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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20211C7951997-09-18018 September 1997 Ro:On 970916,reactor Staff Discovered That Intrusion Alarm Sys Was Not Tested for Operability During First Calendar Wk of Sept.Caused by Other Members Being on Leave or Alternate Duty.All Sys Tests Were Properly Documented ML20096C5351996-01-11011 January 1996 Ro:On 960104,Shim-2 Control Rod Stopped at 917 Units. Operator Went Out on Reactor Bridge to Check Rod.After Examining Rod,Operator Shook Barrel & Rod Fell Into Core. Reactor Remains in Shutdown Condition ML20082P0161991-09-0303 September 1991 Ro:On 910830 Analog scram-capable Safety Channel of Dow Triga Research Reactor Found to Be Not Operating During power-up Operation of Reactor.Caused by Broken Connection in high-voltage Cable for Neutron Detector.Broken Cable Fixed ML20082N6131991-08-30030 August 1991 RO:analog-capable Safety Channel of Reactor Inoperable During Reactor Operation.Caused by Broken Connection in High Voltage Cable for Neutron Detector.Reactor Shutdown & Secured ML20210B2751987-03-18018 March 1987 Ro:Holes Found in Aluminum Reactor Tank Line.Cause Unknown. Operations Suspended Until Extent of Problem & Solution Determined.Proposed Actions to Correct Problem Will Be Submitted Prior to Resuming Operations 1997-09-18
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20202E9081998-12-31031 December 1998 Geological Survey Triga Reactor Annual Rept for Period Jan- Dec 1998. with ML20206K7031998-12-31031 December 1998 Revised Us Geological Survey Triga Reactor Annual Rept,Jan- Dec 1998 ML20217A2151998-04-15015 April 1998 Safety Evaluation Supporting Amend 9 to License R-113 ML20216H7811998-03-16016 March 1998 Safety Evaluation Supporting Amend 8 to License R-113 ML20202H1471997-12-31031 December 1997 USGS Triga Reactor Annual Rept for Jan-Dec 1997 ML20247F8221997-12-31031 December 1997 Corrected Pages for 1997 Annual Rept of USGS Survey Triga Reactor Facility, Originally Submitted on 980202,IAW License Conditions ML20211C7951997-09-18018 September 1997 Ro:On 970916,reactor Staff Discovered That Intrusion Alarm Sys Was Not Tested for Operability During First Calendar Wk of Sept.Caused by Other Members Being on Leave or Alternate Duty.All Sys Tests Were Properly Documented ML20096C5351996-01-11011 January 1996 Ro:On 960104,Shim-2 Control Rod Stopped at 917 Units. Operator Went Out on Reactor Bridge to Check Rod.After Examining Rod,Operator Shook Barrel & Rod Fell Into Core. Reactor Remains in Shutdown Condition ML20096G1881995-12-31031 December 1995 USGS Triga Reactor Annual Rept for Jan-Dec 1995 ML20078A6451994-12-31031 December 1994 USGS Triga Reactor Annual Rept for 1994 ML20063C6501993-12-31031 December 1993 USGS Survey Triga Reactor Annual Rept for Jan-Dec 1993. W/ ML20127N4481992-12-31031 December 1992 USGS Triga Reactor Annual Rept for Jan-Dec 1992 ML20087F3971991-12-31031 December 1991 Us Geological Survey Triga Reactor Annual Rept 910101-1231 ML20082P0161991-09-0303 September 1991 Ro:On 910830 Analog scram-capable Safety Channel of Dow Triga Research Reactor Found to Be Not Operating During power-up Operation of Reactor.Caused by Broken Connection in high-voltage Cable for Neutron Detector.Broken Cable Fixed ML20082N6131991-08-30030 August 1991 RO:analog-capable Safety Channel of Reactor Inoperable During Reactor Operation.Caused by Broken Connection in High Voltage Cable for Neutron Detector.Reactor Shutdown & Secured ML20066K5821990-12-31031 December 1990 Corrected Annual Rept of USGS Triga Reactor Facility 1990 ML20066H8881990-12-31031 December 1990 Annual Rept of USGS Triga Reactor Facility 1990 ML20006A5611989-12-31031 December 1989 USGS Triga Reactor Annual Rept 1989. W/900118 