ML20216H330
| ML20216H330 | |
| Person / Time | |
|---|---|
| Site: | Arkansas Nuclear |
| Issue date: | 09/12/1997 |
| From: | Howell A NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV) |
| To: | Hutchinson C ENTERGY OPERATIONS, INC. |
| Shared Package | |
| ML20216H336 | List: |
| References | |
| 50-313-97-14, 50-368-97-14, EA-97-382, NUDOCS 9709160202 | |
| Download: ML20216H330 (6) | |
See also: IR 05000313/1997014
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September 12, 1997
EA 97 382
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C. Randy Hutchinson, Vice President
Operations
Arkansas Nuclear One
Entergy Operations, Inc.
1448 S.R. 333
Russellville, Arkansas 72801-0907
SUBJECT: NRC INSPECTION REPORT 50 313/97 14; 50 308/97 14
Dear Mr. Hutchinson:
An NRC inspection of Units 1 and 2 steam generator activities was conducted onsite
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during May 27 through June 20,1997, at your Arkansas Nuclear One, Units 1 and 2
reactor f acilities, with additional offsite review performed during July 14 through August 7,
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1997. The offsite inspection included review of a position paper provided by your staff
regarding the 1990 bobbin coil examination indications obtained during Unit 2
Outage 2F901, that were not identified as missed indications until Refueling Outage 2R12
in 1997. The position paper has been included as Attachment 2 to tho inspection report.
The enclosed report presents the scope and results of this inspection. A telephone exit
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interview was conducted on August 8,1997.
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Based on the results of this inspection, three apparent violations were identified and are
being considered for escalated enforcement action in accordance with the " General
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Statement of Policy and Procedure for NRC Enforcement Actions" (Enforcement Policy),
NUREG 1000. Accordir. gly, no Notice of Violation is presently being issued for these
inspection findings. In addition, please be advised that the number a
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opparent violations described in the enclosed inspection report may change as a result of
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- further NRC review, The three apparent violations involve: (1) the noncompliance with
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bobbin coil sizing qualification criteria; (2) the f ailure to remove Unit 2 tubes from service
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during Outage 2F901, which contained flaws that exceeded the plugging litnit of the
Technical Specifications; and (3) the lack of prompt corrective action in November 1995
prior to returning potentially defective sleeved tubes to service.
While we recognize that the eddy current program enhancements implemented during
Refueling Outage 2R12 were instrumental in the identification of the existence of bobbin
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_c' oil small voltage flaws in prios oJtage data, we remain concerned about the circumstances
_ pertaining to the change in status, for a significant number of Unit 2 tubes, to one. requiring-
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Entergy Operations, Inc.
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plugging or repair af ter only approximately 5 months of unit operation from Outage 2F901.
Also of concern is the adequacy of management controls over the adoption and
implernentation of a now sizing technique for depth of intergranular attack in Unit I steam
generator tubing, in particular, wo would like you to discuss the specific details involved in
your decision to use tubet data obtained from another licensee's steam generators to
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implement this technique. The acceptanco in 1995 of contractor proposed "use as.is"
dispositions for oddy current examirvion identified wold anomalies in installed Unit 2
slooves is also of concern, in that no attempt was made to understand the nature of the
anomalios. Eddy current examination identiflod wold anomalios in gas tungston arc wolded
slooves woro subsequently found by another licensoo to be indicators of actual wold defect
conditions.
A prodocisional enforcement conference to discuss the apparent violations has been
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scheduled for September 20,1997, at 12 noon in the Hogion IV offico. The decision to
hold a prodocisional enforcement conferenco does not mean that the NRC has mado a final
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determination that violations havo occurred or that enforcement action will be taken. This
conference is being hold to obtain information to enable the NRC to make an enforcement
decision, such as a common understanding of the f acts, root causes, missed opportunities
to identify the apparent violations sooner, corrective actions, significance of the issues and
the need for lasting and offectivo correctivo action, in addition, this is an opportunity for
you to point out any errors in our inspection report and for you to provido any information
concerning your perspectivos on 1) the severity of the apparent violations, 2) the
application of the f actors that the NRC considers when it datormines the amount of a civil
penalty that may be assessed in accordance with Section VI.B.2 of the Enforcement Policy,
and 3) any cther application of the Enforcement Policy to this case, including the exorciso
of discretion in accordanco with Section Vll. This conference will be open to public
observation in accordance with the Enforcement Policy.
You will be advised by separato correspondence of the results of our deliberations on this
matter. No response regarding the apparent violations is required at this timo,
in accordanco with 10 CFR 2.700 of the NRC's " Rules of Practice," a copy of this letter
and its enclosure will be placed in the NRC Public Document Room (PDR),
Should you have any questions concerning this inspection, wo will be pleased to discuss
them with you.
Sincoroly,
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MI(4 )
ut lN
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Arthur T. Hos eli lil, Director
Division of Reactor Safety
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Entergy Operatio.,s, Inc.
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Docket Nos.: 50 313;50 368
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License Nos.: DPR 51: NPF 0
Enclosures:
NRC Inspection Report
50 313/97 14; 50 308/97 14
cc w/onclosures:
Executive Vice President
& Chief Operatin9 Officer
Entetgy Operations, Inc.
P.O. Box 31995
Jackson, Mississippl 39280 1995
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Vice President
Operations Support
Entergy Operations, Inc.
P.O. Box 31995
Jackson, Mississippi 39280
Manager, Washington Nuclear Operations
ABB Combustion Engineering Nuclear
Power
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12300 Twinbrook Parkway, Suite 330
Rockville, Maryland 20852
County Judge of Pope County
Pope County Courthouse
Russellville, Arkansas 72801
Winston & Strawn
1400 L Street, N.W.
Washington, D.C. 20005 3502
David D. Snellings, Jr., Director
Division of Radiation Control and
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Emergency Management
4815 West Markham Street,. Mail Slot 30
Little Rock, Arkansas 72205 3807
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Entergy Operations, Inc.
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Manager
Rockville Nuclear Licensing
Framatome Technologies
1700 Rockville Pike, Suite 525
Rockville, Maryland 20852
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Entergy Operations, Inc.
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OFFIClAL RECORD COPY
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Enter 0y Operations, Inc.
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E Mail report to T. Frye (TJF)
E Mail report to T. Hiltz (TGH)
E Mail report to NRR Event Tracking System (IPAS)
E Mail report to Document Control Desk (DOCDESK)
bec to DCD (IE01)
bcc distrib, by RIV:
Regional Administrator
Resident inspector
DRP Director
MIS System
Branch Chief (DRP/C)
RIV File
Project Engineer (DRP/C)
DRS-PSB
Branch Chief (DRP\\1SS)
W. Brown
G. Sanborn
J. Lieberman
OE:EAFile
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DOCUMENT NAME: R:\\_ANO\\AN14RP.lXB
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4'reviously concurred
OFFIC AL RECORD COPY
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