ML20237K902

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Monthly Operating Repts for June 1987
ML20237K902
Person / Time
Site: Hatch  Southern Nuclear icon.png
Issue date: 06/30/1987
From: Gucwa L, Richardson J
GEORGIA POWER CO.
To:
NRC
References
SL-2843, NUDOCS 8708190447
Download: ML20237K902 (13)


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W GEORGIA POWER COMPANY MONTH LY OPERATING DATA REPORTS PLANT HATCH UNITS 1 AND 2 0

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ENCLOSURE 1 l

TABLE OF CONTENTS i PLANT HATCH - UNIT 1 s NRC DOCKET DPR-57 i l

MONTHLY OPERATING REPORT ll)NE 1981 NARRATIVE REPORT s- Nge El-1 1

OPERATING DATA REPORT Page El-2 ]

1 AVERAGE DAILY POWER LEVEL , Page El-3 I UNIT SHUTDOHNS AND PONER REDUCTIONS Page El-4 l

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i NARRATIVE REICRI DOCKET No. 50-321 ,

WIT 1 DATE: JULY 7, 1987 CM PLETED BY: J.H. RICHARDSON ,

TEEPH3NE: (912) 367-7781 x2878 i

. June 1 0000 Refueling outage continues.

June 1 1600 Core reload began.

June 8 0305 Core reload ocenpleted.

June 23 0218 ' Began pulling rods for startup. '

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Reactor critical.

1 June 23 .0338 June 26 0412 Main gonarator tied to line.

June 26 0807 Generator taken off line to perform turbine overspeed testing.

June 26 , 0851: Generator tied to line. Pt:7er ascension in progress.

June 27 2103 Reducing pcwer to shutdown for -

investigation of Drywell Cooler problems. i June 27 2148 Initiated manual scram.

June 28 1608 Began pulling rods for startup. Inlet .

flow control valve for Plant Service Water to "A" Drywell Cooler was found to be manually jacked closed.

June 28 1837 Reactor critical.

June 29 0515 Generator tied to'line. Power ascension in progress.

June 30 1624 Began load reduction to approximately 360 MWe to isolate 5B Feedwater Heater to repair leaking manway on feedwater side of heater.

June 30 2400 Operating at reduced load of 450 NNe for repair of 5B Feedwater Heater, El-1

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I OPERATDG DATA m.w xr DOCKET 10. 50-321 DATE: JULY 7, 1987 CDiPIZIED BY: J. H. RIGARDSON TEI.EEHONE: (912) 367-7781 x2878 OPERATDIG STATUS

1. UNIT NAME: E. I. HATCH UNIT 3
2. REFORP PERIOD: JUNE-87
3. LICENSED THERMAL POWER (!&t): 2436
4. NAMEPI. ATE RATDG (GROSS MWe): 850
5. DESIGN ELECIRICAL RATDG (NET NNe): 776.3
6. MAXD0M DEFENDABIE CAPACITY (GROSS MNe): 783
7. MAXIMUM DEFENDABIE CAPACITY (NET !@e): 750
8. IF CHANGES OCCUR IN CAPACITY RATHIGS (ITDiS 3 THROUGH 7) SINCE IAST REFORD, GIVE REASONS: 10 GANGES

- 9. BDWER IEVEL 70 WHIG REs1MCTED, IF ANY (NET IMe): 10 RESTRICTIONS l

10. REASONS FOR RF.s1MCTION, IF ANY: N/A THIS MONIH YR. TO DATE CUFUIATIVE l
11. HOURS IN mwfulNG PERIOD: 720 4343 100774
12. NUMBER OF HOURS REACIOR NAS CRITICAL: 167.6 2813.8 70461.3
13. REACIOR RESERVE SHUTIn@l HOURS: 0.0 0.0 0.0

.14. HOURS GENERATOR ON-LINE: 83.7 2687.4 66412.8

15. UNIT RES G VE SHUIDOWN HOURS: 0.0 0.0 0.0
16. GROSS THERMAL ENERGY GENERATED (MWH): 103214 6079315 142551226
17. GROSS EI.EC. ENERGY GENERATED (!EH): 22300 1966330 46033680
18. NET EI.EC. ENERGY GENERATED (MWH): 14508 1869694 43712604
19. UNIT SERVICE FACIOR: 11.6% 61.9% 65.9%
20. UNIT AVAII. ABILITY FACIOR: 11.6% 61.9% 65.9%
21. UNIT CAPACITY FACIOR (USDIG MDC NET): 2.7% 57.4% 57.8%
22. UNIT CAPACITY FACIOR (USDG DER NET): 2.6% 55.5% 55.5%
23. UNIT FORCED OUIAGE RATE: 27.3% 3.5% 16.0%
24. SHUTIU4NS SCHEDUIED OVER THE NEXT 6 IONIHS (TYPE, DATE, AND IUPATION OF EAG): N/A
25. IF SHUIDOWN AT END OF wmxr PERIOD, ESTIMATED DATE OF STARIUP: N/A
26. UNITS IN TEST STATUS ( PRIOR TO CCitIERCIAL OPERATION): N/A El-2

