Letter Sequence RAI |
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EPID:L-2021-LLA-0015, Unit 2; License Amendment Request - One-Time Change to Support Proactive Upgrade of the Emergency - Cooling Pond Supply Piping (Approved, Closed) |
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Category:E-Mail
MONTHYEARML24227A0072024-08-13013 August 2024 NRR E-mail Capture - LIC-109 Acceptance - ANO 2 - Proposed Alternative for Implementation of Extended Reactor Vessel In-Service Inspection Interval (ANO2-ISI-24-02) - EPID L-2024-LLR-0048 ML24218A0652024-08-0202 August 2024 NRR E-mail Capture - LIC-109 Acceptance Review - Arkansas Nuclear One, Unit 1 - License Amendment Request - Request for Review and Approval Changes to SAR and to a Confirmatory Order - Pzr Htr Emergency Power Supply - EPID L-2024-LLA-0092 ML24180A0022024-06-26026 June 2024 NRR E-mail Capture - LIC-109 Acceptance - ANO 1 and 2 - Proposed Alternatives for Examinations of SG Pressure Retaining Welds and Full Penetrations Nozzles - EPID L-2024-LLR-0038 ML24117A0262024-04-26026 April 2024 NRR E-mail Capture - ANO Unit 2 - Acceptance of Requested Licensing Action License Amendment Request to Revise Typographical Errors in Technical Specifications ML24088A0082024-03-27027 March 2024 NRR E-mail Capture - ANO-2 -- TSTF-505 Post-Audit Final RAI (L-2023-LLA-0052) ML23269A0232023-09-22022 September 2023 NRR E-mail Capture - Arkansas Nuclear One, Unit 2 - TSTF-505 Audit Questions ML23240A3412023-08-28028 August 2023 NRR E-mail Capture - ANO-2, Grand Gulf, and River Bend - Acceptance Review of LAR Revising TSs to Adopt TSTF-205, Revision of Channel Calibration, Channel Functional Test, and Related Definitions ML23194A1752023-07-13013 July 2023 NRR E-mail Capture - ANO-1 - Acceptance Review of Alternative Request ANO1-ISI-037 ML23187A0432023-07-0303 July 2023 NRR E-mail Capture - Arkansas Nuclear One, Unit 1 - TSTF-505 Audit Agenda ML23166A0132023-06-14014 June 2023 NRR E-mail Capture - Arkansas Nuclear One, Unit 1 - TSTF-505 Audit Questions ML23130A2752023-05-10010 May 2023 NRR E-mail Capture - ANO Unit 2- Acceptance of Requested Licensing Action LAR to Adopt TSTF-505 Revision 2 ML23118A0692023-04-28028 April 2023 NRR E-mail Capture - ANO Unit 1 - Acceptance of Requested Licensing Action LAR to Modify ANO-1 TS 3.3.1, Reactor Protection System Instrumentation (L-2023-LLA-0048) ML23104A1052023-03-10010 March 2023 NRR E-mail Capture - ANO-2 Final RAI Alternative Request for Life-of-Repair of RVCH Pen. 46 ML23072A3672023-03-0909 March 2023 NRR E-mail Capture - Entergy Fleet - Acceptance Review of Quality Assurance Program Manual Reduction in Commitment ML23039A0872023-02-0808 February 2023 NRR E-mail Capture - Arkansas Nuclear One, Unit 2 - Acceptance Review of Relief Request ANO2-RR-23-001, Half-Nozzle Repair of RVCH Penetration 46 (L-2023-LLR-0000) ML23026A1322023-01-26026 January 2023 NRR E-mail Capture - ANO Unit 1 - Acceptance of Requested Licensing Action LAR to Adopt TSTF-505 Revision 2 ML22354A0122022-12-19019 December 2022 NRR E-mail Capture - ANO-1 and ANO-2 - Acceptance Review of Request for Alternative ANO-CISI-002 Alternative Frequency to Containment Unbonded Post-Tensioning System Inservice Inspection (L-2022-LLR-0080) ML22349A0112022-12-14014 December 2022 NRR E-mail Capture - Final RAI Relief Request ANO1-ISI-035 