ML20215E519

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SALP Rept 50-285/86-27 for Mar 1985 - Sept 1986
ML20215E519
Person / Time
Site: Fort Calhoun 
Issue date: 12/17/1986
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20215E522 List:
References
50-285-86-27, NUDOCS 8612220360
Download: ML20215E519 (45)


See also: IR 05000285/1986027

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SALP BOARD REPORT

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U.S. NUCLEAR REGULATORY COMISSION

REGION IV

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

Inspection Report 50-285/86-27

Omaha Public Power District

Fort Calhoun Nuclear Station

March 1, 1985, through September 30, 1986

8612220360 861217

PDR

ADOCK 05000285

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PDR

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I.

INTRODUCTION

The Systematic Assessment of Licensee Performance (SALP) program is an

integrated Nuclear Regulatory Commission (NRC) staff effort to collect

available observations and data on a periodic basis and to evaluate

licensee performance based upon this information.

The SALP program is

supplemental to normal regulatory processes used to ensure compliance with

NRC rules and regulations.

The SALP program is intended to be

sufficiently diagnostic to provide a rational basis for allocating NRC

resources and to provide meaningful guidance to the licensee's management

to promote quality and safety of plant operation.

An .NRC SALP Board, composed of the staff members listed below, met on

November 13, 1986, to review the collection of performance observations

and data, and to assess licensee performance in accordance with the

guidance in NRC Manual Chapter 0516, " Systematic Assessment of Licensee

Performance." A summary of the guidance and evaluation criteria is

provided in Section II of this report.

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This report is the SALP Board's assessment of the licensee s safeI,y

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performance at Fort Calhoun Nuclear Station for the period March 1, 1985,

through September 30, 1986.

SALP Board for Fort Calhoun Nuclear Station:

E. Johnson, Director, Division of Reactor Safety and Projects,

Region IV

J. Gagliardo, Chief, Reactor Projects Branch, Region IV

D. Hunter, Chief, Project Section B, Reactor Projects Branch,

Region IV

L. Yandell, Chief, Emergency Preparedness and Safeguards Program

Section, Region IV

P. Harrell, Senior Resident Inspector, Fort Calhoun Nuclear Station,

Region IV

A. Thadani, Director, PWR Project Directorate 8, Office of Nuclear

Reactor Regulation (NRR)

D. Sells, Project Manager, Fort Calhoun Nuclear Station, NRR

Other personnel who participated in all or part of the SALP Board were:

W. Seidle, Chief, Technical Support Staff, Region IV

M. Murphy, Project Inspector, Project Section B, Region IV

H. Chaney, Inspector, Facilities Radiological Protection Section,

Region IV

R. Baer, Inspector, Facilities Radiological Protection Section,

Region IV

N. Terc, Inspector, Emergency Preparedness Section, Region IV

A. Earnest, Inspector, Safeguards Section, Region IV

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II.

CRITERIA

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Licensee performance was assessed in 11 selected functional areas.

Functional areas normally represent areas significant to nuclear safety

and the environment.

Some functional areas may not be assessed because of

little or no licensee activities, or lack of meaningful. observations.

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Special areas may be added to highlight significant observations.

One er more of the following evaluation criteria were used to assess each

functional area.

A.

Management involvement in assuring quality

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B.

Approach to the resolution of technical issues from a safety

standpoint

C.

Responsiveness to NRC initiatives

D.

Enforce' ment history

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E.

Operational events (including response to, analysis of, and

corrective actions for)

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F.

Staffing (including management)

G.

Training and qualification effectiveness

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However, the SALP Board is not limited to these criteria and others may

have been used where appropriate.

Based upon the SALP Board assessment, each functional area evaluated is

classified into one of three performance categories. The definitions of

these performance categories are:

Category 1.

Reduced NRC attention may be appropriate.

Licensee

management attention and involvement are aggressive and oriented toward

nuclear safety; licensee resources are ample and effectively used so that

a high level of performance with respect to operational safety and

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construction quality is being achieved.

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Category 2.

NRC attention should be maintained at norcal levels.

Licensee management attention and involvement are evident and are

concerned with nuclear safety; licensee resources are adequate and are

reasonably effective so that satisfactory performance with respect to

operational safety and construction quality is being achieved.

Category 3.

Both NRC and licensee attention should be increased.

Licensee management attention or involvement is acceptable and considers

nuclear safety, but weaknesses are evident; licensee resources appear to

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be strained or not effectively used so that minimally satisfactory

performance with respect to operational safety and construction quality is

being achieved.

III. SUMARY OF RESULTS

The SALP Board review revealed licensee areas of significant strength with

high management invcivement in assuring quality and with a strong approach

to the resolution of technical issues from a safety standpoint.

However,

the SALP Board also noted that the licensee has failed to improve its

performance in the functional area of security and safeguards and showed a

declining trend in t.he functional areas of radiological controls and

outages.

Even though the functional area of training and qualification

effectiveness showed an improving trend there remain a number of

improvement initiatives to be completed and strong management attention

should continue in this area.

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The licensee's performance is summarized in'the table below, along with

the performance categories from the previous SALP assessment period...

Previous

Present

Performance Category-

Performance Category

Functional Area

(9/1/83 to 2/28/85)

(3/1/85 to 9/30/86)

A.

Plant Operations

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B.

Radiological Controls

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2

C.

Maintenance

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D.

Surveillance

1

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E.

Fire Protection

1

1

1

F.

Emergency Preparedness

2

2

G.

Security and Safeguards

3

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H.

Outages

1

2

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Quality Programs and

2

2

Administrative Controls

Affecting Quality

J.

Licensing Activities

1

1

K.

Training and Qualification

3

2

Effectiveness

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Fifty-two NRC inspections were conducted during this SALP assessment

period, involving 5828 direct inspection man-hours. NRC inspection

reports issued during this assessment period were:

285/85-02 through 285/85-04; 285/85-06; 285/85-08 through 235/85-29

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285/86-01 through 285/86-26

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IV.

PERFORMANCE ANALYSIS

A.

Plant Operations

1.

Analysis

This area was inspected on a continuing basis by the NRC

resident inspector. The inspections included reviews and

observations to verify facility operations were performed in

accordance with regulations, Technical Specifications (TS), and

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procedures.

No violations or deviations were identified in this functional

area.

The three licensee event reports (LER) listed below were

attributed to activities in the functional area of Plant

Operations.

Initiation of the ventilation isolation actuation

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system (VIAS) due to operator error.

(LERs85-004 and

85-005)

Partial loss of onsite power during(a refueling outage due

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to an abnormal electrical lineup.

LER 85-011)

The licensee continued to maintain an experienced group of

licensed senior reactor operators (SR0) and reactor

operators (RO). The operator staff was stable during this

assessment period with a very small turnover rate of licensed

onshift operators.

Staffing was at a level that permitted the

licensee to maintain a six-shift rotation except during heavy

vacation schedules in the summer months. The licensee was in

the process of adding an additional six licenses to the operator

staff and upgrading five R0s to SR0s. The additional licenses

and upgrades were scheduled to be completed in the latter part

of 1987.

Nine plant management personnel held and maintained SRO

licenses. These personnel provided support and technical

expertise to the operations department. The licensed management

personnel included the plant manager, reactor engineer, training

supervisor and instructors, and operations supervisor and

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operations support personnel. During this assessment period,

one shift supervisor was reassigned to serve as an interface

between the maintenance and operations organizations, and an

additional SR0 was assigned to the operations support group.

In the latter part of this assessment period, all management

personnel, licensed and unlicensed, made frequent tours and

inspected the control room, equipment areas, and other operating

spaces. These tours resulted in improved conduct of operations

and increased management visibility.

The licensed operators exhibited a strong, and dedicated

comitment to procedural compliance and a good understanding of

the technical issues associated with plant operations.

These

strengths were observed by the NRC resident inspector and other

NRC inspectors during tours of the control room, during

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emergency and abhormal plant conditions, and during the annual

emergency preparedness exercise. Log keeping and other

documentation maintained by plant operators was performed in an

accurate and highly professional manner.

The NRC resident inspector and other NRC personnel noted that

operator morale declined over this assessment period. The

decline in morale was attributed to the inability of licensed

operators to pass NRC-administered examinations and the lack of

a career path advancement program for onshift licensed

operators.

The NRC resident inspector monitored activities of

onshift licensed operators and noted that the decline in

operator morale did not affect the safe operation of the plant.

During this assessment period, the plant experienced two reactor

trips. One trip occurred in July 1986 due to failure of an

instrument inverter and the other manually initiated trip in

August 1986 was due to overheating of an electrical generator

bus duct.

The last reactor trip prior to these two occurred in

July 1984. On July 31, 1986, the licensee received a letter

from H. R. Denton, Director of NRR, complimenting the licensee

on its low frequency of reactor trips and noting that the low

frequency is an important indication of safe and reliable plant

operation.

In January 1986 the licensee issued and implemented upgraded

emergency operating procedures (E0P), based on the Combustion

Engineering guidelines for emergency procedures.

These E0Ps

provided a symptom-based approach to plant emergencies.

In

conjunction with issuance of the E0Ps, the licensee issued

revised abnormal operating procedures (A0P) in January 1986. The

new A0Ps were issued as an upgrade to the previous emergency

procedures to complement the revised E0Ps.

During this assessment period, the emergency plan was

implemented on two occasions.

