ML20247G215

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Insp Rept 50-344/89-01 on 890101-0211.Violations Noted.Major Areas Insepcted:Operational Safety Verification,Maint, Surveillance,Event Followup & Followup on Previously Identified Items
ML20247G215
Person / Time
Site: Trojan File:Portland General Electric icon.png
Issue date: 03/13/1989
From: Rebecca Barr, Mendonca M, Suh G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML20247G201 List:
References
50-344-89-01, 50-344-89-1, NUDOCS 8904040162
Download: ML20247G215 (12)


See also: IR 05000344/1989001

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U. S. NUCLEAR REGULATORY COMMISSION

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REGION V

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Report No. 50-344/89-01

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Docket No. 50-344

License No. NPF-1

Licensee:

Portland General Electric Company

-121 S. W. Salmon' Street

Portland, Oregon 97204

Facility Name: Trojan Nuclear Plant

Inspection at: Rainier, Oregon

Inspection conducted: January 1 - February 11, 1989

Inspectors:

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R. C. Barr

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Senior Resident Inspector

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G. Y. Suh

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Resident Inspector

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Approved By:

M. M. Mendonca, Chief

Date Signed

Reactor ProjectsSection I

Sumary:

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Inspection on January 1 - February 11, 1989 (Report 50-344/89-01)

Areas Inspected: Routine inspection of operational safety verification,

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-maintenance, surveillance, event follow-up, and follow-up on previously

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' identified items.

Inspection procedures 30702, 30703, 35502, 61726, 62703,

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<71707, 90712, 92700, 92701, 92702 and 93702 were used as guidance during the

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conduct of the inspection.

Results:

Paragraph 5 discusses instances of procedural non-compliance during

the performance of routine channel functional testing. Continued management ~

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attention appears to be warranted, particularly with instrument and control

technicians.

Paragraph 5 discusses the performance of an inadequate quality control-

observation of work activities. Recent inspection findings'and a-previously

identified violation in this area appear to indicate the need for improvements

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in quality control effectiveness.

8904040162 890315

PDR

ADOCK 05000344

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PDC

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Paragraph 7 discusses the failure to provide accurate information in a

Licensee' Event Report, and a missed surveillance that resulted from the

failure to comply with procedures and having procedures inappropriate for the

circumstance.

Paragraphs 6 and 7 relate the result of operatir.g with inter-office memorandum

vice changing operating procedures.

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DETAILS

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1.

Persons Contacted

  • D.

W. Cockfield, Vice President, Nuclear

  • C. A. Olmstead, Plant General Manager

L. W. Erickson, Manager, Nuclear Quality Assurance

  • R. P.-Schmitt, Manager, Operations and Maintenance

D. W. Swan,' Manager, Technical Services

M. J. Singh, Manager, Plant Modifications

J. D. Reid, Manager, Plant Services

  • J. W. Lentsch, Manager, Personnel Protection
  • J. M. Anderson, Manager, Material Services
  • R. E. Susee, Manager, Planning and Scheduling

D. F. Levin, Supervisor, Plant Modifications

E. A. Curtis, Procurement Supervisor

  • P. A. Morton, Branch Manager, Plant Systems Engineering

R. L. Russell, Operations Supervisor

R. H. Budzeck, Assistant Operations Supervisor

D. L. Bennett, Maintenance Supervisor

R. A. Reinart, Instrument and Control Supervisor

T. O. Meek, Radiation Protection Supervisor

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W. Ritschard, Security Supervisor

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C. H. Brown, Operations Branch Manager, Quality Assurance

  • D. L. Nordstrom, Nuclear Engineer, Nuclear Safety and Regulation

The inspectors. also interviewed and talked with other licensee employees

during the course of the inspection.

These included shift supervisors,

reactor and auxi'liary operators, maintenance personnel, plant technicians

and engineers, and quality assurance personnel.

  • Denotes those attending the exit interview.

2.

Plant Status

The Trojan facility operated at 100% power throughout this reporting

period.

The main condenser experienced a minor intermittent circulating

water leak throughout the reporting period; however, the leakage was

within the cleanup capacity of the condensate demineralizers and did not

significantly impact plant operation.

On February 1, 1989, after

approximately two weeks of intermittent alarming, the

"C" Reactor Coolant

Pump (RCP) lower bearing oil reservoir high level alarm " locked in".

The

licensee, as a precautionary measure, has since continuously monitored

the "C" RCP bearing temperatures.

The bearing temperatures are normal.

3.

