ML20211L421

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Monthly Operating Rept for Nov 1986
ML20211L421
Person / Time
Site: Hope Creek PSEG icon.png
Issue date: 11/30/1986
From: Phillips M, Salvesen R
Public Service Enterprise Group
To:
NRC OFFICE OF ADMINISTRATION (ADM)
References
NUDOCS 8612160017
Download: ML20211L421 (6)


Text

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HOPE CREEK GENERATING STATION MONTHLY OPERATING

SUMMARY

NOVEMBER 1986 The Hope Creek Generating Station operated continously from October 19, 1986 to Novenber 14, 1986 when the reactor scrammed on a valid high reactor pressure signal. The scram was attributed to personnel error by startup personnel in the performance of turbine control valve testing. Following the scram the unit was placed in shutdown cooling and an unexplained failure of the B Residual Heat Eer. oval Pump occurred. Control Room Operators observed high vibration readings and a significant increase in motor amps and subsequently removed the pump from service. Station management decided to replace the pump with a spare unit available on-site and following maintenance and retest activities, the reactor was restarted on November 28, 1986.

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AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.90-394 UNIT Hnpa craak Can. Statio!

DATE __12/3/Rs -- -__

COM,PLETED BY - Mika phil1ipn TELEPHONE (sao) 114-373 8 November 1986 MONTH DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net) 590 0 1 _ _ _ _ _ _ _ _ _ _ _ _____ 17 - - --_. _.

581 0 2 __ ___ 18 __

778 0 3 _ _ _ _ _ _ __- -

19 - - =

677 0 4 _ _ _ _ _ _ _ = 20 _ ___ _

185 0 5 __ __ _____ _ _ _ _ _ 21 _ _ _ _ _ _ _ _ _ _ . _ __

649 0 6 _ _ 22 519 0 7 _ 23 _. ___

634 0 8 _ . _ __ _

24 930 0 9 = = = _ _ = _ _ __ 25 __

963 0 10 _ ___ 26 ______ _ _________

1024 0 11 _ _ _ 27 ___ - - -

936 0 12 _ _ _ _ _ _ _ _

_ __ 28 _ _ _ _ - - _ _ _ - - - - - - =

998 0 13 ____=__ ___ 29 __

352 170 14 - - ___ 30 _

0 -

15 ______ _ _ _ _ _ 31 _ --______

0 16 --

OPERATING DATA REPORT ONIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-354

-UNIT NAME Hope Creek Gen. Station DATE 12/03/86 ,

COMPLETED BY M. Phillips REPORT MONTH November '86 TELEPHONE (609) 339-3738 METHOD OF SHUTTING DOWN THE TYPE REACTOR OR F FORCED DURATION, REASON REDUCING CORRECTIVE ACTION /

NO. DATE S SCHEDULED (HOURS) (1) POWER (2) COMMENTS 18 11/14 F 330 B 3 Power Ascension test Turbine Control valve.

Extended outage on B RHR pump.

SUMMARY

OPERATING DATA REPORT l

DOCKET NO. 50-354 UNIT Hope._CInclL_Gea, Statio{

DATE 12/03/lL6 COMPLETED BY M . _EhiLLi1Lt.___

TELEPHONE ((0_A)__319_-17)_lL OPERATING STATUS

1. REPORTING PERIOD Nov '86 GROSS HOURS IN REPORTING PERIOD __7 2_p_ _
2. CURRENTLY AUTHORIZED POWER LEVEL (MWt) 3_2_9_3___

MAX. DEPEND. CAPACITY (MWe-Net) 1967 DESIGN ELECTRICAL RATING (MWe-Net) l_0_6_7_,_ __

3. POWER LEVEL TO WHICH RESTRICTED (IF ANY) (MWe-Net) N_o_n_e_ _ _ _ _ _
4. REASONS FOR RESTRICTION (IF ANY)

THIS YR TO MONTH DATE CUMULATIVE

5. NO. OF HOURS REACTOR WAS CRITICAL 375_ 10_6_2_ 2062___
6. REACTOR RESERVE SHUTDOWN HOURS 0_ 0__ _ _ _

_0

7. HOURS GENERATOR ON LINE 339_ ]

_JL9_3_ 10_93

8. UNIT RESERVE SHUTDOWN HOURS 0 0_ _-0
9. GROSS THERMAL ENERGY GENERATED (MWH) 7 88,533 1_,831,133_1JL3.Ld36
10. GROSS ELECTRICAL ENERGY GENERATED (MWH) 231SJJ _.fi.pl303__.191337
11. NET ELECTRICAL ENERGN GENERATED (MWH) 231,2JJ _471945___471S_46
12. REACTOR SERVICE FACTOR _ _ . _ _ _.
13. REACTOR AVAILABILITY FACTOR _ - - -__
14. UNIT SERVICE FACTOR -
15. UNIT AVAILABILITY FACTOR _
16. UNIT CAPACITY FACTOR (Using Design MDC) -

17.' UNIT CAPACITY FACTOR (Using Design MWe) - -

18. UNIT FORCED OUTAGE DATE ____
19. SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE, & DURATION) : Attached
20. IF SHUT DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP: NA
21. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION) :

FORECAST ACHIEVED ,

INITIAL CRITICALITY _JBJMJ INITIAL ELECTRICITY 8/1/86 COMMERCIAL OPERATION 12/ljif.35 _ _____

-SCHEDULED SHUTDOWNS (ITEM 19)

TXPE Db1E DDBb11DE

1. MSIV Isolation - Scram 12/03/86 2 days
2. Load Rejection - Scram 12/96/86 4.5 days

O PSEG Public Service Electnc and Gas Company P.O. Box L Hancocks Bndge, New Jersey 08038 Hope Creek Operations December 3, 1986 U. S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555

Dear Sir:

MONTHLY OPERATING REPORT HOPE CREEK GENERATING STATION UNIT 1 DOCKET NO. 50-354 In compliance with Section 6.9, Reporting Requirements for the Hope Creek Technical Specifications, the operating statistics for Novenber are being forwarded to you.

Sincerely yours, jhb R. S. Salvesen General Manager -

Hope Creek Operations WJM:tib Distribution CC Regional Administrator USNRC Region I 631 Park Avenue King of Prussia, PA 19406 Enclosures The Energy People

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