ML20211L421
| ML20211L421 | |
| Person / Time | |
|---|---|
| Site: | Hope Creek |
| Issue date: | 11/30/1986 |
| From: | Phillips M, Salvesen R Public Service Enterprise Group |
| To: | NRC OFFICE OF ADMINISTRATION (ADM) |
| References | |
| NUDOCS 8612160017 | |
| Download: ML20211L421 (6) | |
Text
.
HOPE CREEK GENERATING STATION MONTHLY OPERATING
SUMMARY
NOVEMBER 1986 The Hope Creek Generating Station operated continously from October 19, 1986 to Novenber 14, 1986 when the reactor scrammed on a valid high reactor pressure signal. The scram was attributed to personnel error by startup personnel in the performance of turbine control valve testing.
Following the scram the unit was placed in shutdown cooling and an unexplained failure of the B Residual Heat Eer. oval Pump occurred.
Control Room Operators observed high vibration readings and a significant increase in motor amps and subsequently removed the pump from service.
Station management decided to replace the pump with a spare unit available on-site and following maintenance and retest activities, the reactor was restarted on November 28, 1986.
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AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.90-394 UNIT Hnpa craak Can. Statio!
DATE __12/3/Rs --
COM,PLETED BY - Mika phil1ipn TELEPHONE (sao) 114-373 8 November 1986 MONTH DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)
(MWe-Net) 590 0
1 17 581 0
2 18 778 0
3 19
- - =
677 0
4 20
_ _ _ _ _ _ _ =
185 0
5 21 649 0
6 22 519 0
7 23 634 0
8 24 930 0
9
= = = _ _ = _
25 963 0
10 26 1024 0
11 27 936 0
12
_ _ _ - - _ _ _ - - - - - - =
28 998 0
13 29
____=__
352 170 14 30 0
15 31 0
16
OPERATING DATA REPORT ONIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-354
-UNIT NAME Hope Creek Gen. Station 12/03/86 DATE COMPLETED BY M. Phillips November '86 TELEPHONE (609) 339-3738 REPORT MONTH METHOD OF SHUTTING DOWN THE TYPE REACTOR OR F FORCED
- DURATION, REASON REDUCING CORRECTIVE ACTION /
NO.
DATE S SCHEDULED (HOURS)
(1)
POWER (2)
COMMENTS 18 11/14 F
330 B
3 Power Ascension test Turbine Control valve.
Extended outage on B RHR pump.
SUMMARY
OPERATING DATA REPORT l
DOCKET NO.
50-354 UNIT Hope._CInclL_Gea, Statio{
DATE 12/03/lL6 COMPLETED BY M. _EhiLLi1Lt.___
TELEPHONE
((0_A)__319_-17)_lL OPERATING STATUS 1.
REPORTING PERIOD Nov '86 GROSS HOURS IN REPORTING PERIOD
__7 2_p_ _
2.
CURRENTLY AUTHORIZED POWER LEVEL (MWt) 3_2_9_3___
MAX. DEPEND. CAPACITY (MWe-Net) 1967 DESIGN ELECTRICAL RATING (MWe-Net) l_0_6_7_,_ __
N_o_n_e_ _ _ _ _ _
3.
POWER LEVEL TO WHICH RESTRICTED (IF ANY) (MWe-Net) 4.
REASONS FOR RESTRICTION (IF ANY)
THIS YR TO MONTH DATE CUMULATIVE 5.
NO. OF HOURS REACTOR WAS CRITICAL 375_
10_6_2_
2062___
_0 6.
REACTOR RESERVE SHUTDOWN HOURS 0_
0__
_JL9_3_
10_93 7.
HOURS GENERATOR ON LINE 339_
]
8.
UNIT RESERVE SHUTDOWN HOURS 0
0_
_-0 9.
GROSS THERMAL ENERGY GENERATED (MWH) 7 88,533 1_,831,133_1JL3.Ld36
- 10. GROSS ELECTRICAL ENERGY GENERATED (MWH) 231SJJ _.fi.pl303__.191337
- 11. NET ELECTRICAL ENERGN GENERATED (MWH) 231,2JJ _471945___471S_46
- 12. REACTOR SERVICE FACTOR
- 13. REACTOR AVAILABILITY FACTOR
- 14. UNIT SERVICE FACTOR
- 15. UNIT AVAILABILITY FACTOR
- 16. UNIT CAPACITY FACTOR (Using Design MDC) 17.' UNIT CAPACITY FACTOR (Using Design MWe)
- 18. UNIT FORCED OUTAGE DATE
- 19. SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE, & DURATION) : Attached
- 20. IF SHUT DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP: NA
- 21. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION) :
FORECAST ACHIEVED INITIAL CRITICALITY
_JBJMJ 8/1/86 INITIAL ELECTRICITY COMMERCIAL OPERATION 12/ljif.35
-SCHEDULED SHUTDOWNS (ITEM 19)
TXPE Db1E DDBb11DE 1.
MSIV Isolation - Scram 12/03/86 2 days 2.
Load Rejection - Scram 12/96/86 4.5 days
O PSEG Public Service Electnc and Gas Company P.O. Box L Hancocks Bndge, New Jersey 08038 Hope Creek Operations December 3, 1986 U. S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555
Dear Sir:
MONTHLY OPERATING REPORT HOPE CREEK GENERATING STATION UNIT 1 DOCKET NO. 50-354 In compliance with Section 6.9, Reporting Requirements for the Hope Creek Technical Specifications, the operating statistics for Novenber are being forwarded to you.
Sincerely yours, jhb R.
S.
Salvesen General Manager -
Hope Creek Operations WJM:tib Distribution CC Regional Administrator USNRC Region I 631 Park Avenue King of Prussia, PA 19406 Enclosures
[bN The Energy People no n,d u 85