Operational Safety Verification (71707, 35502)

During this inspection period, the inspectors observed and examined

activities to verify the operational safety of the licensee's facility.

The observations and examinations of those activities were conducted on a

daily, weekly or biweekly basis.

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Daily, the inspectors observed control room activities to verify the

licensee's adherence to limiting conditions for operation as prescribed

in the facility Technical Specifications.

Logs, instrumentation,

recorder traces, and other operational records were examined to obtain

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information on plant conditions, trends, and compliance with regulations.

On occasions when a shift turnover was in progress, the turnover of

information on plant status was observed to determine that' pertinent

information was relayed to the oncoming shift personnel.

Each week the inspectors toured the accessible areas of the facility to

observe the following items:

(a) General plant and equipment conditions.

(b) Maintenance requests and repairs.

(c) Fire hazards and fire fighting equipment.

(d)

Ignition sources and flammable material control.

(e) Cnnduct of activities in accordance with the licensee's

administrative controls and approved procedures.

(f) Interiors of electrical and control panels.

(g) Implementation of the licensee's physical security plan.

(h) Radiation protection controls.

(i) Plant housekeeping and cleanliness.

(j) Radioactive waste systems.

(k) Proper storage of compressed gas bottles.

Weekly, the inspectors examined the licensee's equipment clearance

control with respect to removal of equipment from service to determine

that the licensee complied with technical specification limiting

conditions for operation.

Active clearances were spot-checked to ensure

that their issuance was consistent with plant status and maintenance

evolutions.

Logs of jumpers, bypasses, caution and test tags were

examined by the inspectors.

Each week the inspectors conversed with operators in the control room,

and with other plant personnel.

The discussions centered on pertinent

topics relating to general plant conditions, procedures, security,

training and other topics related to in progress work activities.

The inspectors examined the licensee's nonconformance reports (NCRs) to

confirm that deficiencies were identified and tracked by the system.

Routine inspections of the licensee's physical security program were

performed in the areas of access control, organization and staffing, and

detection and assessment systems.

The inspectors observed the access

control measures used at the entrance to the protected area, verified the

integrity of portions of the protected area barrier and vital area

barriers, and observed in several instances the implementation of

compensatory measures upon breach of vital area barriers.

Portions of

the isolation zone were verified to be free of obstructions.

Functioning

of central and secondary alarm stations (including the use of CCTV

monitors) was observed.

On a sampling basis, the inspectors verified

that the required minimum number of armed guards and individuals

authorized to direct security activities were on site.

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The inspectors conducted routine inspections of selected activities of.

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the licensee's' radiological protection program.

A sampling of radiation

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work permits (RWP) was-reviewed for completeness and adequacy of

information. . During the course of inspection activities and periodic

tours of plant areas, the. inspectors verified proper use of personnel

monitoring equipment, observed individuals leaving the radiation

controlled area and signing out on appropriate RWP's, and observed the

posting of radiation areas and contaminated areas.

Posted. radiation

levels at locations ~within the fuel and auxiliary buildings were verified

using both NRC and licensee portable survey meters.

The involvement of

health physics supervisors and engineers and their awareness of

significant plant activities was assessed through conversations and

review of RWP sign-in records.

The inspectors verified the operability of selected engineered safety ,

features.

This was done by direct visual verification of the correct

position of valves,. availability of power, cooling water' supply, system

integrity and general condition of. equipment, as applicable.

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No violations or deviations were identified.

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Maintenance (62703)

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he inspectors observed ongoing fuel repair. activities being conducted in-

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the spent fuel pool area.

Eighteen fuel assemblies damaged primarily

from the baffle gap jetting phenomena and removed from the reactor vessel

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after Cycle 4 were being repaired either by transferrin'g fuel rods to new

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fuel assembly skeletons or by replacing damaged fuel rods with stainless

steel rods.

The inspectors observed the transfer of several fuel rods in

the reassembly of fuel assembly F18.

The work was being performed by a

vendor field crew. The inspectors observed continuous radiation

protection coverage as required by radiological work permit RWP 89-26.

The inspectors reviewed the safety evaluation for the conduct of fuel

repair activities.

Observed work in progress was found to be consistent

with the safety evaluation.

In addition, technical specification

requirements with regard to the spent fuel pool ventilation system were

verified to be met.

Applicable work procedures were on hand at the work

site with inspection hold points being observed.

The inspectors

discussed various aspects of the work activities with cognizant

engineers.