In September 1985 a Notice of

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Unusual Event-(N0VE) was declared due to a leaking chlorine

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bottle. The leak was quickly contained and the NOUE was

terminated.

In May 1986 another NOUE was declared due to

incorrect operation of a sampling valve by a chemistry

technician. The misoperation of the valve caused a release of

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radioactive gas to the auxiliary building (AB) and the gas was

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discharged to the atmosphere through the AB ventilation system.

The ventilation system was secured and the unplanned release

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terminated approximately two minutes after initiation due to

quick identification of the problem and subsequent initiation of

corrective actions by the plant operators. Operator actions

limited the level of the release at the offsite boundary. The

magnitude of the release was approximately three times the TS

limit at the site boundary for a duration of approximately

2 minutes. This release did not pose a threat to the health and

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safety of the public. After the AB was isolated and the release

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secured, the NOUE was terminated.

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The safety parameter display system (SPDS) was declared

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operational by the licensee during this assessment period.

Training was provided for plant operators on the use of the SPDS

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and observations by the NRC resident inspector indicated that

the operators used the SPDS effectively. A control room

modification was performed in order to locate an SPDS terminal

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near the plant control boards.

This nodification allowed the

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operators easy access to the terminal while performing

activities on the control boards.

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The licensee continued to implement changes to the control room

based on the results of'the detailed control room design review.

This' effort was ongoing and was not completed during this

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assessment period. The completion of the review was scheduled

for February 1987.

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A program for upgrading the annunciator system to eliminate

nuisance alarms continued throughout this assessment period.

Even though many nuisance alarms were eliminated, the

annunciator system Was still plagued by a number of alarms. The

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licensee continued to work at elimination of all nuisance

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alarms.

During tours of the facility made by the NRC Chairman, NRC

Regional Administrator, and other NRC Region IV personnel

subsequent to the review period, it was noted that plant-wide

housekeeping activities were adecuate.

However, it was also

noted that areas in the plant hac not received the level of

management attention to housekeeping that was considered

appropriate.

In these areas, dust, miscellaneous debris, and

cigarette butts had accumulated.

The need for additional

housekeeping attention in these areas was considered to be an

indication of the need for additional management attention in

maintaining the plant in a clean condition.

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During these tours, NRC personnel also noted that labeling of

valves and piping systems was inadequate.

The licensee used a

method of marking that included uncontrolled, handwritten

identification of system designations on pipes and walls with

felt-tip markers.

The licensee also used brass tags on valves

with the valve number designation only.

The tags did not

contain a description of the valve function.

The licensee

should consider upgrading the plant labeling program by removing

the miscellaneous felt-tip pen markings and initiating a

controlled system for marking piping systems.

In addition, the

Itcensee should consider the use of valve tags that provide a

description of the function, as well as the number of the valve.

2.

Conclusion

The overall performance level in this functional area was

excellent during this assessment period.

Plant management

involvement was effective as evidenced by no violations or

deviations being identified in this functional area and by an

excellent past operating history.

The licensee maintained a

well qualified and stable operations staff.

The licensee is considered to be in Performance Category 1 in

this functional area.

3.

Board Recommendations

a.

Recommended NRC Actions

The NRC inspection effort in this functional area should

remain at the present reduced level,

b.

Recommended Licensee Actions

Licensee management should continue past efforts to ensure

that this functional area is maintained at the current high

level of performance.

Management should take actions to

complete the detailed control room design review and

implement the appropriate control room upgrades in a timely

manner, to eliminate all remaining nuisance alarms from the

control boards, and to upgrade the plant-wide housekeeping

and the plant labeling programs.

B.

Radiological Controls

1.

Analysis

Ten inspections in the functional area of Radiological Controls

were performed during this assessment period by NRC Region IV

personnel.

These inspections included the following areas:

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occupational radiation safety, radioactive waste management,

radiological effluent control and monitoring, transportation of

radioactive materials, and water chemistry controls.

The 13 violations listed below were identified in this

functional area.

No deviations were identified.

Failure to instruct workers prior to entering a restricted

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area.

(Severity Level V, 285/8502-01)

Failure to maintain occupational external radiation

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exposure histories, Form NRC-4.

(Severity Level V,

285/8502-02)

Failure to maintain the data for current occupational

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external radiation exposures, Form NRC-5.

(Severity

Level V, 285/8502-03)

Failute to provide workers with exposure information in a

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termination report.

(Severity Level V, 285/8502-04)

Failure to follow procedures in posting a radiation area.

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(Severity Level IV, 285/8502-05)

Failure to identify a shipment as radioactive and failure

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to perform a transportation survey.

(Combined as one

Severity Level III, 285/8601-01)

Failure to provide workers with exposure information in a

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termination report.

(Severity Level IV, 285/8601-02)

Failure to cuntrol a very high radiation area.

(Severity

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Level III, 285/8601-03)

Failure to report Strontium 89 and 90 results.

(Severity

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Level IV, 285/8605-01)

Failure to review environmental monitoring procedures.

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(Severity Level IV, 285/8605-02)

Failure to follow procedures for retention of radiation

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monitor calibration records.

(Severity Level IV,

285/8608-01)

Failure to submit a special report on the inoperability of

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the postaccident sampling system (PASS).

(Severity

Level IV, 285/8608-02)

Failure to establish operating and calibration procedures

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for portable radiation monitors.

(Severity Level V,

285/8608-03)

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The three LERs listed below were attributed to activities

associated with this functional area.

A chemistry technician caused the initiation of a VIAS

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while purging a line to take a reactor coolant sample.

(LER 85-001)

Containment purge initiated prior to complete purging of

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pressure in contairment caused a VIAS.

(LER 85-007)

Release of radioactive gas to the AB due to misoperation of

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a sampling valve by a chemistry technician.

(LER 86-003)

A detailed discussion of activities associated with this

functional area is provided below.

a.

Occupational Radiation Safety

This area was inspected four times during this assessment

period.

These inspections included three inspections

during routine plant operations and one refueling outage

inspection.

Eight violations related to radiation

protection activities were identified.

The numerous violations identified in the radiation

protection program was an indication of a lack of

management involvement in assuring quality, and worker

training.

Management / supervision had not performed routine

reviews of work activities at the job sites within the

radiation controlled area to ensure radiation protection

controls were properly implemented.

An aggressive,

comprehensive licensee audit / review program had not been

implemented regarding radiation protection activities.

Repeat violations were identified which indicated that the

root causes were not effectively eliminated. Weaknesses in

the radiation protection program were identified in that

radiation protection personnel were not familiar with basic

regulatory requirements and plant procedures.

The size of the radiation protection staff was adequate to

support plant operations.

A low personnel turnover rate

within the radiation protection group was experienced

during this assessment period.

The licensee's approach

concerning the resolution of technical issues indicated a

clear understanding of each issue and included a generally

sound and thorough solution.

The licensee continued to be below the national average

regarding personnel exposures.

The person-rem exposure for

1985 was 373 as compared with the PWR national average of

427.

In 1986 the licensee expended 73 person rem for the

period ending September 30, 1986.

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b.

Radioactive Waste Management

The licensee's program concerning the processing and onsite

storage of gaseous, liquid, and solid radioactive waste was

inspected once during this assessment period.

No

violations or deviations were identified.

The Itcensee implemented a well defined program for the

processing of gaseous, liquid, and solid waste.

No

particular problems were identified in this area,

c.

Radiological Effluent Control and Monitoring

The plant liquid and gaseous effluent control program was

inspected twice during this assessment period.

Two

violations involving gaseous effluent monitoring

instrumentation were identified.

Effluent sampling and

analyses activities were well defined in plant procedures

to ensure compliance with the new Radiological Effluent

Technical Specifications that were implemented during this

assessment period.

Gaseous and liquid release permit

programs were established to ensure that planned releases

received the necessary review and approval prior to

release.

The offsite radiological environmental monitoring program

was inspected twice during this assessment period.

Two

minor violations were identified.

In general, the offsite

radiological environmental monitoring program was well

managed.

The radiochemistry program was inspected once which

included onsite confirmatory measurements with the NRC

Region IV mobile laboratory.

No violations or deviations

were identified.

The results of the confirmatory

measurements indicated that the licensee's percent

agreement was slightly below the value expected for an

operational radiochemistry program.

The PASS was inspected

in conjunction with the radiochemistry program.

One

observation was made which noted that the licensee had not

established a PASS operator requalification/ training

program nor documented chemistry technician performance

training on the PASS.

d.

Transportation of Radioactive Materials

This area was inspected once.

Two violations were

identified.

The two violations were the failure to survey

a radioactive contaminated main steam valve prior to

shipment to an offsite laboratory for repair, and the

failure to identify a radioactive shipment by labeling or

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marking.

These two violations were combined into one

Severity Level III violation.

As a result of the

transportation inspection findings and other related

radiation protection Severity Level III and IV violations,

an enforcement conference was held on April 11, 1986.

Weaknesses were noted concerning the maintenance of

training records and the scheduling of training activities

concerning personnel responsible for transportation

activities.

These weaknesses involved fragmented records

storage, with some of the training information being

maintained outside of the training department, and the lack

of an established schedule for required refresher training.

e.

Water Chemistry Controls

The primary and secondary systems affecting plant water

chemistry were inspected once.

No violations or deviations

were identified.

