ML20236S830

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Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-344/87-13
ML20236S830
Person / Time
Site: Trojan File:Portland General Electric icon.png
Issue date: 11/25/1987
From: Kirsch D
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To: Cockfield D
PORTLAND GENERAL ELECTRIC CO.
References
NUDOCS 8711300122
Download: ML20236S830 (1)


See also: IR 05000344/1987013

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NOV 251987

Docket No. 50-344

Portland General Electric Company

121 S. W. Salmon Street

Portland, Oregon 97204

Attention:

Mr. David W. Cockfield

Vice President, Nuclear

Gentlemen:

Thank you for your letter dated November 13, 1987 in response to our Notice

of Violation and Inspection Report No. 50-344/87-13, dated October 16, 1987,

informing us of the steps you have taken to correct the items which we

brought to your attention.

Your corrective actions will be verified during a

future inspection.

Your cooperation with us is appreciated.

Sincerely,

D @ el A;n s up

Denn9s F.% YPsch, Director

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Division of Reactor Safety and Projects

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David W. Cockfield Vice President, Nuclear

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November 13, 1987

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Trojan Nucicar Plant

Docket 50-344

License NpF-1

U.S Nuclear Regulatory Commission

ATTN: Document Control Dock

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Washington DC 20555

Dear Sir:

Response to Notice of Violation

Your letter of October 16, 1987 forwarded a Notice of Violation concerning

inadequate environmental qualification documentation for Rosemount type

resistance temperature detectors (RTDs) and Limitorque valvo actuators that

were not maintained in a condition similar to that in which they werc

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tested. Our response to the Notice of Violation is provided in the

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attachment.

Sincerely,

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Attachment

c: d r. John B. Martin

Regional Administrator, Region V

U.S. Nuclear Regulatory Commission

Mr. Dave Yaden, Director

State of Oregon

Department of Energy

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Mr. R. C. Barr

NRC Resident Inspector

Trojan Nucicar Plant

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Trojan Nuclear Plant'

Document Control Desk

Docket 50-344

. November 13, 1987

License NPF-1

Attachment

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_ Page 1 of 3

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RESPONSE TO NOTICE OF VIOLATION

Violation'No. l'

Contrary to Paragraphs (f) and (k) of 10 CFR 50.49 and Sections 5.2.5 and

8.0 of the Division of Operating. Reactors (DOR) Guidelines, Qualification

File No.15 for Rosemount Type 176KF and 176KS resistance temperature

detectors (RTDs) did not demonstrate that the plant functional perfor-.

mance requirements for their application were met under the postulated

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accident conditions.

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This is a Severity Level IV violation (Supplement 1).

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Response

Portland General Electric (PGE) acknowledges the violation.

A.

The reason for the Violation.

Although the Westinghouse test report, WCAP-9157,zcontained in Quali-

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fication File No. 15, provided documentation to ' demonstrate qualifi-

cation of the Rosemount RTDs to the DOR Guidelines,'the Sandia

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National Laboratory Report, [NUREG-CR/3597 (SAND 84-093) of December-

1984), which provides additional supporting documentation, was not

included in the file to demonstrate RTD qualification.

PGE believed

that the Westinghouse test report provided sufficient documentation

to demonstrate qualification.

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B.

Corrective steps that have been taken and the results achieved.

An evaluation of the Sandia lab report (NUREG-CR/3597 (SAND 84-093)

of 12/84] has been completed in order to provide supplemental data to

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demonstrate that performance requirements were met. Additional in-

formation regarding RTD accuracies was also requested from Westing-

house. Westinghouse is the vendor for the Rosemount RTD sensors

used at the Trojan Nuclear Plant. Westinghouse has reaffirmed that

the methods used to verify RTD accuracies during high-energy line

break (HELB) conditions are sufficient to demonstrate acceptable

performance of the RTDs. This position applies to all RTDs

(including Rosemount Mod.cis 176KF .tnd 176KS).

PGE has incorporated this information into Qualification File No.15,

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The Sandia lab report supports the original qualification methodology

used for demonstrating acceptabic performance under accident

conditions.

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Trojan Nuclear Plant

Document Control Desk

Docket 50-344

November 13, 1987

License NPF-1

Attachment

Page 2 of 3

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C.

Corrective steps that will be taken to avoid further violations.

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PGE is currently involved in an in-depth review of all the equipment

files for environmental qualification of electrical equipment. PGE

is also developing thorough and systematic calculations for enginecr-

ing review of instrument accuracy issues, identification of worst-

case errors under accident conditions for instrument loops, and set-

point calculations. These activities will assure that our qualifi-

cation program does not have a programmatic weakness in the area of

worst-case instrument accuracy, and that the Rosemount RTD perceived

file deficiency is an isolated event.

D.

The date when full compliance will be achieved.

Full compliance has been achieved for Environmental Qualification

File No. 15.

Violation No. 2

Contrary to Paragraphs (f) and (k) of 10 CFR 50.49 and Sections 5.2.2 and

8.0 of the DOR Cuidelines, Limitorque valvo actuators in containment were

not maintained in a condition similar to that in which they were tested,

in that many of their gear case grease relief valves have had dust caps

installed and qualification files covering these Limitorque valve actu-

ators did not contain any justification for the deviation.

This is a Severity Level V violation (Supplement 1).

Response

PGE acknowledges the Violation.

A.

The reason for the Violation.

Request for Design Change (RDC)86-033 was initiated by PGE in order

to provide a comprehensive inspection, maintenance, and repair pro-

gram for all environmentally-qualified Limitorque valve operators at

the Trojan Nuclear Plant. This program occurred during the 1987

refueling outage.

The installation of gear case reliefs where needed

was included. However, the work instructions prepared by engineering

did not include an explicit requirement for the removal of any dust

caps provided by the vendor for shipping and pre-installation

handling. Maintenance and construction work group practices were

also inconsistent in that these dust caps were removed from most but

not all Limitorque valve operators where the installation of a gear

case grease relief was required.

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Trojan Nuclear Plant

Document Control Desk-

Docket 50-344

November 13, 1987

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License NPF-1

Attachment

.Page 3 of 3

B. .The corrective actions that have been taken and the results achieved.

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All Limitorque valve' operators with gear case reliefs were reinspec-

ted for dust caps, and all remaining dust caps were removed. This

corrective action was initiated immediately:siter the deficiency was

identified and was' completed during the 1987 refueling outage. Gear

-case grease reliefs were installed'to accommodate possible grease'

expansion during accident conditions. Since the dust caps'are soft

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plartic and are not qualified, PGE believes that the' dust caps-would

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be sufficiently softened and degraded by the accident conditions such

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that they would-not prevent the relief of grease fror 'he casing.

1Thus, had a loss of coolant accident or HELB occurrec,'the potential

impact of this deficiency would have been negligible,

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C.

The corrective steps that will be taken'to avoid further violations.

PGE will communicate to appropriate' Nuclear Plant Engineers the

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importance of considering the removal of dust caps or other temporary-

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covers during installation. Engineers will be reminded to be aware

of the existence of dust caps or other temporary covers on equipment

being installed, and to explicitly ' instruct the work groups' via the

work instructions to remove these items if needed.

In addition,

recommendations will be made to Plant Maintenance, Plant

Modifications, and Quality Control that they improve work group.

awareness of the need to remove dust caps or other temporary covers

in this case.

D.

The date when full compliance will be achieved.

Prior to 1988 refueling outage (April 1988).

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