ML20212L969
| ML20212L969 | |
| Person / Time | |
|---|---|
| Site: | Hatch |
| Issue date: | 10/31/1986 |
| From: | Gucwa L, Richardson J GEORGIA POWER CO. |
| To: | NRC OFFICE OF RESOURCE MANAGEMENT (ORM) |
| References | |
| 0798C, 798C, SL-1542, NUDOCS 8701290455 | |
| Download: ML20212L969 (9) | |
Text
NARRATIVE REPORT UNIT 1 October lat 0000 Unit operating at 1004 thermal power.
October 4th 0015 Reducing load for weekly turbine / valve testing.
0415 Returned to 100% power.
October lith 0038 Reducing Load for weekly turbine / valve testing.
0322 Returned to 100% power.
October'18th 0240 Reducing Load for weekly turbine / valve testing and control rod drive exercise.
0350 Returned to 100% power.
October 20th 0157 Reducing load to backwash and precoat condensate demineralizers.
0427 Returned to 100% power.
October 25th 0032 Reducing load for weekly turbine / valve testing.
0200 Returned to 100% power.
October 31st O' 20 Reducing load to remove 'A' Reactor Feed Pump from service due to high vibration of RFPT.
2400 Unit operating at reduced load of 55% electrical power due to operation with one reactor feed pump. Work in progress to repair turbine / pump coupling.
.c E-l D
5 861031 er R
K 05000321 PDR IEDM
'/ 7
T l
OPERATING DATA REPORT l
s L
DOCKET NO.
50-321 DATE 11-02 l COMPLETED BY: J. H. Richardson l
TELEPHONE (912) 367-7781 x 2360.
l OPERATING STATUS 1.
Unit Name: E.
I. Hatch Nuclear Plant Unit 1 2.
Reporting Period:
10-86 3.
Licensed Thermal Power (MWt):
2436 4.
Nameplate Rating (Gross MWe):
809.3 5.
Design Electrical Rating (Net MWe):
777.3 6.
Maximum Dependable Capacity (Gross MWe):
801.2 7.
Maximum Dependable Capacity (Net MWe):
768.0 8.
If changes occur in capacity ratings (Items Number 3 through 7) since last report, give reasons:
N/A 9.
Power level to which restricted, if any (Net MWe):
No restrictions
- 10. Reasons for restrictions, if any:
N/A This Month Yr-to-Date Cumulative
- 11. Hours In Reporting Period 745 7296 94967
- 12. Number of Hours Reactor was Critical 745.0 4188.2 66314.4
- 13. Reactor Reserve Shutdown Hours 0
0 0
- 14. Hours Generator On-Line 745.0 3878.0 62439.1
- 15. Unit Reserve Shutdown Hours 0
0 0
- 16. Gross Thermal Energy Generated (MWH) 1780497 8913851 133545341
- 17. Gross Electrical Energy Generated (MWH) 579930 2868270.
43110400
- 18. Net Electrical Energy Generated (MWH) 554935 2715587 40929675
- 19. Unit Service Factor (t) 100.0%
53.2%
65.7%
- 20. Unit Availability Factor (t) 100.0%
53.2%
65.7%
- 21. Unit Capacity Factor (t Using MDC Net) 97.0%
48.5%
57.5%
- 22. Unit Capacity Factor (t Using DER Net) 95.8%
47.9%
55.2%
- 23. Unit Forced Outage Rate 0.0%
4.2%
16.8%
- 24. Shutdowns scheduled over next 6 months (Type, Date, and Duration of Each): N/A
- 25. If shutdown at end of report period, estimated date of startup: N/A
- 26. Units in Test Status (Prior to Commercial Operation):
N/A 4
E. 9
AVERAGE DAILY UNIT POWER LEVEL e
.. DOCKET NO.