ML22341A1202022-12-0707 December 2022 NRR E-mail Capture - ANO Unit 1 - Acceptance of Requested Licensing Action LAR to to Remove Technical Specification Condition Allowing Two Reactor Coolant Pump Operation (L-2022-LLA-0161) ML22273A0982022-09-30030 September 2022 NRR E-mail Capture - ANO Units 1 and 2 - Acceptance of Requested Licensing Action Emergency Plan Staffing Requirements ML22265A2012022-09-22022 September 2022 NRR E-mail Capture - ANO-1 - Acceptance Review of Relief Request ANO1-ISI-036 ML22188A1782022-07-0707 July 2022 NRR E-mail Capture - ANO-1 - Acceptance Review of Relief Request ANO1-ISI-035 ML22174A1362022-06-23023 June 2022 NRR E-mail Capture - ANO-2 Final RAI Relief Requests ANO2-ISI-023 Through -028 (EPIDs L-2022-LLR-0022 Through -0027) ML22151A3262022-05-31031 May 2022 August 2022 Emergency Preparedness Exercise Inspection - Request for Information ML22124A2452022-05-0404 May 2022 NRR E-mail Capture - ANO-1 and ANO-2 - Final RAI 2 License Amendment Requests to Implement Provisions of 10 CFR 50.69 (L-2021-LLA-0105/-0106) ML22108A1642022-04-18018 April 2022 NRR E-mail Capture - ANO-1: Final RAI License Amendment Request Concerning TS Changes Due to Revised Dose Calculations (L-2021-LLA-0181) ML22081A3902022-03-22022 March 2022 NRR E-mail Capture - ANO-2 - Acceptance Review of Relief Requests ANO2-ISI-023, -024, -025, -026, -027, and -028 (Epids: L-2022-LLR-022, -023, -024, -025, -026, and -027) ML22034A5482022-02-0303 February 2022 NRR E-mail Capture - Final RAI License Amendment Requests to Implement Provisions of 10 CFR 50.69 (L-2021-LLA-0105/-0106) ML22020A0822022-01-19019 January 2022 NRR E-mail Capture - ANO-1 and 2 - Final RAI 2 License Amendment Requests to Allow the ECP to Remain Operable on a One-Time Basis for Up to 65 Days to Perform Piping Upgrade (L-2021-LLA-0015) ML22020A0742022-01-13013 January 2022 NRR E-mail Capture - ANO Unit 2 - Acceptance of Requested Licensing Action Alternative ANO2-PT-003 ML21314A1212021-11-0909 November 2021 Verbal Authorization of Relief Request ANO2-RR-21-002 ML21312A4792021-11-0505 November 2021 Email: NRC Staff Preliminary Questions Regarding X Energy LLC Xe-100 Topical Report: Risk-Informed Performance-Based Licensing Basis Development ML21312A0382021-11-0505 November 2021 NRR E-mail Capture - ANO-2 RAI Relief Request ANO2-RR-21-002 ML21308A5602021-11-0404 November 2021 NRR E-mail Capture - Arkansas Nuclear One, Units 1 and 2, Grand Gulf, River Bend, and Waterford, Unit 3 - Acceptance Review of LAR to Adopt TSTF-554, Revise Reactor Coolant Leakage Requirements ML21292A0112021-10-18018 October 2021 NRR E-mail Capture - ANO, 1 and 2, Grand Gulf, River Bend, Waterford, 3 - Acceptance Review of LAR to Adopt TSTF-541, Add Exceptions to Surveillance Requirements for Valves and Dampers Locked in the Actuated Position ML21287A1692021-10-13013 October 2021 Record of 10-13-21 Verbal Authorization of ANO2-R&R-012 (L-2021-LLR-0082) ML21298A1562021-10-11011 October 2021 NRR E-mail Capture - ANO-2 Final RAI Relief Request ANO2-R&R-012 Concerning Rv Closure Head Penetration 46 ML21273A0672021-09-29029 September 2021 NRR E-mail Capture - ANO-2 Final RAI 2 License Amendment Request to Adopt a Safety Function Determination Program ML21238A3742021-08-23023 August 2021 RFI Email - Cyber PI&R Inspection (ANO) ML21252A0052021-08-20020 