9 UNIT 1 AVEPNE DAILY DOCKET 10. 50-321 ICWER IEVEL DATE: JULY 7, 1987 O'HPLETED BY: J. H. RICHARDSON TETEPHONE: (912) 367-7781 x2878 DAY Net M1 l 1 ..'....... 0 l 2 ......... 0 3 ......... 0 4 ......... 0 5 ......... 0 6 ......... 0 7 ......... 0 8 ......... 0 9 ......... 0 10 ......... 0 11 ......... 0 12 ......... 0 13 ......... 0 14 ......... 0 15 ......... 0 16 ......... 0 17 ......... 0 18 ......... 0 19 ......... O 20 ......... 0 21 ......... 0 22 ......... 0 23 ......... 0 24 ......... 0 25 ......... 0 26 ......... 87 27 ......... 198 28 ......... 0 29 ......... 145 30 ......... 416 El-3

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UNIT SHUPDCRE AND ECWER REEUCTIONS DOCKET NO. 50-321 DATE: JULY 7, 1987 UNIT NAME: E.I. HAIG 1 02GIEIED BY: J.H. RICHARIEON TEIEPHONE: (912) 367-7781 x2878 Rt.wxr FDNIH JUlE 1987 l l l 1 lRlMl lS j l l l 1 I l lElEl lY l l l l l lTl l A l T l LICENSEE l 3 C l l l 1

l l lYl l S l H I EVENT lTOl l CAUSE & CORRECITVE l l l l P lIXJRATIONl 0 l 0 l REEORT l E D I00MR2ENrl ACTION TO I l NO. I DATE l E l(HOURS) l N I D l NUMBER l M E l CDDE l PREVENT RECURRENCE l l l l 1 i l l I I I I I87-010 l870601l S l 604.2 l C l 4 l N/A l RC l FUELXX lRefuelity outage continues. l l l l l 1 I I I I I I l87-011 l870626l S l 0.7 l B l 1 l N/A l HA l 'IURBIN l Generator taken off line to l l l l l l l l 1 I Iperform turbine overspeed l I I I I i I I i i Itesting. I I I I I I I I I I I I l87-012 {870627l F l 31.5 l H l 2 l- N/A l SB l HIEXCH l Shutdown for investigation ofl l l l l 1 I I I I lDrywell Cooler problems. I l l l l l l l l l l Inlet flow control valve for l l l l l l l l l l l Plant Service Water to "A" l l l { l l l l l l lDrywell Cooler was found to l l l l l l l l l l lbe manually jacked closed. l l l l l l l l l l l l l l l l l l 1 l l l l l l l l I I I I I I I I I I I I I I I I I I I l l l \ l l I I l l l l l l l l l l l 1 1 I I I I I I I l I I I I I I I I I I I I I I I I I I I I I I I I I

.I I I I I I I I I I I I I I l l I I I I I I I I I I I I I I I I I I I I I I I I I I I I F: FORCED REASON: MEIHOD: EVDTIS ut.wxim INVOLVE S: SCHEEULED A-EQUIEMENT FAIIURE (EXPIAIN) 1 - MANUAL A GREATER THAN 20%

B-MADfrENANCE OR TEST 2 - MANUAL SCRAM REDUCTION IN AVERAGE C-REFUELING 3 - AUIO. SCRAM DAILY POWER LEVEL FOR D-RD3UIFIORY RESTRICTION 4 - CONTINUATIONS THE PRECEEDDiG 24 HOURS.