The inspectors understood that seventeen of the fuel

assemblies would be used in upcoming Cycle 12 and verified that the

licensee had applied for NRC review and approval of the use of these fuel

assemblies in License Change Application LCA-161.

No violations or deviations were identified.

5.

Surveillance (61726, 92701)

The inspectors observed the performance of channel functional tests for

steam generator level instrumentation.

Communication was observed

between the test personnel and control room operator, including the

establishment of constant communication when protection cabinet doors

were opened and when bistables were tripped.

The inspectors verified

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calibration of test instruments to be current and observed the

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restoration of the instrumentation channels to service.

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performed by two instrumentation and control technicians. A quality

control inspector performed a work observation during the testing of

steam generator level channels 519 and 549.

The channel functional tests were controlled by the following procedures:

Periodic Instrument and Control Test (PICT) 5-1, Revision 9, titled

" Steam Generator Level, Protection Set

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for steam generator water

level channels 529 and 539; PICT-5-2, Revision 12, titled " Steam

Generator Level, Protection Set II," for channels 519 and 549; PICT-5-3,

Revision 10, titled " Steam Generator Level, Protection Set III," for

channels 518, 528, 538, and 548; PICT 5-4, Revision 11, titled " Steam

Generator Level, Protection Set IV," for channels 517, 527, 537, and 547.

The inspectors reviewed the procedures and verified that the operability

of the trip functions associated with the instrumentation channels were

being demonstrated.

Review of a sample of recently completed data sheets

indicated that the surveillance tests were being performed in a timely

manner.

In the testing of trip functions, a simulated signal from a ramp

generator was injected into the instrument channel at the input test

jack.

The setpoints were determined through the use of a comparator

logic tester.

The test procedures required that a simulated signal

initially set at five volts be decreased to one volt with each bistable

action being recorded, and then increased to record each bistable action

on an increasing signal.

Multiple photocells of the comparator logic

tester were ta be connected to lights associated with each bistable which

performed a trip function.

The inspectors observed apparent procedural violations in the performance

of PICT-5-1, PICT-5-2, PICT-5-3, and PICT-5-4, in that the test personnel

ramped the test input down and up as necessary to observe the bistable

actions and used only one photocell which was moved to the bistable light

which was expected to change state for the given test input.

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addition, the photocells were observed to be connected to indicating

lights different than those indicated in the procedures.

The observed

ramping of the test signal was as follows.

The simulated signal was

decreased until the first bistable changed state, then increased until

the associated trip or reset action occurred, then decreased again to the

next value at which a bistable changed state.

At this point, the signal

was again increased until the associated trip or reset action occurred.

These actions continued until each bistable had been tested and the test

input was at one volt.

Discussions with engineering and maintenance

personnel indicated no technical difference between the observed method

and the steps outlined in the procedure.

The above findings constitu'.2

an apparent violation to follow approved procedures (50-344/89-01-01).

Discussions with maintenance supervision and several instrumentation and

control technicians indicated that the observed method of performing the

surveillance testing may be the general practice within the shop.

The

inspectors noted that draft revisions of PICT 5-1, 5-2, 5-3, and 5-4

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(revised by the contractor for the Procedure Upgrade Program) more

closely outlined the observed method for performing the test.

Testing of channels 519 and 549 per PICT-5-2 was observed by a quality

control inspector performing a scheduled quality inspection calibration

observation. Quality Inspection Procedure QIP 15, Revision 0, titled "QI

Observations of I&C Calibration Activities," provided the requirements

for performing and documenting observations. QIP 15 specifies, in part,

that the inspector :ste whether work was performed in accordance with.

approved procedures to assure that plant procedures are being followed.

The inspectors reviewed the completed observation report and discussed

observation activities with the quality control inspector. The failure

to follow approved procedures was not noted by the QC inspector in his

report. The QC inspector stated that he had not recognized the

procedural violations. He stated that he had been called shortly prior

to the performance of PICT-5-2 and was able to only do a cursory review

of the procedure in prepard ion for performing his observation. The

fai.ure to note that work was not perfomed in accordance with approved

procedures is an apparent violation of QIP-15 requirements

(50-344/89-01-02). A contributing factor to this violation appears to be

the fcct that the QC inspector did not have adequate time to prepare for

the test.

Further, the inspectors reviewed completed quality control observation

reports since July 1988 for observations of surveillance testing

performed by instrumentation and control technicians.