August 2021 NRR E-mail Capture - ANO-1 and 2 Final RAI License Amendment Request to Allow the ECP to Remain Operable on a One-Time Basis for Up to 65 Days to Perform Piping Upgrade (L-2021-LLA-0015) ML21217A3302021-08-0505 August 2021 (ANO) Problem Identification and Resolution (PIR) Request for Information Combined ML21202A1662021-07-20020 July 2021 NRR E-mail Capture - ANO Unit 2 - Acceptance of Requested Licensing Action Alternative ANO2-PT-003 ML21201A0062021-07-19019 July 2021 NRR E-mail Capture - Arkansas Nuclear One, Units 1 and 2, and Waterford, Unit 3 - Acceptance Review of LAR to Adopt TSTF-577, Revised Frequencies for Steam Generator Tube Inspections ML21197A0372021-07-16016 July 2021 NRR E-mail Capture - ANO-1 and 2 - Final RAI Final Response to GL 2004-02 ML21179A0042021-06-25025 June 2021 NRR E-mail Capture - ANO Unit 1 - Acceptance of Requested Licensing Action License Amendment Request to Adopt 10 CFR 50.69 ML21179A0052021-06-25025 June 2021 NRR E-mail Capture - ANO Unit 2 - Acceptance of Requested Licensing Action License Amendment Request to Adopt 10 CFR 50.69 ML21174A0342021-06-22022 June 2021 NRR E-mail Capture - Entergy Fleet (ANO, Ggulf, Rbend, & Waterford) - Acceptance Review for Relief Request to Use a Provision of a Later Edition of the ASME Code, Section XI for Periodic System Pressure Tests Exemptions ML21116A1092021-04-26026 April 2021 NRR E-mail Capture - ANO-1 and ANO-2: Final Supplemental RAI Proposed Alternative to ASME Section XI Requirements for Repair/Replacement of ECP Supply Piping ML21105A0122021-04-0909 April 2021 NRR E-mail Capture - ANO-2 Final RAI License Amendment Request to Adopt a Safety Function Determination Program ML21074A2552021-03-15015 March 2021 NRR E-mail Capture - ANO-1 and ANO-2 - Acceptance of Requested Licensing Action LAR for One-Time Change to Support Upgrade of the ECP Supply Piping 2024-08-02
[Table view] Category:Request for Additional Information (RAI)
MONTHYEARML24143A0632024-05-22022 May 2024 Notification of Inspection (NRC Inspection Report 05000368/2024003) and Request for Information ML24107A0282024-04-17017 April 2024 Notification of Comprehensive Engineering Team Inspection (05000313/2024011 and 05000368/2024011) and Request for Information ML24088A0082024-03-27027 March 2024 NRR E-mail Capture - ANO-2 -- TSTF-505 Post-Audit Final RAI (L-2023-LLA-0052) ML23130A2972023-05-17017 May 2023 Notification of Inspection (NRC Inspection Report 05000313/2023003) and Request for Information ML23104A1052023-03-10010 March 2023 NRR E-mail Capture - ANO-2 Final RAI Alternative Request for Life-of-Repair of RVCH Pen. 46 ML23019A0672023-01-19019 January 2023 Inservice Inspection Request for Information ML22349A0112022-12-14014 December 2022 NRR E-mail Capture - Final RAI Relief Request ANO1-ISI-035 ML22213A1662022-08-0101 August 2022 Information Request, Security IR 2022401 ML22208A0542022-07-26026 July 2022 Request for Information ML22174A1362022-06-23023 June 2022 NRR E-mail Capture - ANO-2 Final RAI Relief Requests ANO2-ISI-023 Through -028 (EPIDs L-2022-LLR-0022 Through -0027) ML22159A3242022-06-0909 June 2022 Notification of NRC Triennial Heat Exchanger/Sink Performance Inspection (05000313/2022003 and 05000368/2022003) and Request for Information ML22151A3262022-05-31031 May 2022 August 2022 Emergency Preparedness Exercise