This inspection was limited in scope;

therefore, a more detailed inspection was planned for 1987.

2.

Conclusion

The following conclusions were made concerning the functional

area of Radiological Controls.

The licensee maintained a high

level of quality in the radiological environmental monitoring

and effluent release control programs.

The areas of

radiochemistry and radioactive waste management were deemed to

be satisfactory.

Several weaknesses were identified involving

management oversight, adequacy of records, conduct of the

radiation exposure control program involving high radiation

areas, and in the radiation protection and radioactive materials

transportation programs.

While management oversight of the various radiological control

program areas was evident by the performance of audits, a

programatic problem existed in that the audits were generally of

insufficient scope and detail to identify program weaknesses.

It was noted that some licensee personnel did not have a good

understanding of regulatory requirements and plant procedures

which is an indication of an ineffective training program.

The licensee's performance was considered adequate in the areas

of resolution of technical issues, reporting operational events,

and staffing.

The licensee's performance was judged to be less

than satisfactory in the area of responsiveness to NRC

initiatives in that responses were often viable, but lacking in

thoroughness or depth.

The licensee is considered to bo in Performance Category 2 with

an overall declining trend in this functional area.

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3.

Board Reconuendations

a.

Recommended f4RC Actions

Inspection effort should be maintained at the normal level

with decreased emphasis in the areas of radiological

environmental monitoring, radiochemistry, effluent control

and monitoring, and radioactive waste management.

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Inspection effort in the areas of occupational radiation

safety, transportation, and water chemistry controls should

be increased,

b.

Recommended Licensee Actions

Management / supervision should spend more time visiting job

sites to ensure radiation controls are properly

implemented. The audit / review program should be expanded

to improve the self-identification of program weaknesses.

The effectiveness of training should be reviewed to ensure

personnel have a good understanding of regulatory

requirements and plant procedures.

C.

Maintenance

1.

Analysis

This area was inspected on a continuing basis by the flRC

resident inspector. These inspections included verification

that maintenance activities were performed in accordance with

procedures, regulatory requirements, and TS.

This area was also

inspected during a special inspection conducted by an NRC

inspection team in the area of equipment environmental

qualification (EEQ).

Two violations and two deviations were identified in this

functional area during this assessment period.

Maintenance was not performed on the component cooling

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water pumps to maintain the EEQ status of the pumps.

(Severity Level IV, 285/8509-01)

Failure to meet a comitment related to cleanliness of

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fluid systems.

(Deviation, 285/8527-01)

Failure to meet a connitment related to storage of critical

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quality equipment (CQE))in temporary storage areas.

(Deviation, 285/8527-02

Failure to store boric acid in a CQE storage area to

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prevent damage or deterioration.

(Severity Level IV,

285/8621-01)

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No LERs were identified in this functional area.

The licensee maintained a very stable and well qualified

maintenance work force with little turnover during this

assessment period.

The licensee added three new instrumentation

and control (I&C) technicians and five new maintenance engineers

to the maintenance staff during this SALP period.

These

additions provided additional technical support for the

maintenance group and additional I&C technicians for an

increased work load in site security systems maintenance and

calibrations.

The maintenance group maintained plant equipment in good working

order.

For this reason, the licensee did not experience any

forced plant shutdowns due to maintenance problems.

During this SALP period, the licensee implemented an automated

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tracking system for maintenance orders (MO).

This system,

CHAMPS, was also used to track and generate preventive

maintenance (PM) items to ensure PM activities were performed

when due to minimize delinquent PMs.

The CHAMPS tracking system

was initiated just prior to the refueling outage in 1985-1986

and tracked each M0 and PM to verify proper and timely

completion.

A special inspection was performed by an NRC inspedion team in

the area of EEQ.

The team noted a maintenance-related problem

in the area of performing maintenance on electrical motors.

The

licensee completed corrective actions for the identified

deficient area.

In the area of EEQ, the licensee also took

corrective actions related to the checking and repair of all

Limitorque motor-operated valves.

The corrective actions

included checking and replacement, as necessary, of the internal

wiring in the Limitorque valves based on problems identified by

the NRC in IE Information Notice 86-03.

This effort was

completed during the 1985-1986 refueling outage.

The licensee's backlog of maintenance activities for all crafts

remained approximately constant during this assessment period.

The level of backlog was approximately 250 man-hours of work on

safety-related systems in each of the areas of electrical, I&C,

and mechanical maintenance.

To ensure that maintenance efforts were directed toward

equipment and components requiring the most immediate attention,

a daily meeting was held between the maintenance and operations

groups.

In this meeting, operations personnel established their

priorities for which maintenance activities should be completed

first.

8ased on the input, the maintenance group established

its daily work schedule.

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The licensee experienced problems controlling the temporary

storage of CQE material during this assessment period.

During

followup on a violation (285/8501-01) identified during the

previous SALP period, the NRC resident inspector noted that the

licensee had not taken the appropriate corrective actions as was

stated in the licensee's response to the violation.

Appropriately, a deviation was issued. At a later time, it was

noted that the boric acid used for control of primary plant

reactivity was not properly stored to prevent damage or

deterioration.

The licensee took actions to correct these

problems.

To correct the problems of having to store CQE

materials in the plant in temporary storage areas, the licensee

proposed and secured funds to relocate the warehouse.

The

warehouse is currently located outside the plant protected area.

The relocation of the warehouse will allow access to materials

from within the protected area and eliminate the need to store

material inside the plant.

The proposed schedule for completion

of the warehouse relocation was 1988.

2.

Conclusion

The licensee had shown increased management attention in the

functional area of Maintenance as indicated by consistent

evidence of prior planning and assignment of priorities.

Additional licensee management attention is needed to reduce the

backlog of maintenance items and to establish and implement an

effective program for storage of CQE material in the plant.

Licensee management attention was evident in that no

maintenance-forced outages occurred during this assessment

period.

The licensee maintained plant equipment in good working

order through an effectively administered PH program.

The licensee is considered to be in Performance Category 1 in

this functional area.

3.

Board Recommendations

a.

Recommended NRC Actions

The NRC inspection effort in this functional area should

remain at the present reduced level,

b.

Recommended Licensee Actions

Licensee management should continue an active involvement

in this functional area to ensure that the present

performance level is maintained.

Management should

continue to reduce the quantity of the maintenance order

backlog.

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D.

Surveillance

1.

Analysis

This area was inspected on a continuing basis by the NRC

resident inspector and by NRC Region IV inspectors.

The

inspections included verificatlun that tests were completed in a

timely manner using an approved testing procedure, tests were

conducted in accordance with TS requirements, and test results

were reviewed to verify equipment and/or component operability.

The violation listed below was identified in this functional

area.

No deviations were identified.

Failure to implement a surveillance required by the TS,

.

(Severity Level IV, 285/8515-03)

One LER was identified in this functional area.

Containment pressure instrument surveillance test was not

.

completed within the required frequency.

(LER 86-002)

'

,

The licensee maintained an effectively managed surveillance test

program. A monthly surveillance testing schedule was published

that included the test due date and responsible performing

organization to ensure the appropriate individuals were notified

of testing res nsibilities.

The master surveillance schedule

was updated, as appropriate, whenever TS amendments were issued.

The NRC resident inspector verified during numerous observations

of survelliance test activities that the testing was prcperly

completed, the latest revision of the testing procedura was

used, and the test was reviewed for compliance with established

acceptance criteria.

The NRC resident inspector observed that

the individuals performing the tests were well acquainted with

the testing requirements and performed the tests in a highly

,

l

professional manner.

The primary basis for the high level of

I

performance was the licensee's stable work force and experience

of the personnel performing the tests.

Surveillance test

results were reviewed at the completion of the test to verify

the acceptance criteria were met.

If the results indicated that

l

the test was unsatisfactory, the equipment and/or component was

repaired and a retest performed in a timely manner.

Although the licensee experienced one identified problem in

l

implementing TS-required surveillances and one in performing

!

surveillances within the required frequency, these problems

appeared to be isolated cases.

Typically, the licensee

l

performed approximately 2500 TS surveillances each year in a

i

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ ________

o

.

17

timely manner.

The licensee maintained a program to ensure that

surveillance activities required by new TS amendments were

!

incorporated into the surveillance program.

2.

Conclusion

The licensee maintained an effectively managed surveillance test

program.

In this functional area, the responsiveness to NRC

issues was timely and technically sound.

Major violations were

rare and were not indicative of a programatic breakdown.

Personnel performing surveillance activities were well trained

and qualified.

The licensee is considered to be in Performance Category 1 in

this functional area.

3.

Board Recommendations

a.

Recommended NRC Actions

The NRC inspection effort in this functional area should

remain at a reduced level,

b.

Recommended Licensee Actions

Licensee management should continue to exercise strong

management controls over the surveillance test program to

ensure that the current high level of performance is

maintained.

E.

Fire Protection

1.

Analysis

This area was inspected by NP,C Region IV inspectors and on a

continuing basis by the NRC resident inspector.

The inspections

were performed to verify the licensee maintained a fire

protection / prevention program in accordance with Branch

Technical Position 9.5-1, commitments to Appendix R to 10 CFR Part 50, and the licensev's fire hazards analssis; housekeeping

and cleanliness control were adequate; and fire brigade training

was perforned in accordance with the TS.

Two violations and no deviations were Identified in this

functional area.

