ML20210C424

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Responds to NRC Re Violations Noted in Insp Rept 50-482/85-37.Corrective Actions:Checklist Ckl EG-120 Revised to Indicate Four Valves Locked Closed & Affected Valves Added to Procedure A0M 02-102 to Ensure Proper Positioning
ML20210C424
Person / Time
Site: Wolf Creek 
Issue date: 01/31/1986
From: Koester G
KANSAS GAS & ELECTRIC CO.
To: Johnson E
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML20210C405 List:
References
KMLNRC-86-019, KMLNRC-86-19, NUDOCS 8603260024
Download: ML20210C424 (2)


Text

F-1 KANSAS GAS AND ELECTRIC COMPANY THE ELECTAC COhM2ANY SLENN L.

MOESTER b ett persetset - seucLEAe January 31, 1986 Mr. E.H. Johnson, Acting Director

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>'h3 Division of Reactor Safety and Projects 1 I

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U.S. Nuclear Regulatory Commission

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'I Region IV bO

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611 Ryan Plaza Drive, Suite 1000 d.,J

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Arlington, TX 76011

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KMLNRC 86-019 Re:

Docket No. STN 50-482 Subj :

Response.to Inspection Report STN 50-482/85-37

Dear Mr. Johnaon:

This letter is written in response to your letter of January 2, ~1986, which transmitted Inspection Report STN 50-482/85-37. As requested, the violation (50-482/8537-01) identified in the Inspection Report is being addressed in four parts.

(a) The reason for the violation if admitted; (b) The corrective steps which have been taken and the results achieved; (c) Corrective steps which will be taken to avoid further violations; and (d) The date when full compliance will be achieved.

N J$

1.

Violation (50-482/8537-01): Nonseismic Glass Level Gauge Not Isolated Fi8' oo Finding:

on CD J 10 CFR Part 50, Appendix B, Criterion V states, in part, " Activities nu affecting quality shall be prescribed by documented instructions,

@O procedures, or drawings of a type appropriate to the circumstances..."

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N The Checklist (CKL) EG-120, Revision 5,

" Component Cooling Water System Valve, Switch, and Breake-Lineup," has been established in accordance CD O C with 10 CFR Part 50, Appendix B, Criterion V.

Contrary to the above, CKL EG-120 was inappropriate to the circumstances in that Valves EG-V 160,

161, 171, and 172 were opened in accordance with Checklist A of-CKL'EG-120 when the valves should have been closed due to the level gauge between the valves being nonseismic.

201 N. Market - Wicluta, Kansas - Mail Address: PO. Box 208 I Wichita, Kansas 67201 - Telephone: Area Code (316) 261-6451

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i Mr. E.H. Johnson KMLNRC 86-019 Page 2 January'31, 1986 Reason For Violation If Admitted:-

This personnel error occurred because the need to isolate ' nonseismic level gauges was not recognized in the procedure preparation / review process.

Corrective Steps Which Have Been Taken And Results Achieved:

L Checklist CKL EG-120 has been revised to show.the four valves ' locked closed.

A review of all safety-related tanks was conducted to identify -similar nonseismic level gauges. Five additional tanks'were identified:

Containment Spray Additive Tank (valves'were closed but not locked)

Emergency Fuel Oil Day Tank A Emergency Fuel Oil Day Tank B Jacket Cooling Water Expansion Tank A Jacket Cooling Water Expansion Tank B The appropriate checklists have been revised to require the level gauge isolation valves locked closed.

All affected valves have been locked closed.

Each has been added to procedure ADM 02-102, Control of Locked Component Status, to ensure proper positioning.

Corrective Steps Which Will Be Taken To Avoid Further Violations:

Corrective actions discussed - above provide adequate assurance that further violations will be avoided.

Date When Full Compliance Will Be Achived:

Full Compliance has been achieved.

Very truly yours, Glenn L. Koester

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Vice President - Nuclear i

GLK:see cc: P0"Connor (2)

JCummins JTaylor m

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