ML20236T366
| ML20236T366 | |
| Person / Time | |
|---|---|
| Site: | Hope Creek |
| Issue date: | 11/24/1987 |
| From: | Cowles R, Labruna S Public Service Enterprise Group |
| To: | NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM) |
| References | |
| 87-009-00, 87-9, NUDOCS 8712010184 | |
| Download: ML20236T366 (2) | |
Text
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Pubhc Service Electric and Gas Cornpany P.O. Box L Hancocks Bridge, New Jersey 08038 Hope Creek Operations November 24, 1987 U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555
Dear Sir:
HOPE CREEK GENERATING STATION DOCKET NO. 50-354 UNIT NO. 1 SPECIAL REPORT 87-009-00 This Special Report is being submitted pursuant to the requirements of Technical Specification 3.5.1 Action g.
Sincerely, S.
LaBruna General Manager -
Hope Creek Operations RBC/
Attachment SORC Mtg.87-171 C Distribution l
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U E. NUCLEAM REOULATOAV COMMINION NiC Pere 388
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Apr.ROvt0 Oud eso 3190 0104 LICENSEE EVENT REPORT (LER)
DOCERT NUMSER (26 PAGE G PACILITY NAME 11)
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TELEPMONE NUMBER gagg ARE A COOE R.B.
Cowles, Lead Engineer - Technical p;l ng q qi 3 ql _ iSl2 6l4 1
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This Special Report is being submitted pursuant to the requirements of Technical Specification 3.5.1 Action g.
to document the circumstances of a High Pressure Coolant Injection system injection to the reactor vessel on 8/29/87. The HPCI injection occurred as a result of low reactor vessel water level excursion (level 2,
-38")
experienced immediately following a reactor scram.
For a description of the
- scram, refer to LER_87-038.
HPCI injected to the vessel for approximately 3 minutes.
At the onset of the injection, vessel pressure was about 900
As of 8/29/87, Hope Creek had experienced 9 HPCI injections to the reactor vessel (120 cycles are allowed by the FSAR).
Because of the early life of the plant, the HPCI injection nozzle usage factor has not been calculated.
The station is in the initial stages of implementing a thermal cycle tracking program.
This program will allow the calculation of component thermal usage factors.
RBC/
SORC Mtg.87-171 t
JT
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