There were four

observations on PICT-5-1, PICT-5-2 PICT-5-3, or PICT-5-4. There were

eight other observations. performed for similar surveillance tests which

involved similar procedural steps. None of these observation reports

documented failure to follow approved procedures. The inspectors

discussed initial findings with quality assurance management who stated

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that they were conducting an evaluation in response to the findings.

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Two apparent violations and no deviations were identified.

6.

Event Follow-Up (93702, 92701)

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Control Room Doors Blocked Open-Entry into T.S. 3.0.3

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From approximately 8:40 AM to 9 05 AM, A January 23, 1989, with the

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reactor at 100% power, the control room door s were maintained open while

conducting corrective maintenance per a Maintenance Request (MR 89-0656)

to repair the lower door latch assembly. Tbc control room doors are part

of the control room emergency ventilation system boundary. With respect

to Trojan Technical Specification 3.7.6.1., two independent control room

emergency ventilation systems shall be operable. With the control room

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doors maintained open, both trains of the control room emergency

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ventilation system were technically rendered inoperable. However, it

should be noted, the sealing surface was capable of providing the

boundary i f the door had been shut,

Plant Administrative Procedure (AO)

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3-21, Revision 2, dated July 7, 1987, permitted the work that was

performed by stating in section 4.2, "If any portion of the control room

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emergency ventilation system boundary as defined in 4.1.1 through 4.1.5

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above is breached, the entire control room emergency ventilation system

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may'be rendered inoperable.

If work must take place on the boundary

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during modes 1-4 or during fuel ~ movement,>an' individual must be~available

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at all times at the work site who is capable of immediately plugging the.

' breach if the control room emergency ventilation system is required. .If

the breach cannot be immediately plugged, then depending on thetsize'of,

the breach and operating margin (>1.75 sq. inch is significant) the'

control room emergency ventilation system boundary may be Linoperable,.

placing the plant in a one-hour action statement."

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When the shift supervisor returned to the control room from a' meeting, he'

directed the control room doors be immediately1 shut due'to his recalling

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previous direction provided by a memorandum dated September 27, 1988 from

the Operations Manager to the Shift Supervisors that directed " control

room doors shall not be blocked oper until'this issue is resolved.

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applies in Modes 1-4 and during core alterations." The inspectors noted

that the memorandum was not in the active Night Order book in the control

room.

The inspectors also noted administrative procedure A0-3-21,

Revision 2, " Control Room Emergency Ventilation Boundary" had no,been

changed to reflect tne direction provided by the memorandum.

Further,

operation at 100% power in Mode I with both trains of control room,

emergency ventilation system inoperable constituted entry into Technical Specification 3.0.3. and went unrecognized for approximately twenty

minutes and was not noted in the maintenance work request.

Additionally,

the review of the maintenance request appeared to be superficial in that

i t did not identi fy technical specifications were applicable.

Although this condition was controlled such that there was not a

technical concern, this event provides another example where the practice

of using internal memorandums vice changing procedures resulted in an

unwanted operation.

A revision to A0 3-21 was made on February 21, 1989

to assure acceptable control of the doors.

Additional licensee analysis

showed.that the doors could be opened for transit of materials since

recent design modification added a second set of doors to the control

room boundary.

No violations er deviations were identified.

7.

Follow-Up of Lice 7see Event Reports (90?l2 ,92700)

The following LER's are closed based on in-office review, inspector

verification of the implementation of selected corrective actions and

licensee commitment to perform future corrective actions:

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LER 88-18, Revision 2, (Closed), " Unfiltered In-Leakage in the Control

Room Emergency Ventilation System".

The inspectors reviewed Revision 2

to Licensee Event Report 88-18 and concluded that the report addressed

questions raised in the review of Revision 1, as discussed in Inspection

Report 50-344/88-40.

LER 88-22, Revision 1, (Closed), " Train 'A'

Safety Injection Due to

Spurious Electronic Spike During Plant Heat-uo"

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LER 89-01, Revision 0, (Closed), ' Engineered Safety Features Valve

Actuation Due to an Electrical Shovt Circuit When Incorrect Indicating

Lamp Used"

The following LERs are closed based on inspector follow-up that included

discussions with licensee representatives, detailed event evaluation,

verification of appropriateness and implementation of corrective actions,

and the licensee commitment to perform future corrective actions-

LER 88-49, Revision 0, (0 pen) " Partial Containment Isolations Result

f rom Signal Spike and Operator Error."

This event report describes three

events that resulted in the automatic isolation of the steam generator

blowdown (SGBD) system.

Two of the events were caused by spurious

electronics spikes and the other by operator error.