50-321
~
DATE:
11-02-86 COMPLETED BY: J. H. Richardson TELEPHONE (912) 367-7781 x'2360~
MONTH: OCTOBER 86 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)
(MWe-Net) 1 748 17 763' 2
746 18 761 3
746 19 766 4
742 20 762 5
745 21
'764 6
752 22 765 7
753 23 761 8
753 24 758 9
751 25 752 10 752 26 790 11 752 27 762 12 756 28 763 13 750 29 765 14 750 30 762 15 760 31 408 16 766 E-3
UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO.
50-321 UNIT NAME __ HATCH ONE
~
j COMPLETED BY J.
H. Richardson TELEPHONE (912) 367-7781 (2360) DATE NOVEMBER 1, 1986 REPORT MONTH OCTOBER 1986 i
R S
E Y
T A
METHOD OF LICENSEE SC Y
S SHUTTING EVENT TO CAUSE & CORRECTIVE 1
P DURATION O
DOWN REPORT ED COMPONENT ACTION TO NO.
DATE E
(HOURS)
N REACTOR NUMBER ME CODE PREVENT RECURRENCE 86-041 861004 S
4.0 D
5 N/A HA TURBIN Weekly turbine / valve test.
1 86-042 861011 S
2.73 B
5 N/A HA TURBIN Weekly turbine / valve j
test.86-043 861018 s
1.17 B
5 N/A HA TURBIN Weekly turbine / valve j
test and control rod exercise.86-044 861020 F
2.50 B
5 N/A WC DEMINX Backwash and precoat condensate j
demineralizers.
1 86-045 861025 S
1.47 B
5 N/A HA TURBIN Weekly turbine / valve j
test.
t 86-046 861031 F
23.67 A
5 N/A CH TURBIN Removed
'A' RFP from service due to high 4
1 vibration of RFPT.
F: Forced Reason:
Method:
Ever.ts reported involve S: Scheduled A-Equipment Failure (Explain) 1-Manual a greater than 20% reduction B-Maintenance or Test 2-Manual Scram in average daily power level C-Refueling 3-Automatic Scram for the preceeding 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
D-Regulatory Restriction 4-Continuations E-Operator Training & License 5-Load Reduction Examination 9-Other (Explain)
F-Administrative G-Operational Error (Explain)
H-Other (Explain)
E-4
'. +,
NARRATIVE REPORT.
UNIT 2 October lat 0000 Unit in refueling outage.
!~
0540' Core unload complete.
October 27th 0235 Began core reload.
October 31st 2400 Unit in refueling outage.
1 9
4 E-5
~..
OPERATING DATA REPORT
- ~
1 DOCKET NO.
50-366 DATE 11-02-86 COMPLETED BY: J. H. Richardson TELEPHONE (912) 367-7781 x 2360 OPERATING STATUS
- 1. Unit Name:
E.
I. Hatch Nuclear Plant Unit 2
- 2. Reporting Period:
10-86
- 3. Licensed Thermal Power (MWt):
2436
- 4. Nameplate Rating (Gross MWe):
820.0
- 5. Design Electrical Rating (Net MWe):
784.0
- 6. Maximum Dependable Capacity (Gross MWe):
803.9
- 7. Maximum Dependable Capacity (Net MWe):
777.0
.8, If changes occur in capacity ratings (Items Number 3 through 7) since last report, give reasons:
N/A
- 9. Power level to which restricted, if any (Net MWe)
No Restrictions
- 10. Reasons for restrictions, if any:
N/A This Month Yr-to-Date Cumulative
- 11. Hours In Reporting Period 745 7296 62593
- 12. Number of Hours Reactor was Critical 0
5877.9 43449.4 l
- 13. Reactor Reserve Shutdown Hours 0
0 0
- 14. Hours Generator On-Line 0
5709.4 41576.4
- 15. Unit Reserve Shutdown Hours 0
0 0
- 16. Gross Thermal Energy Generated (MWH) 0 11085658 89268864
- 17. Gross Electrical Energy Generated (MWH) 0 3545200 29326700
- 18. Net Electrical Energy Generated (MWH) 0 3362676 27901330 j
- 19. Unit Service Factor (t) 0.0%
78.3%
66.4%
i
- 20. Unit Availability Factor (%)
0.0%
78.3%
66.4%
- 21. Unit Capacity Factor (t Using MDC Net) 0.0%
59.3%
57.4%
- 22. Unit Capacity Factor (t Using DER Net) 0.0%
58.8%
56.9%
- 23. Unit Forced Outage Rate 0.0%
6.2%
9.5%
- 24. Shutdowns scheduled over next 6 months (Type, Date, and Duration of Each):
Refueling Outage-began September 18, 1986 l
- 25. If shutdown at end of report period, estimated date of startup: 11/19/86 l
- 26. Units in Test Status (Prior to Commercial Operation):
N/A j
l l
E-6
--.i
c AVERAGE DAILY UNIT POWER LEVEL a
DOCKET NO.