Ltr ML20246F6621989-04-30030 April 1989 Reactor Operator Requalification Program,Usgs Triga Reactor ML20149E5581988-01-0404 January 1988 Safety Evaluation Supporting Amend 4 to License R-113 ML20150A7641987-12-31031 December 1987 USGS Triga Reactor Annual Rept,1987 ML20210B2751987-03-18018 March 1987 Ro:Holes Found in Aluminum Reactor Tank Line.Cause Unknown. Operations Suspended Until Extent of Problem & Solution Determined.Proposed Actions to Correct Problem Will Be Submitted Prior to Resuming Operations ML20210E4261986-12-31031 December 1986 USGS Triga Reactor Annual Rept for 1986 ML20137P4431985-12-31031 December 1985 Us Geological Survey Triga Reactor Annual Rept,1985 ML20079P6951983-12-31031 December 1983 Annual Operating Rept for 1983 ML20028G0771982-12-31031 December 1982 Annual Rept 1982. ML20040F5761981-12-31031 December 1981 Annual Rept 1981. ML20003A4871980-12-31031 December 1980 Annual Rept,Jan-Dec 1980. ML19296B3521979-12-31031 December 1979 Annual Operating Rept 1979 ML19250A8001979-10-10010 October 1979 Ro:On 791009,power Signal Was Lost About 60-s After Reactor Reached 1 MW Power Level.Reactor Immediately Shut Down. Caused by Moisture Shorting Signal Line Whose Coaxial Connector Was Lying in Water Near Reactor Tank ML19256A8441978-12-31031 December 1978 1978 Annual Rept for Triga Reactor.Prime Function Was to Provide Neutrons for Various Research Programs.Irradiations Were Also Done for Other Govt Agencies 1998-04-15
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- United States Department of the Interior
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VEY GEOL OGICAl. St *p24 llOX 25016 .\l.5 i i 41 1 I)ENVER FEI)ERAl. CENTER l
I)ENVER, Col.ORAI)O 80223 n.m....... March 18, 1987 !
Reactor License:R-113 Docket No. 50-274 Administrator ,oc l U.S. Nuclear Regulatory Commission Region IV .
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. 611 Ryan Plaza Drive Suite 1000 iij l MAR 231981 j Arlingto'n, Texas 76011 4:
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Dear Sir:
i This letter is to notify you that we have found some holes in the aluminum l reactor tank liner that have penetrated the k" aluminum liner. Our reactor 4
is a TRIGA Mark I with the tank below ground level. The tank is surrounded j with four feet of concrete.
We have not been able to determine a leak rate. Annual water loss due to evaporation and possible leakage has not shown a trend. Our loss rate has l been approximately 4000 gallons per year. Over the past six years, the maximum difference between the lowest and highest usage is about 500 gallons, j but there is no trend shown. The variations each year are cyclical. :
4 l The radiation levels in the reactor water are low. The most recent analyses
{ show a gross < concentration of 4.4 X 10-9 pC1/ml, and a gross ( concentration 1 of 4.8 X 10-8 pCi/ml. H3 concentrations have had a stable history of abouc l 9 X 10-5 pCi/ml. '
We do not believe there is an immediate safety problem. We have suspended !
l routine operations while we seek to determine the extent of the problem
! and a feasible solution. We will conduct cperations that are needed to satisfy surveillance requirements of our Tech Specs.
i
- We will notify you of actions we propose to take to correct the problem
! prior to resuming routine operations.
4 This matter was discussed by telephone with Mr. Ron Baer of Region IV, and
] Mr. Bob Carter of NRR on March 18, 1987. ,
! Sincerely, l ok D 5 4 Qk(( 0 Donald H. Rusling '
i Reactor Supervisor F
l cc: Document Control Desk (2)
- Mr. Robert Carter
- l Standardization and Special Projects Directorate
! Division of PWR Licensing - B I .
Office of Nuclear Reactor Regulation
! 614G b ,
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