As follow-up, the

inspectors verified, as was stated in the LER, that no discharge to the

Columbia River was in progress.

Also, the inspectors examined the

licensee's corrective actions including that the setpoints of the process

radiation monitor (PRM 10) had been changed.

The LER committed to changing the setpoints of PRM 10, the steam

generator blowdown sample line radiation monitor alert and high alarm

setpoints, to 2 times background and 25,000 cpm, respectively.

The

inspectors verified that the licensee had performed a 50.59 Safety

Analysis for the setpoints change.

However, two concerns were raised by

the inspector during the verification of the setpoint change.

First, the

procedurc Periodic Operating Test (POT) 26-2, Revision 24, " Radiation

Monitoring System," had not been changed, as had been stated in the LER,

to reflect the change of the setpoints.

This is an apparent violation of

10CFR50.9 (50-344/89-01-03).

Further research identified that on

December 30, 1988, the setpoint change had been performed using the

guidance given in a memorandum from the Plant General Manager to the

Manager Nuclear Safety and Regulation Department; however, sometime

between December 30, 1988 and January 23, 1989, the setpoints had been

returned to the pre-memo values.

Then on January 23, 1989, while

performing POT 26-2, the setpoints were again returned to the memo

desired values without actually deviating the procedure.

Using memoranda

to direct plant operation vice approved procedures was the major

contributing cause of this apparent violation.

Second, the calibration

sticker located on the face of PRM10 indicated the old setpoints for the

alert and high alarms and not the revised setpoints.

The licensee, when notified of the inspector's concerns and the apparent

violation, immediately deviated the procedure to indicate the memo

desired setpoints of 2.0 times background and 25,000 cpm for the alert

and high alarm setpoints, respectively.

Additionally, the licensee

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changed plant procedures to require plant procedures be deviated within

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24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of issuing a memorandum affecting plant operations.

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licensee identified personnel oversight as the reason the procedure

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change had not been made, as stated in the LER.

Finally, the licensee

corrected the calibration sticker on the PRM 10 meter face.

While performing the follow-up, the inspectors also noted the Final

Safety Analysis Report (FSAR) section 10.4.8., Steam Generator Blowdown

System, had not yet been revised to reflect the major design change made

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to-the system during the 1988 Refueling Outage. Although the update of the-

FSAR is not outside the 1 year requirement, there was ample opportunity to

revise the:FSAR.(for example in the November 8, 1988 FSAR amendment) with

the~ design * change. Also, the licensed operator training manual had not yet

been updated; although the training lesson plan had been updated and

operators had been trained on the new system.

LER 88-19, Rev 0 and Rev 1,(Closed), " Surveillance Required by Technical

Specifications Not Performed Following Containment Hydrogen Vent System

Adsorber Replacement."

This event report describes an incident in which a Technical

Specification surveillance was not performed due to a series of errors in

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the control of plant surveillance and work activities.

A maintenance request (MR-0177) was written by the system engineer on

November 24, 1987, to perform sampling of various charcoal adsorber

systems. The charcoal adsorber sampling was. performed by a maintenance

craftsman. On January 14, 1988, the system engineer requested the

Maintenance Engineering Supervisor, via telephone vice formally

annotating the MR, to have the "A" train hydrogen vent adsorber (CS-9A)

sampled. Due to a communication error, the "B" train charcoal was

sampled. Subsequent to sampling CS-9B, the mechanic did not annotate the

MR, as required to do by Administrative Procedure (AO-3-9, Revision 26,-

" Maintenance Requests"), that he had sampled CS-98. Therefore, the

system engineer, who believed the sample wa's from CS-9A, incorrectly and

unknowingly labeled the sample CS-9A.

It should be noted the work

instructions did not require the mechanic to. label the samples.

On February 2,1988, a sample of CS-9A was taken, with the results

requiring CS-9A charcoal adsorber replacement. A new system engineer

amended MR-0177 (that authorized sampling of charcoal adsorbers) to

replace the adsorber in CS-9A.

A0-3-9, " Maintenance Requests", section

I.B., permits amending MR's by stating " Maintenance Requests written for

support activities such as H&V testing and engineering troubleshooting

shall not be used to implement corrective actions unless the work

instructions have been amended to direct the specific action." The

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inspectors consider this a poor practice - even though allowed by

procedures, and indicated that a better practice may be to generate a

new maintenance request.

It should also be noted, there was no requirement for shift supervision

to approve the amended work instructions even though the initial work

scope required shift supervision approval. This also appears to be a

weak work practice.