Failure to perform hourly fire watch patrols of degraded

.

fire barriers.

(Severity Level IV, 285/8603-02)

.

-

-

--

-

-

-

-

-

-

.

e

18

Failure to submit a report, as required by the TS, for a

.

fire barrier that was degraded longer than 30 days.

(Severity Level V, 285/8621-02)

The LER listed below involved activities in the functional area

of Fire Protection.

A continuous firewatch was not posted during halon system

.

inoperability.

(LER 85-012)

During this assessment period, the NRC completed the review and

processing of the licensee's exemption requests under Appendix R

to 10 CFR Part 50 and issued the final fire protection Safety

Evaluation Report.

The licensee completed all commitments for

modifications made to satisfy the requirements of Appendix R.

Other significant items initiated by the licensee during this

assessment period are listed below.

-

Requested and received an inspection of all fire doors by

.

Underwriters Laboratory.

As a result of this inspection,

the licensee identified a number of fire doors to be

repaired or replaced.

Installation of new fire doors was

in process at the end of the assessment period.

Selected plant personnel were trained and certified to

.

install and/or inspect the most common types of fire

barrier penetration seals.

Fire barrier records were revised to make them more usable.

.

New fire barrier labels were being installed.

.

A revised fire hazards / transient loading study was

.

initiated.

The licensee issued five special reports on the inoperability of

fire barriers as required by the TS during this assessment

period.

In each reported case, the licensee issued an MO for

repair of the barrier and established a roving or continuous

fire watch, as appropriate.

The licensee took appropriate

corrective actions to ensure the degraded barrier was repaired

as soon as possible.

The 11consee maintained the plant in en adequately clean

condition, with only a few exceptions.

On four occasions, the

NRC resident inspector noted areas where significant amounts of

miscellaneous material had accumulated and the licensee had to

provide addition 6l housekeeping attention.

In each case, the

licensee provided immediate attention to the areas to eliminate

the identified discrepancies.

In no case identified by the NRC

_ - _ _ _ - _ _ _ _ _ _ _ _ _ _

O

3

t

19

inspector, did the housekeeping discrepancies cause the fire

loading for the affected areas to exceed the fire loading stated

in the fire hazards analysis.

During this assessment period, reviews were performed by NRC

inspectors to verify that fire brigade training was performed in

accordance with the TS. The results of these reviews indicated

that the licensee implemented an effective fire brigade training

program and that the individuals participating in the program

were well trained and qualified.

2.

Conclusion

The licensee continued to show significant progress in the

development of an effective fire protection / prevention program.

Licensee management involvement in this functional area was

evident by the progress made in the program.

'

The licensee is considered to be in Performance Category 1 in

this functional area.

3.

Board Recommendations

a.

Recommended NRC Actions

The NRC inspection effort in this functional area should be

reduced.

b.

Recommended Licensee Actions

Lic. ensue management should continue to implement the

program improvement initiatives by completion of the

activities presently underway.

F.

Emerooney Preparedness

1.

Analysis

This area was inspected on a periodic basis by NRC Region IV

inspectors, the NRC resident inspector, and contract personnel.

Three violations and one deviation were identified in the

functional area of Emergency Preparedness.

Three operating shifts were unable to demonstrate the

.

ability to perform 15-minute notifications to state and

local authorities.

(Severity Level IV, 285/8519-01)

.

. _

.

-

l

.

,-

'

'

20

Failure to provide adequate emergency response training to

.

health physics technicians, shift technical advisors, and

reactor operators, and failure to provide adequate training

tests.

(Severity Level IV, 285/8519-02)

Inadequate review of the emergency preparedness program.

.

(Severity Level IV, 285/8519-03)

Failure to meet a commitment to perform training of

.

emergency personnel within 1 year.

(Deviation,

285/8519-04)

No LERs were identified in this functional area,

r

During this assessment period, an emergency response

facilities (ERF) appraisal and four emergent.y preparedness

inspections were conducted.

Two of the inspections consisted of

exercise observations and evaluations, and the other two were

,

routine unannounced inspections.

The results of these inspections indicated that the licensee

demonstrated weaknesses in the areas of training; internal audit

,

program; and procedures related to notifications, protective

action recommendations, security during emergencies, and dose

projections.

Repeat deficiencies were identified during observation of the

,

annual emergency exercise drills.

The deficiencies were

prompting and coaching of the drill players by individuals

running the delli and excessive delay in making notifications to

'

local and state authorities.

These deficiencies are discussed

in NRC Inspection Reports 50-0d5/85-16 and 50-285/86-19.

Additional deficiencies identified during the second exercise

performed during this SALP period indicated that more definitive

corrective actions were needed and that, although the exercise

demonstrated a satisfactory state of emergency response

readiness, improvement was needed in some areas.

,

.

i

The violations and deviation identified during inspections

{

i

indicated a minor programatic breakdown in these areas.

1

However, the licensee's replies and responses to NRC-identified

.

I

problems showed a proper understanding of the issues; viable.

'

generally sound, and thorough approaches and timely responses

i

and resolution of issues.

For example, the NRC inspectors

!

verified that adequate corrective actions were taken in response

'

l

to the violations identified during this assessment period.

l

Sixteen deficiencies were identified during this assessment

i

period aside from the deficiencies identified during the ERF

!

Inspection.

The NRC inspectors closed nine of ten deficiencies

.

l

identified during the first emergency exercise inspection.

l

1

i

i

!

!

t

. _ _ _ _ _ _ _ _ _ _ _ _ _ - .

O

8

21

During this assessment period, a special team inspection was

performed to verify that the licensee had properly constructed,

located, and equipped the ERF as required by NUREG-0737,

Supplement 1.

The results of the inspection noted no violations

or deviations; however, fourteen deficiencies were identified.

The 14 deficiencies identified during the ERF appraisal

pertained to the methods and models used for performing dose

assessment; to the availability of radiation instruments, pocket

dosimeters, and meteorological data; and to the procedures used

for protective action recommendation decisionmaking.

The

details of the deficiencies are provided in NRC Inspection

Report 50-285/86-20.

On May 1, 1986, the licensee declared a NOUE due to release of

radioactive gas to the A8 which was subsequently released to the

environment.

See the functional area of Plant Operations for a

discussion of this event.

The licensee implemented the

emergency plan as required by regulations.

The actions taken by

the licensee for this event included staffing of the technical

support center (TSC).

The NRC resident inspector was present at

the plant and observed the actions taken by the licensee.

Licensee personnel demonstrated the ability to implement the

requirements of the emergency plan during an actual event.

2.

Conclusion

The licensee established adequate emergency response

capabilities and responded well to violations and other

deficiencies identified during NRC inspections.

The results of

the licensee's participation in annual emergency exercises

demonstrated a satisfactory state of emergency response

readiness.

No violations or deviations were identified during

the ERF appraisal and a relatively small number of deficiencies.

However, repeat findings and new exercise deficiencies indicated

the need for additional management attention in this area.

The licensee is considered to be in Performance Category 2 in

this functional area.

3.

Board Recommendations

a.

Recommended NRC Actions

lhe NRC Inspection effort in this functional area should

s

remain at the present level,

b.

Recommended Licenson Actions

The licrnsee should address the weaknesses in the emergency

preparedness training program and correct the deficiencies

-

.

,

22

identified in the last exercise and the ERF appraisal.

The

licensee should establish a program to determine the root

cause of identified problems to ensure the problems are

corrected and not found to be repeat problems in subsequent

inspections.

G.

Security and Safeguards

1.

Analysis

This area was inspected on a continuing basis by the NRC

resident inspector and periodically by NRC Region IV inspectors.

The inspections were performed to verify the licensee was

maintaining a security and safeguards program as required by the

licensee's security program and 10 CFR Part 73.

The 16 violations listed below were identified in the functional

area of Security tend Safeguards.

No deviations were identified.

Unqualified security personnel were performing security

.

duties.

(Severity Level IV, 285/8508-01)

Failure to follow a search procedure at an access control

.

point.

(Severity Level V, 285/8520-01)

Failure to display security badges while in the protected

.

area.

(Severity Level V, 285/8527-03)

Locks, keys, and combinations were not properly controlled.

.

(Severity Level IV, 285/8528-01)

Detection aids for the protected area were found to be

.

inadequate.

(Severity Level IV, 285/8604-01)

Assessment aids were inadequate.

(Severity Level IV,

.

285/8604-02)

Control of locks and keys was inadequate.

(Severity

.

Level IV, 285/8604-03)

A vital area barrier was found to be inadequate.

(Severity

.

Level IV, 285/8607-01)

Inadequate control of a protected area barrier.

(Severity

.

Level IV, 285/8610-01)

Inadequate security force response capability.

(Severity

.

Level IV, 285/8615-03)

Individual guard suitability records were unauthenticated.

.

(Severity Level IV, 285/8615-01)

.

-

-

-

-

- -

-

-

-

-

-

. _ _

-

.

.

23

Failure to conduct behavioral observations.

(Severity

.

Level IV, 285/8615-02)

Inadequate access control for a vital area barrier.

.

(Severity Level to be determined, 285/8617-01)

Inadequate control of safeguards information.

(Severity

.

Level IV, 285/8623-01)

Not identifying a diagram as safeguards information.

.

(SeveriLy Level IV, 285/8623-02)

Inattentive compensatory watchperson.

(Severity level IV,

.