E-OPERATOR TRAINING & LICENSE 5 - ICAD REDUCTION F-AININISTRATIVE 9 - OIHER (EXPIADI)

G-OPERATIOtE ERROR (EXPIADI)

H-CIHER (EXPIAIN)

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Geoigia Powerkn i

l ENCLOSURE 2 TABLE OF CONTENTS PLANT HATCH - UNIT 2 NRC DOCKET NPF-5 MONTHLY OPERATING REPORT JUNE 1987 NARRATIVE REPORT Page E2-1 OPERATING DATA REPORT Page E2-2 AVERAGE DAILY POWER LEVEL Page E2-3 UNIT SHUTDOWNS AND POWER REDUCTIONS Page E2-4 0166C 100715

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  • NARRATIVE REPTT DOCKET No. 50-366 UNIT 2. DATE:- JULY 7, 1987 '

COMPLETED BY: J. H. RICHARDSON l TELEPHONE: (912) 367-7781 x2878 June 1 0000 Unit Operating at 90% power to limit offgas activity. ,

June 12 2207 Reducing load to 620 We for weekly turbine valve / auxiliaries testing.

June 13 0025 Returning unit to 90% power.

Reducing load to approximately 670 We for weekly June 20 2310 turbine valve / auxiliaries testing.

June 20 2352 Returning unit to 90% power.

June 28 0020 Reducing load to approximately 650 We for weekly turbine salve / auxiliaries testing. 1 June 28 0110 Returning unit to 90% power.

June 30 2400 Unit operating at 90% power to limit offgas activity.

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e OPERATHIG DATA REM RT DOGET 10. 50-366 DATE: JULY 7, 1987 CmPIETED BY: J. H. RIGARDSON ,,

TEIZ1 HONE: (912) 367-7781 x2878 OPERATHG STAIUS:

1. UNIT IGNE: E. I. HAI m UNIT 2
2. m2ucitiG PERIOD: .

JUNE-87

3. IICENSED THERMAL POWER (Wt): 2436
4. IDWEPIATE RATDG (GROSS We): 850
5. DESIGN ELECIRICAL RATHIG (NET We): 784
6. MAXIMUM DEFENDABIE CAPACITY (GROSS We): 794
7. MAXIMUM DEFENDABIE CAPACITY (NET We): 761
8. IF GANGES OCCUR IN CAPACITY RATDGS (ITDiS 3 'IHROUGH 7) SDiCE IAST REFORT, GIVE REASONS: 10 GANGES
9. POWER IEVEL 'IO NHICH hic 1CIED, IF ANY (NET We): 90% (700 We)
10. REASONS FOR RESTRICTION, IF ANY: ADMINISTRATIVE 'IO IlMIT OFICAS ACTIVITY.

'IHIS !ONIH YR /IO-DATE CUMUIATIVE

11. HOURS Di REwinu.tiG PERIOD: 720 4343 68400
12. NUMBER OF HOURS REACIOR WAS CRITICAL: 720.0 4306.0 48329.3
13. REACIOR RESERVE SHUTDOWN HOURS: 0.0 0.0 0.0
14. HOURS GENERATOR ON LINE: 720.0 4272.2 46312.0
15. UNIT RESERVE SHUIDOWN HOURS: 0.0 0.0 0.0
16. GROSS THERMAL ENERGY GDIERATED (MWH): 1580256 9978330 100078265
17. GROSS ELEC. ENERGY GENERATED (MWH): 518150 3306480 32901690
18. NET ELEC. ENERGY GDIERATED (MWH): 495974 3167603 31317482
19. UNIT SERVICE FACIOR: 100.0% 98.4% 67.7%
20. UNIT AVAILABILITY FACIOR: 100.0% 98.4% 67.7%
21. UNIT CAPACITY FACIOR (USDiG MDC NET): 90.5% 95.8% 5949%
22. UNIT CAPACITY FACIOR (USDiG DER NET): 87.9% 93.0% 58.4%
23. UNIT FORCED CUIAGE RATE: 0.0% 1.6% 8.8%
24. SHUIDOWNS SGEDUIED OVER IHE NEXT SIX !ONIES (TYPE, DATE, AND DURATION OF EAG): N/A
25. IF SHUIDOWN AT DID OF m2uc PERIOD, ESTIMATED DATE OF STARIUP: N/A
26. UNITS IN TEST SIAIUS (PRIOR TO CmMERCIAL OPERATION): N/A E2-2

e UNIT 2 AVERAGE DAILY DOCKET NO. 50-366 FCWER IEVEL DATE: JULY 7, 1987 CrHPIEIED BY: J. H. RICHARDSON TEIEPHONE: (912) 3.67-7781 x2878 DAY Net 151

'l ......... 687 2 ......... 689

-3 ......... 690 4 ......... 690 5 ......... 693 6 ......... 693 7 ......... 694 8 ......... 696 9 ......... 696 10 ......... 693 11 ......... 693 12 ......... 684 13 ......... 684 14 ......... 688 15 ......... 689 16 ......... 688 17 ......... 690 18 ......... 687 19 ......... 690 20 ......... 687 21 ......... 687 22 ......... 687 23 ......... 687 24 ......... 683 25 ......... 684 26 ......... 684 27 ......... 686 28 ......... 691 29 ......... 691 30 ......... 685 E2-3

