ML20247R740

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Fulfills Commitment by Providing Results of Pulled Tube Analyses Including Laboratory Leak & Burst Testing by 980601
ML20247R740
Person / Time
Site: Crane 
Issue date: 05/19/1998
From: Langenbach J
GENERAL PUBLIC UTILITIES CORP.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
1920-98-20256, NUDOCS 9805290207
Download: ML20247R740 (4)


Text

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Tel 717-944-7621 May 19,1998 1920-98-20256 U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555 Gentlemen:

Subject:

Three Mile Island Nuclear Station, Unit 1 (TMI-1)

Docket No. 50-289 Operating License No. DPR-50 Results from Cycle 12 Refueling (12R) Outage Pulled Tube Examinations

References:

1. GPU Nuclear Letter to NRC dated January 12,1998 (6L20-98-20004)," Cycle 12 Refueling (12R) Outage Once Through Steam Generator (OTSG) Tube Inspection Report with ASME NIS Data Reports for Inservice Inspections (ISI)."
2. ABB Combustion Engineering Nuclear Operations Report #060-PENG-TR-107, Rev. 00, May 1998, " Comparison of Field and Laboratory ECT Results, Helium Leak Tests and Observations of Three Mile Island Unit 1 Steam Generator Tube Sections."
3. ABB Combustion Engineering Nuclear Operations Report #060-PENG-TR-117, Rev. 00, May 1998, " Leak and Burst Testing of Three Mile Island Unit 1 Steam Generator Tube Sections."

I In our letter which transmitted the results of TMI-Isteam generator inspections performed during the Cycle 12 Refueling (12R) Outage (Reference 1), GPU Nuclear committed to provide the results ~

of the pulled tube analyses including laboratory leak and burst testing by June 1,1998. The purpose of this letter is to fulfill that commitment.

. In October 1997 during the 12R Outage, one tube was pulled from each of TMI-l's two Once Through Steam Generators:

1.

Tube A52-34 was chosen to examine the inside diameter (ID)- initiated volumetric eddy

~ current indications which were believed to be remnants ofID degradation (currently inactive) that occurred as a result of a 1981 sodium thiosulfate intrusion event.

9905290207 990519 l-PDR ADOCK 05000289 Y

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  • 1920-98-20256 Page 2 of 2 II. Tube B91-55 was the only tube out of the 100% bobbin coil tu'oe examination scope that was.found to contain axial indications typical of " groove" IGA, a potentially active mechanism at B&W plants.

Table 1 provides a summary of the pulled tube leak and burst test results. Sections were selected for helium leak tests, water leak tests, and burst tests to ensure that the eddy current indications most likely to burst or leak would be tested.

Helium leak tests were conducted on five tubing sections (three from tube A52-34, two from tube B91-55). One tube section (Tube A52-34, Section 18) indicated a small amount ofIcakage during the preliminary helium test, but did not leak during subsequent tests with water.

Water leak tests were performed on five tube sections: first at 1500 psig (normal operating delta p),

then at 2900 psig (MSLB delta p), and again at 4400 psig (3 times normal operating delta p). No leakage was detected during any of these tests up to the highest test pressure,4400 psig. These tests were conducted with and without an additional axial load applied to obtain the calculated Main Steam Line Break (MSLB) axial tensile load of 1402 lb. at each test pressure'. Additional axial load was not applied during the leak test of Section 18 of tube B91-55, because the indications contained in this section were of axial orientation such that the applied tensile axial load would tend to " tighten" the indication and decrease any leakage. Had any leakage been detected during the test of this section, it would have been possible to apply the additional axial tensile load and evaluate the change in leak rate.

Four tubing sections were burst tested. It was not necessary to apply additional load to achieve the MSLB axial tensile load for the burst tests, because the "end cap load" at the burst pressures exceeds the calculated 1402 lb. MSLB axial load by a significant margin. The burst pressures of all of the sections tested were above 10,000 psig. Burst testing was not performed on Section 18 of the B91-55 tube so that the OD indication surface could be preserved for further laboratory work, because this was the only tube found during the 12R Outage examinations with indications typical of" groove" IGA. The structural and leakage integrity of this inbe section was established by the j

water leak tests at 4400 psig.