285/8626-01)

No LERs were identified in this functional area.

Eight inspections were conducted by NRC Region IV physical

security inspectors during this assessment period.

Additionally, physical security violations were identified in

four separate reports issued by the NRC resident inspector.

During this assessment period, the licensee failed to take

appropriate corrective action as evidenced by recurring

violations in three different areas. The areas affected

included two violations in control of locks and keys; three

violations for failure to properly control vital and protected

area barriers; and three violations related to the performance,

training, and quantity of security personnel.

These violations

of a repetitive nature was an indication of licensee

management's failure to determine the root cause of identified

problems and take appropriate corrective actions, and the

failure to apply generic corrective actions for eclat,d areas

when a problem was identifled in a specific area.

An enforcement conference was held in Region IV on August 22,

1986, to discuss identified problems related to the failure to

maintain a vital area barrier.

This violation is currently

under review by NRC Headquarters for potential escalated

enforcement.

The enforcement conference was followed by a

management meeting between the licensee and NRC Region IV

security management and inspection personnel to discuss

recurring problems in the area of security.

During this SALP period, the licensee established and staffed

new positions within the security organization.

The licensee

placed nuclear watch officers (unarmed security personnel) on

each shift to supplement the existing security force.

The watch

officers performed compensatory measures and various security

duties.

In addition, the security force was increased to eight

e

.

24

guards per shift.

These actions were taken to ensure sufficient

manpower was available to meet requirements stated in the

licensee's security plan.

The licensee made a personnel change in the security

organization during this SALP period.

The change replaced the

previous management-level individual with an individual with

little previous background and experience in the area of

security.

The licensee has taken action to increase management

positions on each security shift by creating a new position of

security shift supervisor. The positions were in the process of

being filled at the end of the assessment period.

The licensee commenced expansion of the security ouilding during

this assessment period.

The security building expansion will

allow the licensee to control the entrance and exit of personnel

to and from the protecteu area at different control points. The

expansion is currently scheduled to be completed in early 1987.

The licensee also proposed to upgrade the security computer

system.

The upgrade should be completed in 1988.

In May 1986 a Regulatory Effectiveness Review (RER) was

performed by NRC Headquarters, Region IV, and U.S. Army Special

Forces personnel.

The RER was performed to review the impact of

security on safe plant operations and to evaluate the overall

effectiveness of the security program to protect against the

design basis threat for theft and radiological sabotage as

defined in 10 CFR Part 73.

The results of the RER found similar

probleas as had been found by the NRC Region IV inspectors

during this SALP period.

The results of the RER were issued in

a special report dated November 4, 1986.

2.

Conclusion

Licensee management demonstrated a lack of dedication to

establishing and maintaining a security program that is only

minimally acceptable.

Fxpertise and staffing did not appear to

be adequate at the security management level, but the licensee

initiated action to correct this problem.

The licensee was slow

in correcting basic security component deficiencies and tended

to rely on long-term compensatory measures.

At the end of this

assessment period, the licensee developed plans for correcting

some of the long-term deficiencies, but actual hardware changes

were not implemented.

The licensee is considered to be in Performance Category 3 in

this functional area.

.

.

25

.

3.

Board Reconmendations

a.

Recommended NRC Actions

The NRC inspection effort in this functional area should be

increased due to weak management controls and the large

number of violations identified during this assessment

l

period.

The NRC inspection effort should focus on

management effectiveness in resolving problems identified

in weak areas.

b.

Recommended Licensee Actions

The licensee should take aggressive action to increase

management attention to resolve the weaknesses identified

in this functional area. These actions should include

obtaining personnel with a strong security background to

assist in resolving the problems that continue to plague

the licensee's security and safeguards program, resolution

of identified problems and implementation of appropriate

corrective actions to ensure problems do not recur, and

initiation of a program to establish a sound management

approach for upgrading the program.

H.

Outages

1.

Analysis

This functional area was inspected on a continuing basis by the

NRC resident inspector during the period of the Cycle 10

refueling outage from September 28, 1985 through January 9,

1986.

A special inspection was performed by the Safety Systems

Outage Modification Inspection (SSOMI) team of activities

related to this functional area.

The SS0MI team consisted of

members from NRC Headquarters, Region IV, and consultants.

The

inspections included verification that refueling activities,

outage taanagement, repairs and modifications to equipment, and

precperational startup testing were performed in accordance with

the TS, regulatory requirements, and procedures.

No violations, deviations, or LERs were identified during this

assessment period for this functional area.

For the first time, in-house personnel provided supervision and

coordination of Cycle 10 refueling activities.

The supervision

and coordination included refueling of the reactor, modification

work, and preoperational testing.

To provide additional

management involvement with future naintenance and refueling

outages, the licensee established a new position of

L

.

- .

m

.

- --

.

-

m

. . .

. -

_ _ _ _ _ , _ _ - _ _

_.

_ ..

'

, ; "-

.

,

i-

2G

L

Supervisor-Outage Projects. The group headed by this new

manager will provide planning and scheduling of refueling

activities.

Movement of the fuel was completed without incident. The'NRC

resident inspector observed fuel handling activities on numerous

occasions.

Refueling activities were performed in accordance

with TS requirements. The personnel performing fuel movement

activities were well trained and qualified.

The SSOMI team inspection noted significant problems associated

with the installation and testing of modifications installed

during the Cycle 10 outage.

Problems were noted in the areas of

control of special processes, not following testing and

installation instructions, and not providing required

independent inspections by the quality control (QC)

organization. The details of the identified problem areas are

provided in NRC Inspection Report 50-285/85-29.

The NRC is

currently reviewing the results of the inspection and will be

making a determination of the expected enforcement actions. For

this reason, the violations were not listed in this functional

area.

2..

Conclusion

Licensee management demonstrated effective control of the outage

activities associated with the movement and handling of fuel-

during transport to and from the reactor vessel. The licensee

demonstrated significant weaknesses in the area of installation

and testing of plant modifications during the outage. The

weaknesses identified by the SS0MI team were attributed to

taking corrective action that was not effective in correcting the

root cause of identified problems, failing to fully understand

the technical issues and apparent programmatic breakdowns.

The licensee is considered to be in Performance Category 2 in

this functional area.

3.

Board Recommendations'

a.

Recommended NRC Actions

,

The NRC inspection effort in this functional area should

remain at a reduced level for activities associated with

fuel handling and movement. The inspection effort for

installation of modifications should remain at the normal

level. The NRC should perform a detailed followup of

licensee actions taken in response to the items identified

by the SS0MI team.

.

..

27

b.

Recommended Licensee Actions

Licensee management should continue.to exercise the same

level of management control as has been apparent in the

past for the movement of fuel. Management attention and

control should be increased in the significant weak areas

identified by the SSOMI team to ensure activities in these

'

areas are performed in accordance with requirements.

I.

Quality Programs and Administrative Controls Affecting Quality

1.

Analysis

This functional area was inspected on a continuing basis by the

NRC resident inspector and by NRC Region IV inspectors.

This

area was also inspected by a special team inspection performed

in the area of EEQ. A special inspection was also performed of

activities related to this functional area by the SSOMI team.

Inspections performed in this functional area included review of

the administration of quality assurance (QA) and QC activities,

operations QA program, QC program, safety review committees

(onsite and offsite), document control, records, procedures, IE

Bulletin followup, and procurement controls.

The 13 violations and one deviation identified in this

functional area are listed below.

Records for piping thermal stress analysis were not

.

retrievable.

(Severity Level IV, 285/8503-02)

Failure to request exemption for inservice inspection

.

requirements for recirculation piping.

(Severity Level V,

285/8503-04)

Accuracies for PASS monitoring transmitters had not been

.

established.

(Severity Level IV, 285/8509-02)

Containment electrical penetration assemblies instal:ed in

.

the plant were not properly qualified for EEQ applic5tions.

,

(Severity Level III, 285/8509-03)

'

Terminal blocks installed in the plant were not properly

i

.

qualified to EEQ applications.

(Severity Level IV,

285/8509-04)

Electrical cable installed in the plant was not properly

l

.

'

qualified for EEQ applications.

(Severity Level IV,

285/8509-05)

Failure to maintain completed surveillance tests in the

.

files.

(Severity Level V, 285/8511-01)

{'

.

28

Failure to establish document control procedures. (Severity

.

Level IV, 285/8515-01)

Failure to meet licensing requirements related to storage

.

of uranium hexafluoride (UF6) cylinders.

(Severity

Level IV, 285/8515-02)

Failure to follow a procedure related to inspection of UF6

.

cylinders.

(Severity Level IV, 285/8602-07)

Modification to a safety-related system was performed

.

without the use of an approved procedure.

(Severity

Level IV, 285/8603-01)

Failure to maintain installation of cable trays and cable

.

tray covers in accordance with design documentation.

(Severity Level IV, 285/8614-01)

Failure to establish measures to prevent acceptance of

.

electrical cable without a material test report.

(Severity

Level V, 285/8616-01)

Failure to meet a commitment related to parameters

.

monitored by the SPDS. (Deviation, 285/8618-01)

The LER listed below was identified for this functional area.

A nonsingle-failure proof circuit was identified during a

.

refueling shutdown.

(85-009)

A special inspection in the area of EEQ was performed by an NRC

inspection team that included personnel from NRC Headquarters

and Region IV.

The team noted problems affecting the

qualification of various plant components due to inadequate or

missing documentation.