Inspection - Request for Information ML22124A2452022-05-0404 May 2022 NRR E-mail Capture - ANO-1 and ANO-2 - Final RAI 2 License Amendment Requests to Implement Provisions of 10 CFR 50.69 (L-2021-LLA-0105/-0106) ML22122A2952022-05-0404 May 2022 Notification of Inspection NRC Inspection Report 05000368/2022003 and Request for Information ML22108A1642022-04-18018 April 2022 NRR E-mail Capture - ANO-1: Final RAI License Amendment Request Concerning TS Changes Due to Revised Dose Calculations (L-2021-LLA-0181) ML22034A5482022-02-0303 February 2022 NRR E-mail Capture - Final RAI License Amendment Requests to Implement Provisions of 10 CFR 50.69 (L-2021-LLA-0105/-0106) ML22020A0822022-01-19019 January 2022 NRR E-mail Capture - ANO-1 and 2 - Final RAI 2 License Amendment Requests to Allow the ECP to Remain Operable on a One-Time Basis for Up to 65 Days to Perform Piping Upgrade (L-2021-LLA-0015) ML21312A0382021-11-0505 November 2021 NRR E-mail Capture - ANO-2 RAI Relief Request ANO2-RR-21-002 ML21286A7132021-10-15015 October 2021 ANO2022010 Tfp RFI Stg, Arkansas Nuclear One, Units 1 and 2 - Notification of an NRC Fire Protection Baseline Inspection (NRC Inspection Report 05000313/2022010 and 05000368/2022010) and Request for Information ML21273A0672021-09-29029 September 2021 NRR E-mail Capture - ANO-2 Final RAI 2 License Amendment Request to Adopt a Safety Function Determination Program ML21236A3222021-09-19019 September 2021 Request for Information ML21252A0052021-08-20020 August 2021 NRR E-mail Capture - ANO-1 and 2 Final RAI License Amendment Request to Allow the ECP to Remain Operable on a One-Time Basis for Up to 65 Days to Perform Piping Upgrade (L-2021-LLA-0015) ML21217A3302021-08-0505 August 2021 (ANO) Problem Identification and Resolution (PIR) Request for Information Combined ML21204A0842021-07-28028 July 2021 ANO Phase 4 2021013 RFI Gap ML21197A0372021-07-16016 July 2021 NRR E-mail Capture - ANO-1 and 2 - Final RAI Final Response to GL 2004-02 0CAN042105, Supplement to Response to Request for Additional Information Reduction of Commitment to the Entergy Operation'S Quality Assurance Program Manual Description2021-04-30030 April 2021 Supplement to Response to Request for Additional Information Reduction of Commitment to the Entergy Operation'S Quality Assurance Program Manual Description ML21116A1092021-04-26026 April 2021 NRR E-mail Capture - ANO-1 and ANO-2: Final Supplemental RAI Proposed Alternative to ASME Section XI Requirements for Repair/Replacement of ECP Supply Piping ML21105A0122021-04-0909 April 2021 NRR E-mail Capture - ANO-2 Final RAI License Amendment Request to Adopt a Safety Function Determination Program ML21071A2172021-03-10010 March 2021 NRR E-mail Capture - ANO-1 and ANO-2 - Final RAI Proposed Change to Quality Assurance Program Manual ML21026A2682021-01-26026 January 2021 Request for Information ML21022A0842021-01-22022 January 2021 Request for Additional Information - Proposed Alternative to ASME Section XI Requirements for Repair/Replacement of Emergency Cooling Pond Supply Piping - Arkansas Nuclear One,Units 1 and 2 -Entergy Operations, Inc. NON-PROPRIETARY Redacted ML21019A5142021-01-14014 January 2021 March 2021 Emergency Preparedness Exercise Inspection - Request for Information ML20324A6412020-11-19019 November 2020 NRR E-mail Capture - ANO-1 - Final RAI Relief Request ANO1-ISI-034 ML20316A0102020-11-0202 November 2020 NRR E-mail Capture - ANO-1 and ANO-2 - Final RAI Concerning Relief Request EN-20-RR-01 ML20262H0752020-09-17017 September 2020 NRR E-mail Capture - ANO-2 Final RAI 2 License Amendment Request Concerning Proposed Technical Specification Additions, Deletions, and Relocations ML20260H4762020-09-0909 September 2020 NRR E-mail Capture - ANO-1 Final RAI License Amendment Request to Revise Lov Relay Allowable Values ML20154K7622020-06-0101 June 2020 NRR E-mail Capture - ANO-2 Final RAI License Amendment Request Concerning Proposed Technical Specification Additions, Deletions, and Relocations ML20119A0982020-04-28028 April 2020 Notification of Inspection (NRC Inspection Report 05000368/2020003 and Request for Information ML20106E8522020-04-13013 April 2020 Information Request, NRC Inspection Report 05000313/2020410 and 05000368/2020410 ML20065H7992020-03-0606 March 2020 Supplemental Information Needed for Acceptance of Requested Licensing Action License Amendment Request to Revise Loss of Voltage Relay Allowable Values ML20055E9092020-02-24024 February 2020 NRR E-mail Capture - ANO-2 Final RAI License Amendment Request to Revise Control Element Assembly Drop Time ML20036D3092020-02-0505 February 2020 NRR E-mail Capture - ANO-2 - Final RAI Alternative Request VRR-ANO2-2019-1 ML20013C7472020-01-10010 January 2020 NRR E-mail Capture - ANO-1 and 2 -- Final RAI #2 LAR to Incorporate Tornado Missile Risk Evaluator (TMRE) Into Licensing Basis ML19316A0242019-11-0707 November 2019 NRR E-mail Capture - ANO-1 - - Final RAI Concerning Relief Request ANO1-ISI-033 (L-2019-LLR-0100) ML19280A0402019-10-0707 October 2019 NRR E-mail Capture - ANO-1 and 2 - Final RAI #1 License Amendment Request to Incorporate Tornado Missile Risk Evaluator (TMRE) Into Licensing Basis ML19339F5902019-09-23023 September 2019 Request for Information: Arkansas Nuclear One, IR 05000313/2019-004 Occupational Radiation Safety Inspection ML19281E0032019-08-0505 August 2019 ANO 2019 PIR Request for Information ML19203A0122019-07-16016 July 2019 Request for Information - Inservice Inspection Activities (NRC Inspection Report 05000313/2019004) ML19106A4322019-04-16016 April 2019 NRR E-mail Capture - ANO-2 Final RAI Re LAR to Add TS Actions to Address Inoperability of the Containment Building Sump ML19058A8332019-02-27027 February 2019 NRR E-mail Capture - ANO-1 - Final RAI Relief Request ANO1-ISI-032 2024-05-22
[Table view] |
Text
From: Wengert, Thomas Sent: Wednesday, January 19, 2022 3:15 PM To: Keele Jr, Riley D Cc: Clark, Robert; REID, MARK; Dixon-Herrity, Jennifer
Subject:
ANO-1 and 2 -- Final RAI #2 RE: License Amendment Requests to Allow the ECP to Remain Operable On a One-Time Basis for Up to 65 days to Perform Piping Upgrade (L-2021-LLA-0015)
Attachments: Final RAI #2 Regarding One-time ANO ECP TS Change.pdf On December 16, 2021, the U.S. Nuclear Regulatory Commission (NRC) staff sent Entergy Operations, Inc. (the licensee) the draft Request for Additional Information (RAI) identified below. This RAI relates to proposed technical specification changes that would allow the emergency cooling pond (ECP) to remain operable on a one-time basis for up to 65 days to perform proactive upgrades to the ECP supply piping at Arkansas Nuclear One, Units 1 and 2.