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UNIT SHLTfDOWNS AND KMER REDUCTIONS DOCKETT NO. 50-366 DATE: JULY 7, 1987 UNIT NAME: E.I. HAIG 2 C m PIEIED BY: J.H. RIGARNON TEIEPHONE: (912) 367-7781 x2878 REM RT FONIH JUNE 1987 1 I I I l RIM l lS I I I l l l I lEIEl lY I I l l l lTl l A l T ILICENSEEl S C i l I l I lYl l S I H I EVENT ITOl l CAUSE & CDRRECTIVE l

\ l l l P l DURATION l 0 I O l 1e.kuu I E D lCIMOND7rl ACTION 70 l l 10. I DATE I E l(HCXJRS) l N I D l NUMBER I M E I CDDE I PREVDTI RECURRDIG l 1 I I I I I I I I I I l87-007 I870601l S I OlFI5l N/A l RC l EUELXX l Administrative decision to [

l l l l l l l l l Imaintain 90% power to l l l l l l l l l l l limit offgas activity. l I I I I I I I I I I I I I I I I I I I I I I I I I I I I I I I I l l I l 1 l l I I l l l 1 I I l l l l l l 1 1 I I I I I I I I I I I I I I I I I I I I I I I I I I l l l l I I I I I I I I I I I I I I I I I I I I I I I I I I I I I I I I I I I I I I I I I I I l l \ l l I I I I I I I I I I I I I I I I I I I I I I I I I I I I i l i I I I I I I I I I I I I I I I I i l l I I I I I I I I I I I J l l I F: IDRCED REASON: ME?IHOD: EVDTIS le.wintu INVOLVE S: SGEDULED A-EQUIPMENT FAIIURE (EXPIAIN) 1 - MANUAL A GREATER THAN 20%

B-MADTIENANG OR TEST 2 - MANUAL SGAM REDUCTION IN AVERAGE C-REFUELING 3 - AUIO. SCRAM DAILY FOWER LEVEL FOR D-REGUIAIORY RESTRICTION 4 - CONTINUATIONS 'IHE PRECEEDDIG 24 HOURS.

E-OPERATOR TRAINING & LICENSE 5 - ICAD REEUCTION F-ADMINISTRATIVE 9 - OIHER (EXPIAIN)

G-OPERATIONAL ERROR (EXPIAIN)

H-CIEER (EXPIAIN) e E2-4

a.' Georg a Power Cornpany .

, 333 Piedmont Avenue

w. J Atlanta, Georgia 30306 Telephone 404 526 6526 p Mailing Address:

Fbst Off!ce Box 4545 Alianta, Georgia 30302 Georgia Power L. T. Gucwe .

the southem eicctne systom Manager Nuc;aat Safety -

and ucen3ing SL-2843 0166C X7GJI7-H510 y

. July 13,.'1987 L

Director, Office of Management and Program Analysis U. S. Nuclear Regulatory Commission i Washington, D. C. 20555

-PLANT HATCH - UNITS 1, 2 NRC DOCKETS 50--321, 50-366 OPERATING LICENSES OPR-57, NPF-5 o MONTHLY OPERATING REPORTS Gentlemen: .a Enclosed are the Monthly Operating Reports- for Plant Hatch Unit 1, Docket Number 50-321, and for Plant Hatch Unit 2, Docket Number 50-366.*

These reports are submitted pursuant to the requirements of Technical Specifications Section 6.9.1~.10. 1 Sincerely, f Gu L. T. Gucwa '

LG8/lc  :

Enclosures:

1. Monthly Operating Report for Hatch-1
2. Monthly Operating. Report for Hatch-2 c: (see next page) k 50 I i

Georgia Powerkn c< Director, Office of Management and Program Analysis July 13, 1987 Page Two c: Georaia Power ComDany

}~ Mr. J. P. O'Reilly, Sr. Vice President - Nuclear Operations ,

Mr. J. T. Beckham, Jr. , Vice President - Plant Hatch  !

  • GO-NORMS U. E. Nuclear Regulatory Commission. Washinaton. D. C.

Mr. L. P. Crocker, Hatch Licensing Project Manager 3

U. S. Nuclear Regulatory Commission. Region II Dr. J. N. Grace, Regional Administrator Mr. P. Holmes-Ray, Senior Resident Inspector - Hatch 0166C

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