A Severity Level III violation was

identified during the inspection for the failure to properly

qualify the Conax penetrations installed in the plant.

The

inspection team noted that the licensee had implemented an EEQ

program at an unusually early date and that the program was well

developed.

Two' followup inspections were performed by Region IV

and one by the NRC resident inspector.

The results indicated

that the licensee had corrected the documentation deficiencies.

i

A special inspection by the SSOMI team was also performed

related to activities within this functional area.

This team

inspection noted areas of weakness associated with design

configuration control.

The specific areas included problems in

issuance of inadequate installation and testing procedures and

drawings, modification of the facility without performance of a

documented safety evaluation, lack of control for design inputs,

inadequate or inappropriate design analyses, inadequate

o

-

29

procurement documentation, and an inadequate corrective action

program.

The details of these problems are provided in NRC

Inspection Reports 50-285/85-22 and 50-285/85-29.

The NRC is

currently reviewing the results 'of the S50MI for potential

enforcement actions.

For this reason, the severity Itvel for

any potential violations has not been determined; therefore, the

violations have not been listed in this functional area.

During previous SALP reports, the area of records retention and

retrieval was identified as an area of concern to the NRC.

The

licensee experienced problems with records during this

assessment period.

The problem areas included failure to

maintain completed surveillance tests in the files, failure to

retrieve records for piping thermal stress analysis, and failure

to maintain an adequate licensed-operator and health physics

training records program.

The licensee continued to work on

resolving a problem noted in the last SALP report regarding the

filing and retrievability of construction records.

During this assessment period, the licensee experienced

difficulty in meeting commitments made to the NRC.

This was

evidenced by the issuance of deviations in the functional areas

of Maintenance, Radiological Controls, Emergency Preparedness,

and this functional area.

Deviations were identified due to the

licensee's failure to meet commitments made in response to

notices of violation or in response to implementation of

regulatory requirements.

Deviations were also identified from

the licensee's failure to submit reports required by the TS.

The deviations resulted from the licensee's failure to take

actions or to implement the actions within the required time

frame as specified in the response.

The licensee had not yet

established a formal commitment tracking system to ensure that

commitments were met. The licensee was in the process of

establishing a program for commitment tracking which should be

in place in the near future.

Region IV personnel reviewed the licensee's submittal that

described the QA program in effect in 1985.

The review

concluded that the QA program continued to satisfy the

requirements of Appendix B to 10 CFR Part 50.

The licensee increased the staff size during this assessment

period. The staff was increased from 256 to approximately 320

personnel in the Nuclear Production Division.

The licensee

proposed to increase the staffing level at the plant and in the

engineering offices above the current level to resolve the SSOMI

team identified weaknesses, resolve security problems, and

l

provide additional support in training.

!

'

To provide a more timely response to NRC items of concern and

other issues, the licensee established and staffed a new onsite

!

!

l

L

.

.

.

30

position just prior to the end of this assessment period.

The-

position is an onsite licensing engineer whose primary function

is to interface with NRC inspectors and to provide timely

resolutions of any identified concerns or issues.

The licensee established a program to increase management

involvement in plant activities. This program required that

plant management participate in routine activities performed in

the plant on approximately a weekly basis.

Each week the

management group visited a different area of plant activity and

participated in performance of the activity.

The program was

intended to increase plant management's awareness of problems

arising in daily activities.

During this SALP period, reviews were performed to verify that

the onsite Plant Review Committee (PRC) and the offsite Safety

i

Audit and Review Committee (SARC) performed their activities in

accordance with the TS and licensee requirements. The results

of the inspections indicated that the PRC and SARC are

adequately performing their required activities.

The SARC

performed audits during the assessment period that included more

individuals on the audit team with a technical background in the

area being audited.

Inspections were also performed in the areas related to

activities performed by the QA and QC groups.

These inspections

were performed by NRC Region IV inspectors and on a periodic

basis by the NRC resident inspector.

The results of the

inspections indicated that the licensee was maintaining an

adequate QA and QC staff with the appropriate qualifications.

The licensee has proposed increases in both the QA and QC

staffs.

The QA department has increased the usage of technical

specialists for the performance of audits in the areas of

security, chemistry, EEQ, inservice inspection, and the

radiological effluent program.

2.

Conclusion

The licensee demonstrated implementation of acceptable QA and QA

programs during this assessment period.

The licensee has shown

difficulties in meeting commitments made to the NRC due to a

commitment tracking system not being established.

The licensee continued to exhibit difficulties in the area of

records storage and retrievability.

This has been identified in

past SALP reports and the' licensee has expended resources in

this area; however, the establishment of an appropriately

functioning records system has not been completed.

The licensee has not been timely in resolving or addressing

concerns or issues identified by NRC inspectors.

The problems

%

, ~ .

-

-

, - - - -

. - -

.

.

.e

31

identified by the SSOMI team indicated a need for increased

management attention in the area of design configuration

control.

The licensee is considered to be in Performance Category 2 in

this functional area.

3.

Board Recommendations

a.

Recommended NRC Actions

The NRC inspection effort in this functional area should

remain at ncrmal levels.

b.

Recommended Licensee Actions

Licensee management should increase efforts to resolve the

problems identified in SALP reports regarding a record

retention and retrieval system.

Licensee management

involvement in the area of commitment tracking should be

increased to provide a tracking system that will ensure the

commitments made are completed accurately and in a timely

manner.

Licensee management should take action to ensure

that more timely response to concerns or issues identified

by the NRC is provided. Additional licensee management

'

attention should be provided in the area of design

configuration control.

J.

Licensing Activities

1.

Analysis

This functional area was monitored on a continuing basis by the

NRR Project Manager during this SALP period.

Licensing

activities included technical reviews associated with

amendments, extensions, exemptions, orders, and miscellaneous

reviews related to plant operations.

A listing of the licensing

activities completed during this assessment period is provided

in Section V.H.

,

i

The licensee continued to show good management overview in the

functional area of Licensing Activities.

The licensee

consistently balanced the desire to maintain or improve plant

productivity with the need to protect the health and safety of

the public.

The majority of the licensing actions completed

-

during this SALP period were resolved by the licensing group.

I

This was accomplished by closely coordinating the technical

efforts of the licensee's staff, consultants, contractors, and

suppliers.

In instance's where matters were referred to upper

management, the individuals involved proved to be well informed

and helpful in resolving questions.

Upper management was

f..

32

!

actively involved in resolving problems and was well informed of

conditions that needed their attention.

Upper management was

also involved in maintaining and improving the quality of work

done at the facility by actively participating in the

development of quality improvement programs that included the

initiation of planning to develop an integrated living schedule.

During this assessment period, errors were found in the codes

used in the core physics analysis.

Licensee management took

aggressive action to ensure an early and satisf actory resolution

of this issue.

Licensee management continued to pursue a

program that was aimed at improving and increasing the technical

capability of the staff, including the approval to purchase and

install a site-specific simulator and initiating a construction

program to improve the security and staff facilities at the

plant.

During this assessment period, a SSOMI team inspection

was conducted.

Licensee management was active in addressing the

issues raised by this inspe. tion.

As indicated above, the licensee continued to maintain a

significant technical capability in engineering and scientific

disciplines necessary to resolve items of concern to the NRC and

the licensee.

During this assessment period, the licensee

expanded the staff at the facility as well as the support staff

located at the main office in Omaha.

Further staff expansion

was planned in the future.

In addition, the licensee continued

to utilize the services of Combustion Engineering and other

nuclear support groups to assist in the resolution of technical

problems or to develop improvements that enhanced the operation

t

and safety of the facility.

The licensee was completing the

review of analytical models to be submitted to the NRC for

approval for use in the 1987 refueling outage at the end of this

assessment period.

The licensee's extensive and improving technical capability was

reflected in the submittals made in support of or in response to

I

i

licensee- or NRC-initiated actions. With few exceptions, the

l

technical content of these submittals was complete and thorough.

l

t

Where additional information was needed, it was of a clarifying

!

nature for the most part and in many cases handled by a phone

call with a followup letter to confirm the verbal conversations.

Few licensee responses to NRC requests for additional

information required subsequent questions.

The licensee applied probabilistic risk assessment techniques in

the analysis of the auxiliary feedwater (AFW) system.

The

analyses were used to support the continued operation of the two

i

AFW pump system at the plant.

Although this issue has not been

I

completely resolved, the results of the analyses performed by

the licensee were presented to the staff in November 1985 and

provided the bases for continued use of the existing system.

I

,

, . .

e

I

33

The licensee responded promptly to NRC staff initiatives.

During this assessment period, the licensee worked with the NRC

in resolving multiplant and TMI action items.

In each case, the

licensee carefully evaluated the action in question and provided

meaningful input to the NRC staff.

Particularly noteworthy is

the support provided by the licensee to the control room

habitability study performed by the NRC. The licensee also

provided the necessary support to bring TMI action items related

to the ERF and the SPOS to a point where final NRC closeout can

be expected in the next assessment period. Where differences

occurred, the. licensee negotiated changes to ensure that the

results adequately reflected safety considerations and

incorporated the staff's positions and licensee's desires.

This

c: curred in the development of the TS changes made to

incorporate the requirements of 10 CFR Part 50.72 and 50.73 and

provided the bases for the resolution of the TS changes that

will incorporate the inadequate core cooling instrumentation

system.