The NRC staff held a conference call with the licensee staff on January 19, 2022, to clarify this request. During the call, the NRC staff agreed to make some minor wording changes to RAI SCPB-1 to further clarify the request. At the conclusion of the call, the licensee agreed to provide a response to this RAI within 30 days of this correspondence. A publicly available version of this revised, final RAI (attached) will be placed in the NRCs Agencywide Documents Access and Management System (ADAMS).
From: Wengert, Thomas Sent: Thursday, December 16, 2021 1:58 PM To: Keele Jr, Riley D <rkeele@entergy.com>
Cc: Clark, Robert <RCLARK@entergy.com>; REID, MARK <mreid1@entergy.com>; Dixon-Herrity, Jennifer
<Jennifer.Dixon-Herrity@nrc.gov>
Subject:
ANO-1 and 2 Draft RAI #2 RE: License Amendment Requests to Allow the ECP to Remain Operable On a One-Time Basis for Up to 65 days to Perform Piping Upgrade (L-2021-LLA-0015)
By letter dated February 8, 2021 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML21039A756), as supplemented by letter dated September 23, 2021 (ADAMS Accession No. ML21266A413), Entergy Operations, Inc. (Entergy) requested license amendments for Arkansas Nuclear One, Unit 1 and Unit 2 (ANO-1 and ANO-2) concerning Emergency Cooling Pond (ECP) Technical Specifications (TSs) ANO-1 TS 3.7.8 and ANO-2 TS 3.7.4.1. The proposed amendments would allow the ECP to remain operable on a one-time basis for up to 65 days to perform proactive upgrades to the ECP supply piping. In its letter dated February 8, 2021, the licensee stated that this change would allow Entergy the time to perform upgrades on piping from the ECP to the Service Water System intake bays prior to a spring outage for each unit.
The U.S. Nuclear Regulatory Commission (NRC) staff has reviewed the submittals and has determined that additional information is required for the staff to complete its review of this application. This request for additional information (RAI) is identified as draft at this time to confirm your understanding of the information that the NRC staff needs to complete the evaluation. If the request for information is understood, please respond to this RAI within 30 days of the date of this request.
Please contact me if you would like to set up a conference call with the NRC staff to clarify this request for information.
