ML20210L055
| ML20210L055 | |
| Person / Time | |
|---|---|
| Site: | Cooper |
| Issue date: | 07/31/1997 |
| From: | Ballinger P, Peckham M NEBRASKA PUBLIC POWER DISTRICT |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| NLS970153, NUDOCS 9708200202 | |
| Download: ML20210L055 (4) | |
Text
.
COOPIH NUCLt AA $7 At KjN P.o DOX 96. Browqvitt, M BRAsAA 6put it L E PtONE H0382$ 34O Nebraska Public Power District
'"***a" ers mecscznetasue:grarasse am=warz;aan_ eessausewan.waa= # m e u cenxamms NLS970153 August 14, 1997 U.
S. Nuclear Regulatory Commission Attention: Document Control Desk Washington, D.C.
20555
Subject:
Monthly Operating Status Report for July 1997, Docket No. 50-298.
Gentleme.u Enclosed for your information and use is the Cooper Nuclear Station Monthly Operating Status Report for July 1997.
In accordance with the guidance provided by Generic Letter 97-02, this report includes an Operating Data Report and Unit Shutdown Report for the month of July.
Should you have any comments, or require additional information regarding this report, please contact me.
Sincerely,
\\
l l
M.
F.
Peckham Plant Manager MFPilb Enclosures cci ANI Library R. W. Beck and Associates T.
L. Bundy J. M. Cline
/'..
A.
L. Dostal P. D. Graham R. L. Gumm INPO Records Center E. A. Lanning T,
LaPorte B. Lewis
\\
J. L. Long
\\
W. R. Mayben NRC Regional Administrator NRC Senior Resident Inspector E.
Pasche R. D. Stoddard W. Turnizttli 9708200202 970731 PDR ADOCK 05000298 R
PDR kkh
[hb 5 bh2WEYNNN hN@Nibb b
i O
s APPINDIXA Orl:RAllNG DATA REPORT DOChl'T Mh 3 4298 t'N1'l N Ah!L Cooper Nerleer Mattop liAll:
7/1497 CO%!Pl.l:ll1)IlY P 1. Itallinger 11:11.PilONE 1402)R 3 9299 1
i Reporting Periodt Jaly 1997 This Month Yr to.Date -
Cumulatne 1
Iksign 1.let trical Itatmg (Net MWe) 771t N/A N/A 1he nommal net tiectrical output of the urut specified by the utshty and used for the purpose of plant design j
2 Maumum ikpendabic Capacity (Net MWe) 764 N/A N/A l
%e gross electrical output as measured at the output termmals of the turbme-generator during the most restrictne seasonal conditions mmus the normal station senice loads 3 Number of flours the Reactor Was Critical 6R6 2 3.774 7 151,410 4 1he total number of hours durms the gross hours of the reportmg persed that the reactor was crpical 4 Number ofIlours the Generator Was On I.me 686 2 3.716 2 149.220 1
( Also called service llours) The total number of hours durmg the gross hours of the reporting perkW that the unit operated with the breakers closed to the statum bus ne sum of the hours the generator was on hne plus the total outage hours should equal the gross hours in the reporting period
$ (Lit Rescr ee Shutdown llourn 00 00 00 The total number of hours durms the proas hours of the reportmg pertod that the unit was remosed from service lor economic or similar reasons but was a tailable for operation 6 Net I:lectrical I.ncrgy (h!Wll) 5 t 5.233 0 2.147,272 0 98 312.299 0 The gross electncal output of the umt measured at the output terminals of the turbme-generator micus the normal station service h> ads durmg the gross hours of the reportmg permd, espressed in mega-watt hours Negatn e quanuties should not be used s/1/91 12:4 s r'M V
~
Y-
~
APPENDIX B UNIT SHUTDOHWS DOCKET.W.
N UNIT NAME Ceeper Nedrar Menese DATE 7eltT COMPLETED BY P. L Banager TELEPHONE ade2 325-5295 REPORT MONTH Juiv1997 Type Meehedofsaattwa cat 5EUMtRECTul ACMS g
g
{,,
F: EORCED Dews Reacter (2)
N S: MEFIM11D 97-82 7/29.97 F
Ferred
$7.2 A
2 Plant sheedewe der to failure ofToros se Drywee varmass brember ** suret weigence erseseg. IIepair of vmI=e in is progress.
$t'M4L%RY:
As the result ofa vacuum breaker failure during surveillance testing, a pomcr reductxm and plant shutdowm was initiated on July 29. 1997 to investigate and repair the forus to Drywell vacuum breakers. The shutdown wnhn=J through this reputmg penod.
(I) Remese:
A-F,
_: Feihrer(Emplais)
E..
we er Test C. nessehes D',--
y Restricties E-(W TreieingUcesse Ex:
F-Adseiesserserve G-(W Error (Esplein)
H -Oster(Empimie)
(2) Meched-I - Meneet 2 - Moment Tripirrea 3 - Aweseemeic Trip /% crete d - C_.
5-Oeber(Emploie) 8/7/97 1:33 PM
e
/
- l AT1ACllMENT 3 LIST OF NRC CONMITMENTS j
e 6 Correspondence Not NLS970153 The fo$1owing table identifies those actions conmutted to by the District in this document. Any other actions discus sed in the submittal represent intended or planned actions by the District.
They are described to the NRC for the NRC's information and are not regulatory commitments.
Please notify the Licensing Manager at Cooper Nuclect Station of any questions regarding this document or any associated regulatory commitments.
COMMITTED DATE COMMITMENT OR OUTAGE None u
l PROCEDURE NUMBER O.42 l
REVISION NUMBER 4 l
PAGE 8 OF 9 l
_~