Staffing improvements were made by increasing the number of

qualified personnel and the realignment of responsibilities to

better utilize the individuals that support plant operations.

For example, additional operators were added to the staff during

this assessment period to ease staffing problems that occurred

due to intensified training requirements.

2.

Conclusion

The licensee's activities in this functional area were conducted

by a well staffed and well trained group resulting in an overall

efficient operation.

Management overview was evident in that

the licensing effort, for the most part, was well integrated

into other plant and licensing activities as reflected in a

uniform approach.

Upper management became involved in licensing

actions, when necessary, to assist in resolving potential

deadlocks.

The licensee should be commended for the diligent

way in which licensing actions were resolved and the willingness

to compromise to achieve agreement with NRC staff positions.

The licensee is considered to be in Performance Category 1 in

this functional area.

3.

Board Recommendations

a.

Recommended NRC Actions

Continue the close monitoring of licensee activities in

this functional area and provide the NRC guidance required

to assist the licensee in the resolution of licensing

issues.

m

.

.

34

b.

Recommended Licensee Actions

Continue to improve the quality and size of the staff and

continue to exercise the same level of management attention

that has been apparent in the past.

K.

Training and Qualification Effectiveness

1.

Analysis

This functional area was inspected by Region IV personnel and on

a periodic basis by the NRC resident inspector.

Inspections

included review of nonlicensed training and licensed-operator

training. The review of licensed-operator training was

performed to verify that the licensee implemented the

requirements stated in Appendix A to 10 CFR Part 55 and the

licensee's NRC-approved training program.

No violations, deviations, or LERs were identified in this

functional area.

An inspection was performed in the area of nonlicensed training.

The inspection included reviews in the areas of general employee

training; chemistry and radiation protection training; and

training provided for maintenance, QC, test engineering, and

shift technical advisor personnel. The results of this

inspection indicated that these programs were being implemented

effectively and in accordance with commitments made to the NRC.

During this assessment period, examinations were administered by

the NRC as tabulated below.

Initial Examinations

.

SR0 Candidates

R0 Candidates

Total

Pass Fail

Total

Pass Fail

June 18, 1985

2

2

0

4

4

0

November 12, 1985

1

1

0

0

0

0

Upgrade Examinations

.

SR0 Candidates

Total

Pass Fail

November 12, 1985

3

1

2

____-_____

_ _ _ _

.

.

35

.

Requalification Examinations

.

SR0 Candidates

R0 Candidates

t

Total

Pass Fail

Total

Pass Fail

November 12, 1985

5

0

5

3

2

1

March 18, 1986

5

4

1

2

1

1

Based on the failure rate of the examinations given on

November 12, 1985, a' management meeting was held in

December 1985 to discuss the status of the licensee's

licensed-operator requalification program.

Based on the

management meeting, the licensee committed to institute changes

- to the program.

The licensed personnel that failed the examination were removed

from licensed duties and placed in accelerated requalification

training. At the end of the requalification training, the

personnel were reexamined on March 18, 1986.

Based on the results of the performance by licensed operators on

examinations, the licensed cperator training program was rated

by the NRC as unsatisfactory for fiscal year 1986. The program

will be further evaluated during the week of November 17, 1986.

-

An inspection was performed in the area of licensed-operator

training in August 1986 to evaluate the program status and the

licensee's progress in making improvements in the

requalification program. During this inspection, four

unresolved items were identified that constituted potential

violations. Problems were noted in the areas of review of

emergency procedures, completion of manipulations on plant

controls, lecture attendance, and maintenance of training

records.

The inspection results also indicated that the licensee had

provided accelerated requalification training to the individuals

that failed to pass the NRC-administered examination given on

November 12, 1985. However, the NRC inspectors noted that the

licensee had not completed the actions committed to during the

management meeting in December 1985. The implementation was in

progress but the schedule indicated that corrective actions

would not be completed until the middle part of 1987.

The licensee proposed and secured funds to construct a new

,

training facility with a site-specific simulatcr. The training

l

facility,was scheduled to be completed in 1989 and the simulator

i

to be completed in 1990. During a visit to the plant on

November 5,1986, the NRC Chairman noted that licensee

__

-

_ _ _ _ _ _ _ _ _ _ - _ _ _ _ - _

_ _ _ _ _ _ _ _ _ _ _ _ _

. _ _ _ .

- _ _

-

. __

__

_.

. - - _ _ _ _ _ _

-

9

I

36

h

management should consider taking actions to construct the

training facility and simulator sooner than the currently

proposed schedule.

The licensee began work on obtaining accreditation for training

programs from the Institute of Nuclear Plant Operations (INP0).

The INP0 accreditation was expected to be received by the end of

1986.

'

Just prior to the end of this assessment period, an

organizational change was made within the training organization.

The Supervisor-Station Training was assigned to report to the

Manager-Administrative Services, a corporate-level position.

Prior to this change, the supervisor reported to the plant

manager.

The size of the training staff maintained by the licensee was

small. However, the number of operators at the facility is

small and it appeared that the size of the training staff was

sufficient to meet the facility's training demands.

During this assessment period, the licensee initiated or

completed activities to improve performance in this functional

'

area. A discussion of these activities is provided below.

Developed performance-based training materials.

.

Implementation of the new materials was scheduled to be

completed in the near future.

Expanded the examination question bank to include

.

performance-based questions.

Developed a training program master plan (TPMP) to replace

.

the training manual.

The TPMP will provide more

comprehensive and easier to interpret training

requirements. The TPMP was scheduled for implementation in

1987.

Established a QC personnel training program with the

.

Southeast Commumity College.

This program provided

continued refresher training for QC personnel.

2.

Conclusion

The licensee maintained an effective program in the area of

nonlicensed training. Weaknesses were identified in the area of

licensed-operator training.

The licensee took actions to

improve performance in this functional area.

.

.

37

The effectiveness of the licensee's training programs appeared

to be, in part, due to the low personnel turnover rate.

The

licensee has not demonstrated that the training programs would

be adequate in the event the turnover rate increased.

The licensee is considered to be in Performance Category 2 in

this functional area.

3.

Board Recommendations

a.

Recommended NRC Actions

The NRC inspection effort in this functional area should be

maintained at the normal level with emphasis placed on

licensed operator training.

b.

Recommended Licensee Actions

Licensee manigement should continue implementaton of the

actions initiated during this assessment period to improve

the licensed and nonlicensed training programs.

Licensee

management attention to resolve the weaknesses identified

in the licensed-operator training program should be

increased.

V.

SUPPORTING DATA AND SUMMARIES

A.

Licensee Activities

1.

Major Outages

The license + shut down the plant on September 28, 1985, for the

Cycle 10 re!aeling outage at the Fort Calhoun Nuclear Station.

Major activ w..:s accomplished during the refueling outage

included eddy current testing of both steam generators, plegging

of steart. generator tubes, installation of seismic supports for

masonry walls, replacement of HFA relays, replacement of

instrument invarters, and replacement of containment penetration

assemblies.

Tne reactor was taken critical on January 9,1986,

to end the refueling outage.

2.

Power Limitations

Power was limited during this assessment period during various

plant startups for steam generator chemistry considerations.

When the plant was started up, hold points for power level were

observed to allos steam generator chemistry to be adjusted

within specific guidelines.

After the chemistry was within the

guidelines, power escalation was continued.

o

.

38

3.

License Amendments

Amendment 86

April 3, 1985

Incorporate Requirements

of Appendix I

Amendment 87

April 29, 1985

Toxic Gas Monitoring

Amendment 88

May 9, 1985

Reactor Protection System

Bypassing / Tripping

Amendment 89

May 24, 1985

Postaccident Sampling

Amendment 90

August 19, 1985

Testing Frequency for

AFW Pumps

Amendment 91

August 22, 1985

Process Control Program

Surveillance Requirements

Amendment 92

November 29, 1985

Cycle 10 Power Operation

Amendment 93

December 6, 1985

Administrative Changes

Amendment 94

January 10, 1986

Capsule Removal Schedule

Amendment 95

February 3, 1986

Leakrate Testing

Surveillance

Amendment 96

April 24, 1986

Updated Snubber Tables

Amendment 97

June 3, 1986

Recirculation Heat

Removal

Amendment 98

July 1, 1986

Fire Suppression

Equipment

Amendment 99

August 13, 1986

10 CFR Part 50.72 and

50.73 Requirements

Amendment 100 September 8, 1986

Heatup and Cooldown

Curves

4.

Significant Modifications

Modifications completed during this assessment period included

installation of seismic supports for masonry walls, installation

of a fire support system in the AFW pump area, replacement of

instrument inverters and transformers, and installation of

delta T power process loops.

.

.

p.

39

B.

Inspection Activities

1.

Violations

See Table 1 for a tabulation of the identified violations and

deviations in each functional area for this assessment period.

2.

Major Inspections

Special inspections were' performed in various areas of licensee

activities.

The listing below provides details of the

inspections.

An EEQ special inspection was performed by NRC Headquarters

.

and Region IV personnel in April and May 1985 to verify

licensee compliance with 10 CFR Part 50.49.

The details of

the inspection are provided in NRC Inspection

Report 50-285/85-09.

A special inspection in the area of outage modification

.

activities was performed in September, October, November,

and December 1985 by the S50MI team.

