ML20214L561

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Monthly Operating Rept for June 1986
ML20214L561
Person / Time
Site: Millstone 
Issue date: 06/30/1986
From: Newburgh G
NORTHEAST NUCLEAR ENERGY CO.
To:
Shared Package
ML20214L558 List:
References
NUDOCS 8609100269
Download: ML20214L561 (3)


Text

AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-245 UNIT Millstone 1 DATE 860701 COMPLETED BY G. Newburgh TELEPHONE (203) 447-1791 Ext. 4400 MONTH June 1986 DAY

' AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)

(MWe-Net) 1 655 17

'653 2

656 18 635 3

657 19 520 4

650 20 653 5

654 21 654 6

654 22 653 7

654 23 653 8

654 24 652 4

0 654 25 649 10 653 26 654 11 649 27 625 12 653 28 505 13 592 29 651

'14 653 30 651 15 653 31 N/A 16 652 INSTRUCTIONS On this format, list the average daily unit power level in MWe-Net for each day in the reporting month.

Compute to the nearest whole inegawatt.

I 8609100269 860714 DR ADOCK 05000245 PDR-

OPERATING DATA REPORT DOCKET NO. 50-245 DATE 860701 COMPLETED BY G. Newburgh TELEPHONE (203) 447-1791 Ext. 4400 OPERATING STATUS 1.

Unit Name: Millstone 1 Notes 2.

Reporting Period: June 1986 3.

Licensed Thermal Power (MWt): 2011 4.

Nameplate Rating (Gross MWe): 662 5.

Design Electrical Rating (Net MWe): 660 6.

Maximum Dependable Capacity (Gross MWe): 684 7.

Maximum Dependable Capacity (Net MWe): 654 8.

If Changes Occur in Capacity Ratings (Items Number 3 Through 7)

Since Last Report, Give Reasons:

N/A 9.

Power Level To Which Restricted, If Any (Net MWe): N/A 10.

Reasons For Restrictions, If Any:

N/A This Month Yr.-to-Date Cumulative 11.

Hours In Reporting Period 720 4344 136632 12.

Number Of Hours Reactor Was Critical 720 4160.4 105239.2 13.

Reactor Reserve Shutdown Hours 0

148.9 2983.4 14.

Hours Generator On-Line 720 4119 102308.2 15.

Unit Reserve Shutdown Hours 0

183.7 277.4 16.

Gross Thermal Energy Generated (MWH) 1419403 8159176 188773374 17.

Gross Elec. Energy Generated (MWH) 481700 2789600 63490896 18.

Net Electrical Energy Generated (MWH) 458740 2667560 60557332 19.

Unit Service Factor 100 94.8 74.9 20.

Unit Availability Factor 100 99.0 75.1 21.

Unit Capacity Factor (Using MDC Net) 97.4 93.9 67.8 22.

Unit Capacity Factor (Using DER Net) 96.5 93.0 67.2 l

23.

Unit Forced Outage Rate 0

0.9 12.0 24.

Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):

N/A 25.

If Shut Down At End Of Report Period, Estimated Date of Startup:

N/A 26.

Units In Test Status (Prior to Commercial Operation):

Forecast Achieved i

INITIAL CRITICALITY I

INITIAL ELECTRICITY N/A l

COMMERCIAL OPERATION l

l

DOCKET NO. 50-245 UNIT SHUTDOWNS AND POWER REDUCTIONS UNIT NAME Millstone 1 DATE 860701

~

1 COMPLETED BY G. Newburgh REPORT MONTH JUNE 1986 TELEPHONE (203) 447-1791 Ext. 4400 l

2 No.

Date Type Duration Reason Vethod of Licensee Systeg Compogent Cause & Corrective (Hours)

Shutting Event Code Code Action to 3

Down Reactor Report #

Prevent Recurrence i

4 860619 5

0 B

5 N/A N/A N/A Power reduction to repair steam leak.

5 860628 5

0 8

5 N/A N/A N/A Power reduction to 4

find and repair j

condenser tube leaks.

I i

I I

1 2

3 4

F:

Forced Reason:

Method:

Exhibit G - Instructions 1

S:

Scheduled A-Equipment Failure (Explain) 1-Manual for Preparation of Data B-Maintenance or Test 2-Manual Scram Entry Sheets for Licensee C-Refueling 3-Automatic Scram Event Report (LER) File D-Regulatory Restriction 4-Continued from (NUREG-0161)

E-Operator Training & License Examination previous month F-Administrative 5-Power Reduction 5

G-Operational Error (Explain)

(Duration = 0)

Exhibit 1 - Same Source H-Other (Explain) 6-Other (Explain) 4