ML20215E918

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Notice of Violation from Insp on 861021-1120
ML20215E918
Person / Time
Site: McGuire, Mcguire  Duke Energy icon.png
Issue date: 12/10/1986
From: Walker R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20215E911 List:
References
RTR-REGGD-01.033, RTR-REGGD-1.033 50-370-86-35, NUDOCS 8612230167
Download: ML20215E918 (2)


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le ENCLOSURE NOTICE OF VIOLATION Duke Power Company Docket No. 50-370 McGuire Unit 2 License No. NPF-17 During the Nuclear Regulator Commission (NRC) inspection conducted on October 21

- November 20, 1986, a violation of ' NRC requirements was identified.

The violation involved a failure to comply with Technical Specification (TS) 6.8.1 in that written procedures were not properly implemented.

In accordance with the

" General Statement of Policy and Procedure for NRC Enforcement Actions",.10 CFR Part 2, Appendix C (1986), the violation is listed below:

Technical Specification 6.8.1 requires that written procedures be esta-blished, implemented, and maintained covering the activities recommended in Appendix A of Regulatory Guide 1.33, Revision 2, February 1978.

Regulatory Guide 1.33, Revision 2, February 1978 recommends that general plant operations including heatup from cold shutdown to hot standby be covered by written procedures.

Step 12 of Enclosure 4.2, " Pre-Heatup Checklist", of McGuire Operating Procedure OP/2/A/6100/01, " Controlling Procedure for Unit Startup", directs that no-load programmed steam generator levels be established per OP/2/A/6250/03A, " Steam Generator Wet layup Recirculation".

Contrary to the above, OP/2/A/6100/01 and OP/2/A/6250/03A were not properly implemented during a Unit 2 startup on November 17, 1986, in that a control room operator initialed Step 12 of OP/2/A/6100/01 as complete, when, in actuality, steam generator levels had not been established per OP/2/A/6250/03A.

This resulted in a lifting of the steam generator wet layup pump relief valves and a spill of approximately 3000 gallons of secondary water to the auxiliary building floar.

This is a Severity Level IV (Supplement 1) violation and applies to Unit 2 only.

Pursuant to the provisions of 10 CFR 2.201, Duke Power Company is hereby required to submit to this office within 30 days of the date of the letter transmitting

_ - - this Notice,. a written statement or explanation in reply including for each violation:

(1) admission or denial of the violation, (2) the reason for the

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violation if admitted (3) the corrective steps which have been taken and the B612230167 861210 PDR ADOCK 05000369 Q

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Docket No. 50-370 McGuire Unit 2 License No..NPF-17 results achieved, (4) the corr (ctive steps which will be taken to avoid further violations,'and (S) the date when full compliance will be achieved. Where good cause is shown, consideration will be given to extending the response time.

3 FOR THE NUCLEAR REES ATORY COMMISSION y

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- /d s RogerD.WalAer Direc or Division of Y ctor Projects Dated at Atlanta, Georgia a

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  • day of December 1986 6

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