The SSOMI team

consisted of members from NRC Headquarters, Region IV, and

consultants. This inspection was performed as part of a

trial NRC program being implemented to examine the adequacy

of licensee management and control of modifications

performed during major plant outages.

The details of the

inspection results are provided in NRC Inspection

Reports 50-285/85-22 and 50-285/85-29.

The violations and

associated severity levels from these two reports will be

issued in the near future.

In April and May 1986 an RER was performed by personnel

.

from NRC Headquarters, Region IV, and members of the U.S.

Army Special Forces.

The RER was performed to review the

impact of security on safe plant operations and to evaluate

the overall effectiveness of the security program to

protect against the design basis threat for theft and

radiological sabotage as defined in 10 CFR Part 73. The

results of the RER were issued in a special report dated

November 4, 1986.

A special inspection was performed in July 1986 by NRC

.

Region IV personnel and contractors.

The inspection was

performed to verify the adequacy of the licensee's ERF as

required by NUREG-0737, Supplement 1.

The details of this

inspection are provided in NRC Inspection

Report 50-285/86-20.

i

.

.

40

i

C.

Investigations and Allegations Review

During this assessment period, an allegation was made by a licensee

employee that licensee management had failed to take remedial action

in response to incidents of fighting, sleeping on the job, harassment

of personnel, and intimidation of fellow employees that occurred

during the period 1979 through 1984.

The NRC reviewed the allegation

and determined that the incidents described by the licensee employee

were not a safety concern and that the incidents did not affect the

health and safety of the public.

No investigations were completed during this SALP period.

D.

Escalated Enforcement Actions

Three notices of violation with proposed imposition of civil

penalties were issued to the licensee during this assessment period.

A discussion of each is provided below.

A Severity Level III violation without a proposed civil penalty

.

was issued in NRC Inspection Report 50-285/85-09. The violation

was issued as a result of the licensee's failure to properly.

qualify Conax electrical penetration assemblies in accordance

with the equipment qualification rule stated in 10 CFR Part 50.49(k).

A civil penalty was not proposed for this

violation as the violation was identified prior to the

November 30, 1985, deadline for environmental qualification of

electrical equipment, and an extension for this item could have

been granted by the NRC.

In NRC Inspection Report 50-285/86-01, two Severity Level III

.

violations were issued without a proposed civil penalty.

The

violations included the failure to identify a main steam valve

as radioactive and to perform radiological surveys prior to

shipping the valve offsite, and the failure to control a very

high radiation area.

Due to the licensee's demonstrated past

good performance in the functional area of Radiological

Controls, a civil penalty was not proposed for these two

violations.

E.

Licensee Conferences Held During This Assessment Period

The following conferences were held between the licensee and the NRC

during this assessment period.

A management meeting was held on December 12 and 13, 1985, to

.

discuss the NRC concerns related to the qualification of

NRC-licensed operators.

In an examination given on November 12,

1985, six of eight operators failed to pass the NRC examination.

This high failure rate and the proposed requalification of the

six individuals were the bases for the management meeting.

l'

. - .

41

A management meeting was held December 13, 1985, at the

.

Region IV office to discuss concerns related to the EEQ

inspection.

The bases for the meeting were the results noted

during performance of an NRC inspection in the area of EEQ as

detailed in NRC Inspection Report 50-285/85-09.

An enforcement conference was held on April 11, 1986, to discuss

.

concerns related to health physics activities.

The bases for

the conference were the findings stated in NRC Inspection

Report 50-285/86-01. The NRC noted in the report that the

licensee failed to perform a radiological survey on a

contaminated valve prior to shipment to an offsite calibration

facility and failed to properly control a very high radiation

area.

On July 10, 1986, an enforcement conference was held to discuss

.

the findings of a special inspection performed by the S50MI

team.

The results of the team inspection are detailed in NRC

Inspection Reports 50-285/85-22 and 50-285/85-29.

The NRC is

currently reviewing the results of the team inspections for

potential enforcement actions.

The results of this review will

be issued in the near future.

An enforcement conference was held on August 22, 1986, in the

.

Region IV office to discuss the licensee's failure to adequately

maintain a vital area barrier.

The details of this violation

are provided in NRC Inspection Report 50-285/86-17.

F.

Confirmatory Action Letters

During this assessment period, one confirmatory action letter (CAL)

was issued by the NRC.

This letter, dated December 20, 1985, related

to confirmation of commitments made by the licensee in a management

meeting held in Region IV on December 13, 1985.

The CAL discussed

actions planned to be taken by the licensee as a result of an NRC

followup inspection in the area of EEQ.

G.

Review of Licensee Event Reports and 10 CFR Part 21 Reports Submitted

by the Licensee

1.

Licensee Event Reports

There were 16 LERs issued during this assessment period

including LERs85-001 through 85-012 and 86-001 through 86-004.

Trends were noted in the following areas.

.

The licensee reported seven instances of inadvertent

.

initiation of the VIAS due to various reasons (e.g.

equipment problems, personnel error, and plant systems

leakage).

The VIAS initiations occurred up to the latter

part of 1985.

Since that time, the licensee has not

_ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ .

. _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

.:* a

42

experienced an actuation due to licensee management

involvement in preventing an inadvertent operation of the

system.

The LERs listed below were issued by the licensee during this

assessment period.

The SALP Board reviewed these LERs and

determined that the root cause did not warrant placement within

a specific functional area.

Automatic reactor trip caused by failure of an instrument

.

inverter.

(LER 86-001)

Manual reactor trip due to overheating of a bus duct on the

.

station electrical generator.

(LER 86-004)

Initiation of a VIAS caused by leaking radioactive

.

effluents from a piping system.

(LER 85-002)

Initiation of a VIAS due to torn filter paper in a

.

'

radiation monitor.

(LER 85-008)

Main steam safety valves failed to lift within setpoint

.

values during surveillance testing.

(LER 85-006)

A lockout relay failed to properly function during

.

surveillance testing.

(LER 85-010)

The NRC's Office of the Analysis and Evaluation of Operational

Data performed an evaluation of the content and quality of a

representative sample of LERs submitted by the licensee.

The

results of the evaluation were provided to the licensee under a

separate cover letter.

2.

10 CFR Part 21 Reports

In a letter dated March 17, 1986, the licensee issued a 10 CFR Part 21 report to the NRC regarding failure of Valcor valves.

The report stated that the valve disc guide assembly springs had

failed causing the valve to be inoperable.

The spring failure

was attributed to hydrogen embrittlement.

The licensee replaced

the springs in the valves with the same spring material and

tested the valves for satisfactory operation.

The licensee

intends to replace the springs during the 1987 refueling outage

with a material not susceptible to hydrogen embrittlement.

.~~a

43

H.

Licensing Activities

1.

Licensing Activities Completed

Issue

Completion Date

Special steam generator tube

March 8, 1985

inspection

Reevaluation of the AFW Technical

April 24, 1985

Specifications

Emergency core cooliag system error

June 13, 1985

and core height

Reactor vessel-to-nozzle welds

June 19, 1985

Control of heavy loads, Phase II

June 28, 1985

Loss-of-coolant accident analysis

July 1, 1985

Compliance with 10 CFR Part 50.46

July 1, 1985

Core reload methodology changes for

August 26, 1985

Cycle 10

Alternate shutdown capability, upper

November 4, 1985

electrical penetration room

Steam generator tube integrity

December 11, 1985

Control room habitability

December 27, 1935

Validation of mini-CECOR/ BASS system

March 10, 1985

Inservice inspection relief for

June 24, 1986

recirculation piping

Clarification of fire protection

July 1, 1986

modifications

Generic Letter (GL) 83-28, Salem

July 3, 1986

anticipated transient without

scram (ATWS), Item 3.2

GL 83-28, Salem ATWS, Item 4.5.1

July 10, 1986

2.

Extensions, Exemptions, and Orders

EEQ deadline additional extension

March 29, 1985

i

.

  • a

f

44

Appendix R to 10 CFR Part 50, fire

July 3, 1985

protection

' Modification of Commission Order, dated

January 9,'1986

February 22, 1984

Appendix J to 10 CFR Part 50,

January 10, 1986

containment leakage

3.

Meetings

Reliability of the AFW system

November 8, 1985

. se o

TABLE 1

ENFORCEMENT ACTIVITY

FUNCTIONAL AREAS

NUMBER OF VIOLATIONS IN EACH LEVEL

I

II

III

IV

V

OEVIATIONS

A.

Plant Operations

0

0

0

0

0

0

B.

Radiological Controls

0

0

2

6

5

o

C.

Maintenance

0

0

0

2

0

2

D.

Surveillance

0

0

0

1

0

0

E.

Fire Protection

0

0

0

1

1

0

F.

Emergency Preparedness

0

0

0

3

0

1

G.

Security and Safeguards *

0

0

0

13

2

0

H.

Outages **

0

0

0

0

0

0

I.

Quality Programs and

0

0

1

S

3

1

Administrative Controls

Affecting Quality **

J.

Licensing Activities

0

0

0

0

0

0

K.

Training and Qualification

0

0

0

0

0

0

Effectiveness

TOTAL

0

0

3

35

11

4

  • One additional violation was identified in this functional area but the

severity level of the violation has not been determined.

    • Additional violations were identified in this functional area based on the

results of the SS0MI team inspection.

The number and severity level of the

violations have not been determined.

This determination will be made in the

near future.