Tom Wengert Project Manager - Arkansas Nuclear One NRR/DORL/LPL4 (301) 415-4037
Hearing Identifier: NRR_DRMA Email Number: 1496 Mail Envelope Properties (DM6PR09MB5447DE75D601BB584FF3E74E8F599)
Subject:
ANO-1 and 2 -- Final RAI #2 RE: License Amendment Requests to Allow the ECP to Remain Operable On a One-Time Basis for Up to 65 days to Perform Piping Upgrade (L-2021-LLA-0015)
Sent Date: 1/19/2022 3:14:44 PM Received Date: 1/19/2022 3:14:00 PM From: Wengert, Thomas Created By: Thomas.Wengert@nrc.gov Recipients:
"Clark, Robert" <RCLARK@entergy.com>
Tracking Status: None "REID, MARK" <mreid1@entergy.com>
Tracking Status: None "Dixon-Herrity, Jennifer" <Jennifer.Dixon-Herrity@nrc.gov>
Tracking Status: None "Keele Jr, Riley D" <rkeele@entergy.com>
Tracking Status: None Post Office: DM6PR09MB5447.namprd09.prod.outlook.com Files Size Date & Time MESSAGE 2935 1/19/2022 3:14:00 PM Final RAI #2 Regarding One-time ANO ECP TS Change.pdf 164064 Options Priority: Normal Return Notification: No Reply Requested: No Sensitivity: Normal Expiration Date:
REQUEST FOR ADDITIONAL INFORMATION CONCERNING PROPOSED ONE-TIME LICENSE AMENDMENTS TO ALLOW THE EMERGENCY COOLING POND (ECP) TO BE OPERABLE FOR UP TO 65 DAYS TO PERFORM PIPING UPGRADES TO ECP SUPPLY PIPING ARKANSAS NUCLEAR ONE, UNITS 1 AND 2 DOCKET NOS. 50-313 AND 50-368 By letter dated February 8, 2021 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML21039A756), as supplemented by letter dated September 23, 2021 (ADAMS Accession No. ML21266A413), Entergy Operations, Inc. (Entergy, the licensee) requested license amendments for Arkansas Nuclear One, Unit 1 and Unit 2 (ANO-1 and ANO-
- 2) concerning Emergency Cooling Pond (ECP) Technical Specifications (TSs) ANO-1 TS 3.7.8 and ANO-2 TS 3.7.4.1. The proposed amendments would allow the ECP to remain operable on a one-time basis for up to 65 days to perform proactive upgrades to the ECP supply piping. In its letter dated February 8, 2021, the licensee stated that this change would allow Entergy the time to perform upgrades on piping from the ECP to the Service Water System (SWS) intake bays prior to a spring outage for each unit. The U.S. Nuclear Regulatory Commission (NRC) staff has reviewed the submittals and has determined that additional information is needed to complete its review, as described below.
Regulatory Basis Title 10 of the Code of Federal Regulations (10 CFR) 50.36, Technical Specifications, requires, in part, that the operating license of a nuclear production facility include TSs. The regulations in 10 CFR 50.36(c)(2) require, in part, that the TSs include limiting conditions for operation (LCOs), which are the lowest functional capability or performance levels of equipment required for safe operation of the facility. When an LCO for a nuclear reactor is not met, the licensee shall shut down the reactor or follow any remedial action permitted by the TSs, until the condition can be met.
ANO-1 and ANO-2 are not licensed to 10 CFR 50, Appendix A, General Design Criteria (GDC) for Nuclear Power Plants. Both plants were originally designed to comply with the Proposed General Design Criteria for Nuclear Power Plant Construction Permits, published in July 1967.
The ANO-1 and ANO-2 Safety Analysis Reports provide comparisons with the Atomic Energy Commission GDC published as Appendix A to 10 CFR 50 in 1971.
The following GDCs are applicable:
GDC-5, Shared Structures, Systems, and Components (SCCs) and GDC-44, Cooling Water.
Entergy provided a detailed discussion of GDC-5 and GDC-44 in Section 4.1, Applicable Regulatory Requirements/Criteria in the LAR.
The NRC staff used the following guidance to evaluate the LAR:
NUREG-0800, Standard Review Plan for the Review of Safety Analysis Reports for Nuclear Power Plants: LWR Edition, Chapter 18, Revision 3, Human Factors Engineering, provides 1
the NRC staffs guidance for the review important actions and human performance for applicants.
NUREG-1764, Guidance for the Review of Changes to Human Actions, Revision 1, issued September 2007 (ADAMS Accession No. ML072640413), is used by the NRC staff to risk-inform the review of changes to manual actions.
Regulatory Guide 1.174, An Approach to Using Probabilistic Risk Assessment in Risk-Informed Decisions on Plant-Specific Changes to the Licensing Basis, Revision 3, issued January 2018 (ADAMS Accession No. ML17317A256), describes an approach that is acceptable to the NRC staff for developing risk-informed applications for a licensing basis change that considers engineering issues and applies risk insights.
