, the License Amendment Request has not been submitted.
- 2) Corrective Steps That Have Been Taken and the Results Achieved On June 1, 2023, Compensatory Measures were implemented that ensure a 30-day Ultimate Heat Sink (UHS) cooling water supply.
- Alternate methods to provide make up water to SBCT were established.
- Unnecessary heat load on the SBCT was reduced or eliminated.
RBG-48267 Enclosure Page 3 of 3
- 3) Corrective Steps That Will Be Taken A License Amendment Request will be submitted to the NRC to revise the RBS licensing basis.
The licensing basis will be revised in accordance with Reg Guide 1.27 to credit an alternate makeup source to the SBCT and reduce SBCT inventory requirements from 30 days to approximately 20 days.
- 4) Date When Full Compliance Will Be Achieved Compliance with Compensatory Measures was achieved on June 1, 2023, when the Compensatory Measures described in section 2 above were implemented. Full compliance with no Compensatory Measures will be achieved when the NRG-approved License Amendment is implemented. The License Amendment is scheduled to be submitted to the NRC by September 30, 2024.