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t Water leak tests and burst tests were performed in accordance with a 10CFR50 Appendix B QA program, at room temperature, with additional pressure added for water leak tests to account for the expected difference in material properties between room temperature and normal operating temperatures. The laboratory reports on leak and burst testing have been completed (References 2 and 3) and are available at the TMl site for NRC review.

As stated above, Tube B91-55 was the only tube found during the TMI-l 12R Outage with axial OD IGA indications typical of" groove" 1GA in the upper span. This tube was pulled for the laboratory examinations and was not subjected to in situ pressure testing during the outage. As a result, GPU Nuclear was unable to fully complete its condition monitoring of the TMI-l generators until the leak testing of this tube was completed. Section 18 of this pulled tube contained the most significant of the axial OD IGA indications on the basis of both field and lab eddy current examinations using several different probes. This tube section was subjected to the laboratory leak

' 1402 lbs. is the B&W Owners Group gerieric calculated axial tube tensile load for a MSLB applicable to the OTSG plants (other than Oconee).

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  • 1920-98-20256 Page 3 of 3 testing, with no leakage detected at 4400 psig, which provides confirmation that the tube would have maintained its, structural and leakage integrity during a hypothetical MSLB accident during TMI-l Cycle 11, the operating cycle prior to the 12R outage. With the results from the 100% eddy current examination of the tubes in both OTSGs, in-situ pressure testing, other work described in Reference 1, and the leak and burst testing described above, GPU Nuclear concludes that the TMI-l OTSGs continue to demonstrate adequate tube integrity for the present operating cycle, Cycle 12.

l In addition to leak and burst testing, GPU Nuclear has contracted with a laboratory to provide metallurgical analyses including fractographic, metallographic and chemical analyses. GPU Nuclear will submit the results of these analyses when complete. The final reports from the contractor are expected later this year and prior to GPU Nuclear's submittal of Technical l

Specification Change Requests that will be required to support the TMI-l Cycle 13 Refueling (13R)

OTSG tube examinations.

Sincerely, James W. Langenbach Vice President and Director, TMI MRK Attachment cc:

Administrator, NRC Region I TMI Senior NRC Resident Inspector TMI-l Senior NRC Project Manager File #97087 l

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1920-98-20256 Attathmenf Page 1 of1 Table 1 -Summary of TMI-I 12R Outage Pulled Tube Laboratory Leak Tests Leak Test Results Burst Pulled Tube Pressure l

ECT Indications Within Section*

Section Helium Water * *

(P5'g) 1 l

Tube A52-34, ID volumetric indications with:

NT NLD,t i1,200 Section 12 4 indications detected by field or lab MRPC and not detected by field bobbin l

Tube A52-34, ID volumetric indications including those indications with:

Some NLD,t 10,950 Section 18 Deepest field bobbin depth (estimated 50% TW),

leakage Largest field MRPC voltage, detected Largest lab MRPC indication area, Largest lab indication area not detected by field bobbin 7

Tube A52-34, ID volumetric indications including those indications with:

NLD NLD,t 10,h00 Section 21 Largest field bobbin voltage, Largest field MRPC indication area, Largest field MRPC circumferential length Tube A52-34, ID volumetric indications including those indications with:

NLD NT NT Section 22 Highest lab and field bobbin phase angle Tube A52-34, ID volumetric indications including those indications with:

NT NLD, t 10,800 Section 23 Field bobbin depth (estimated 17% TW),

Largest area field indication not detected by bobbin, Highest field MRPC axial length Tube B91-55, OD axial indications including that indication with:

NLD NT NT Section 17 Lowest field MRPC phase angle Tube B91-55, OD axial indications including those indications with:

NLD NLD NT Section 18 Largest field and lab bobbin vohage, Lowest field and lab bobbin phase angle, Highest field and lab MRPC length, Highest field and lab MRPC voltage, Lowest recorded field MRPC phase angle S3mbols and Acronyms Note that in Table I cddy current indications are compared with other indications in the same pulled tube.

(For example," highest lab MRPC voltage" means that the indication had the highest lab MRPC voltage of the indications in that pulled tube.)

" Water Leak Tests were performed at 1500,2900, and 4400 psig.

t Leak tests were performed both with and without additional axial load applied to achieve the calculated MSLB axial tensile load.

ID

- Inside Diameter NT

- Not Tested NLD - No Leakage Detected OD

- Outside Diameter MRPC - Motorized Rotating Pancake Coil TW

- Through Wall