Request for Additional Information (RAI) 1 RAI STSB-8 In RAI STSB-4.b of the initial request for additional information, the NRC staff requested the licensees response concerning the following issue:
Please specify the delay time or explain the term delay.
In its letter dated September 23, 2021, the licensee stated, in part:
Entergy response considers inability to meet one of the regulatory commitments as a missed surveillance and will invoke either ANO-1 Technical Specifications SR 3.0.3 or ANO-2 Technical Specification SR 4.0.3 guidance.
The NRC staff notes that because the subject compensatory actions are not TS surveillances, TS SR 3.0.3/4.0.3 cannot be invoked for such actions. On failure to meet the compensatory actions, appropriate ECP-related TS LCO Conditions (i.e., LCO 3.7.8 for ANO-1 and LCO 3.7.4.1 for ANO-2) must be entered and Action(s) taken accordingly.
Please confirm your understanding and revise the previous response to RAI STSB-4.b, as necessary.
1 The RAI numbering scheme is based on a continuation of the RAI numbering shown in the licensees letter dated September 23, 2021.
2
RAI STSB-9 The licensees proposed TS change modifies ANO-1 TS 3.7.8 and ANO-2 TS 3.7.4.1 with the addition of the following NOTE:
LCO The ECP shall be OPERABLE.
NOTE-------------------------------------------
The ECP may be considered OPERABLE on a one-time basis for up to 65 days during upgrade of the ECP supply piping to the SWS intake bays provided:
- a. A loss of Lake Dardanelle event is not in progress, and
- b. A temporary pumping system is capable of supplying the SWS from the ECP. The temporary pumping system may be unavailable for testing or necessary maintenance provided its availability is restored within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />, and
- c. The regulatory commitments described in the ANO License Amendment Request (LAR) correspondence letter 0CAN022102 Enclosure Attachment 4 are implemented.
Regarding the proposed Note c above, the NRC staff notes that regulatory commitments can be revised without NRC prior approval and, therefore, may not be relied upon by the staff as a basis for approval.
Consider alternative language for implementing compensatory measures as obligations under this LCO Note.
RAI SCPB-1 In Section 3.2, Justification, of the LAR, the licensee stated that the temporary ECP supply system is a commercial-grade, nonsafety-related system being installed as a compensatory measure, and that the system will consist of high density polyethylene (HDPE) and carbon steel suction and discharge piping. The licensee also stated that the temporary piping and equipment will be restrained to limit movement and stresses due to wind, seismic, and thermal expansion within ASME Code or Plastic Pipe Institute limits. However, the above statements do not identify the specific piping standards that will be used by the licensee in the design of the temporary system.
Please identify the specific standards for the HDPE piping, carbon steel piping, and the interconnection that will be applied in the design of the temporary ECP supply system.
3
RAI EMIB-3 In the response to RAI EMIB-1 in the licensees letter dated September 23, 2021, concerning how the minimum system flow requirements would be determined and why they would be sufficient to support the intended safety function of the ECP temporary pumping system, the licensee provided the following response:
In a conference call on August 18, 2021, the NRC Staff clarified that they were requesting information on how the full flow test will be performed. To perform the test, ANO will install the temporary pumping system into two SW pump bays and test the temporary system while the SW pumps are running, close the Lake Sluice gates and start the temporary pump. The test will verify the system minimum flow using flow meters, validate level control requirements are achieved in the SW Bays, and the system functions properly.
However, the intent of RAI EMIB-1 is to understand the licensees basis for establishing that the pump design characteristics (e.g., capacity/flow rate) will meet the system functional requirements, not the performance of the pump testing.
Please describe how the minimum system flow requirements of the ECP temporary pumping system will be determined and why they will be sufficient to support the intended safety function.
4