ML20215K092

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Confirms 870601 Mgt Meeting to Discuss Control Room Barrier Issues at Facilities,Per 870526 Telcon.Proposed Meeting Agenda Encl
ML20215K092
Person / Time
Site: Sequoyah  Tennessee Valley Authority icon.png
Issue date: 06/11/1987
From: Zech G
NRC OFFICE OF SPECIAL PROJECTS
To: White S
TENNESSEE VALLEY AUTHORITY
References
NUDOCS 8706250212
Download: ML20215K092 (2)


Text

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JUN 11 1987 ennessee Valley Authority ATTN: Mr. S. A. White Manager of Nuclear Power 6N 38A Lookout Place 1101 Market Street Chattanooga, TN 37402-2801 Gentlemen:

SUBJECT:

CONFIRMATION OF MEETING SEQUOYAH - DOCKET NOS. 50-327, AND 50-328 This confirms the telephone conversation between Mr. H. L. Abercrombie of your staff and myself on May 26, 1987, concerning a management meeting to be conducted in the Region II Office on June 1, 1987, at 11:00 a.m.

We requested this meeting to discuss control room barrier issues at Sequoyah. A proposed meeting agenda is enclosed.

Should you have any questions regarding these arrangements, we will be pleased to discuss them.

Sincerely, ORIGINAL SIGNED By GARY G. ZECH g

Gary G. Zech, Assistant Director, 3

Inspection Programs Division of TVA Projects Office of Special Projects j

Enclosure:

Proposed Meeting Agenda cc w/ encl:

F}. L. Abercrombie, Site Director

f. L. Gridley, Director l

Nuclear Safety and Licensing

/J.A.Kirkebo,ActingDirector

/ Nuclear Engineering

@.R. Harding,SiteLicensing Manager c w/ enc 1:

, G. Keppler, OSP

.S.. D. Ebneter, OSP

d. D. Liaw, OSP j

/J. A. Zwolinski, OSP 8706250212 870611 jS.D. Richardson,OSP PDR ADOCK 05000327 S. R. Connelly, OIA P

PDR K. P. Barr, RII

\\/ NRC Resident Inspector 1

NRC Document Control Desk State of Tennessee

/

6/}/87 6/f/87 dl /87

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ZE45

i ENCLOSURE PROPOSED MEETING AGENDA Tennessee Valley Authority 1

June 18, 1987, 1:00 p.m.

I.

Opening Remarks NRC 1

II.

Issues of Concern TVA/NRC A.

Apparent inadequacies in establishment and implementation of procedures which demonstrate a lack of control over testing evolutions, j

system and equipment status, and procedural changes.

This concern is illustrated by the following examples:

1.

Steam generator spill of February 1, 1987 system realignment without proper review to accommodate a test procedure which was not compatible with plant conditions maintenance of operational status clearance procedures 2.

Pressurizer spill of April 29, 1987 maintenance of operational status 3.

Performance of emergency diesel generator testing on May 28, 1987 j

test procedure noncompliances i

(SI-102 M/M, SI-166.36) clearance procedures 4.

Other observed test procedure noncompliances from May 5, 1987, through June 5, 1987 SI-45.1, ERCW pump testing SI-46.3, CCW pump testing 1

SI-102 E/SA, EDG testing B.

Reportability of the pressurizer spill event of April 29,1987.

III.

Closing Remarks NRC