This practice contributed to the event because the

maintenance craftsman, contrary to AC-3-9 requirements, went to the job

' site without the maintenance request, due to the request being in

routing.

Next, the system engineer used poor communication practices when he

verbally directed the mechanic to replace the charcoal adsorber (CS-9A).

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The mechanic then proceeded to the job site. When at the job site, the

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mechanic violated Plant Safety (PS) Procedure 3-30 that states in section IV. E.,

"It is the responsibility of the person accepting the equipment clearance

to check the equipment and assure himself that the equipment.is satisfactorily

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tagged and the equipment is deenergized and cleared for work before starting

work." Next, the mechanic proceeded.to incorrectly replace the charcoal

adsorber in CS-9B, the operable hydrogen ventilation system, and-thereby

-violated Administrative Order (AO) 3-9, Revision 26, in Section I. item 4.

that states, "the assigned craftsman / technician performs the maintenance

prescribed by the MR work instructions and documents its completion in

the work performed section of the MR." (50-344/89-01-04).

When the mechanic completed the adsorber replacement, he left the job

site and because he did not have the maintenance request he did not

annotate that maintenance had been performed on CS-98. However, the

storeroom material issues / returns form (PGE 2345) recorded that charcoal

had been issued for the replacement CS-9B charcoal adsorber. A careful

review of the documentation would have identified the discrepancy'between

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the MR and the issues receipt form.

A0-3-9, " Maintenance Requests"

states in section II.H. that the Work Group Craft Supervisor / Designee

"make routine visits to the work area during the performance of major

work activities." The work group supervisor did not consider the

charcoal replacement to be a major job and, therefore, did not make a

field observation of the work in progress.

" Major" work activities are

not defined and thereby can lead to inconsistent supervisory involvement

in plant activities. This has been a longstanding NRC concern with PGE

work execution and control.

This event contains numerous procedural violations and poor work

practices. Collectively, the causes of this event represent a

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programmatic breakdown of work practices. The licensee is continuing to

review the circumstances of this event and has agreed to submit a revised

LER. The violations in this section are in areas that had not been

acceptably addressed by the licensee.

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Two apparent violations were identified.

8.

Follow-Up on Open Items and Corrective Actions for Violations (92701,

92702)

Open Item 50-344/88-13-01 (Closed) Inadequate Safety Evaluation for

Opening Feedwater Drain Valves.

The licensee responded to the Notice of

Violation via letter dated June 17, 1988.

In this response the licensee

attributed the cause of the event to an inadequate safety evaluation.

The licensee noted personnel, who perform safety evaluations for Portland

General Electric Company, had no formal training in the performance of

safety evaluations. Also, the licensee noted the procedure that governed

safety evaluations lacked detail. As longer term corrective actions, the

licensee committed to revise Nuclear Department Procedure (NDP) 100-5

" Preparation of Safety Evaluations Required by 10 CFR 50 and Trojan

Technical Specifications" by October 31, 1988.

The procedure was revised

on December 22, 1988. The inspectors reviewed the procedure revision to

verify the changes to NDP 100-5 clarified the depth and detail required

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for safety evaluations and specified the qualifications of persons

performing and reviewing evaluations. Subsequent to the event, the

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licensee conducted formal training for those individuals ho ~perforni,

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review or approve safety evaluations.

This training has been formally

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incorporated into the Trojan Training Program.

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Open Item 88-03-01, (Closed), Fastener Receipt Inspection and Material "

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Control: In response to identified deficiencies in the receipt, storage,'.

and issuance of fasteners and nuts, the licensee developed an action planL

which included review of procurement spt.cifications for consistency,

repeat receipt inspection of in stock fasteners and nuts, evaluation of

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the adequacy of receipt inspection plans, and an evaluation of fasteners

issued from purchase orders with no material left in stock.

A

significant portion of ~ the corrective actions were documented in

Nonconformance Report NCR 87-417.

The inspectors reviewed a sampling'of

the evaluations for specific stock items in NCR 87-417.

In addition, the

inspectors discussed completed actions with licensee representatives in

materials control and quality assurance.

Based on the above, this item

is closed.

9.

Exit' Interview (30702, 30703)

The inspectors met with the licensee representatives denoted in paragraph

l'on February 10, 1989, and with licensee management throughout the

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inspection period.

A meeting was also held on February 17, 1989.

In

these meetings the inspectors summarized the scope and findings of the

inspection activities.

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