50-366 DATE:
11-02-86 COMPLETED BY: Jody Richardson TELEPHONE (912) 367-7781 x 2882 MONTH: OCTOBER 86 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)
(MWe-Net) 1 0
17 0
2 0
18 0
3 0
19 0
4 0
20 0
5 0
21 0
6 0
22 0
7 0
23 0
8 0
24 0
9 0
25 0
10 0
26 0
11 0
27 0
12 0
28 0
13 0
29 0
14 0
30 0
15 0
31 0
l 16 0
l l
l 1
l E-7 l
1 m
o
UNIT SHUTDOWNS ?.ND POWER REDUCTIONS DOCKET NO.
50-366 UNIT NAME HATCH 'IWO COMPLETED BY J.
H. RICHARDSON TELEPHONE (912) 367-7781 (2360) DATE NOVEMBER 01, 1986 REPORT MONTH OCTOBER 1986 R
S E
Y T
A METHOD OF LICENSEE SC Y
S SHUTTING EVENT TO CAUSE & CORRECTIVE I
P DURATION O
DOWN REPORT ED COMPONENT ACTION TO NO.
DATE E
(HOURS)
N REACTOR NUMBER ME CODE PREVENT RECURRENCE 86-070 861001 S
745 C
4 N/A RC FUELXX Refueling Outage Continues.
F: Forced Reason:
Method:
Events reported involve S: Scheduled A-Equipment Failure (Explain) 1-Manual a greater than 20% reduction B-Maintenance or Test 2-Manual Scram in average daily power level C-Refueling 3-Automatic Scram for the preceeding 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
D-Regulatory Restriction 4-Continuations E-Operator Training & License 5-Load Reduction Examination 9-Other (Explain)
F-Administrative G-Operational Error (Explain) 5-Other (Explain)
E-8
. Georgis Fbw:5 company -
333 P:edmont Avenus e
Atlanta, Georgia 30308 T lephone 404 5264526 Mailing Address:
Fbst Office Box 4545 Atfanta, Georgia 30302 Georgia Power MaIag"e7 Nuclear Safety and Licensing November 14, 1986 Nuclear Operations NRC Monthly Operating Report File: X7GJ10-H000 Log: SL-1542
- Director, Office of Management and Program Analysis U. S. Nuclear Regulatory Commission Washington, D. C.
20555
Dear Sir:
Enclosed is the Monthly Operating Report for Hatch Unit 1, Docket Number 50-321, and for Hatch Unit 2, Docket Number 50-366.
This report is submitted pursuant to Technical Specifications Section 6.9.1.10.
Sincerely, C
& fcC * =
L. T. Gucwa MJBlackwood/lc Enclosure c: Georria Power Company U. S. Nuclear Regulatory Commission Mr. i. P. O'Reilly Dr. J. N. Grace, Regional Administrator Mr. J. T. Beckham, Jr.
Mr. P. Holmes-Ray, Senior Resident Mr. H. C. Nix, Jr.
Inspector - Hatch Mr. C. Tabet Mr. G. Rivenbark, Hatch Licensing G0-NORMS Project Manager p@
0798C
\\
s
____