ML20207G396

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Discusses Insp Rept 50-395/88-13 on 880501-31 & Forwards Notice of Violation.Addition of Flush Connections on Lines Subj to Bifouling Encouraged
ML20207G396
Person / Time
Site: Summer South Carolina Electric & Gas Company icon.png
Issue date: 08/17/1988
From: Grace J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To: Bradham O
SOUTH CAROLINA ELECTRIC & GAS CO.
Shared Package
ML20207G403 List:
References
EA-88-151, NUDOCS 8808240110
Download: ML20207G396 (3)


See also: IR 05000395/1988013

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AUG 17 $88

Docket No. 50-395

License No. NPF-12

EA 88-151

South Carolina Electric and Gas Company

ATTN: Mr. O. S. Bradham, Vice President

Nuclear Operations

Post Office Box 88

Jenkinsville, South Carolina 29065

Gentlemen:

SUBJECT: NOTICE OF VIOLATION

(NRC INSPECTION REPORT NO. 50-395/88-13)

This refers to the Nuclear Regulatory Comission (NRC) inspection conducted at

the V. C. Sumer Plant on May 1 - 31, 1988.

The inspection included a review

of the circumstance associated with the degraded service water flow to the

reactor building cooling units following a reactor trip on May 12, 1988.

The

report documenting this inspection was sent to you by letter dated June 16,

1988. As a result of this inspection, a significant failure to comply with

regulatory requirements was identified, and accordingly, NRC concerns relative

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to the inspection findings were discussed in an Enforcement Conference held on

June 24, 1988.

The letter summarizing this Conference was sent to you on

July 22, 1988.

The violation described in the enclosed Notice of Violation (Notice) involved a

failure by your operations staff to identify degraded service water flow to the

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reactor building cooling units (RBCUs).

This problem should have been identified

from a post trip review of plant performance data available to the operations

staff following the reactor trip of May 12, 1988.

However, because of- the

inadequate post trip review performed, this problem was not promptly identified

and the reactor was subsequently restarted on May 12, 1988, with the degraded

service water flow to the RBCUs.

On May 16, 1988, the Independent Safety Evaluation Group conducted an

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independent review of the reactor trip data package and subsequently identified

the degraded service water flow problem.

Consequently, imediate corrective

action was initiated.

Nevertheless, the. reactor was operated fu approximately

90 hours0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br /> without the operations staff being aware that service water flow to

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the RBCUs was degraded. A more thorough initial review of the operational data

should have led to the determination thet service water flew was less than

required.

The performance data was available, but it is evident that the

repetitive columnar format of the data package contributed to the degraded

service water flow data being ovar' coked dumtig the initial review.

Your staff

has shown initiative addressin

  1. ta fc N t prob'em by adding gra hics

enhancement to the existing pr

3ther .oitcern nade evident as a result

of this event is the approact

. tons staff to the control room

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annunciators immediately following the reactor trip.

The trip caused over

85 annunciators to activate and two of those annunciators should have indicated

possible problems with service water.

It is apparent that as the operations

staff were clearing the annunciators, they were not alert for problem indica-

tions and were routinely resetting systems which resulted in a missed oppor-

tunity to detect the service water degradation problem.

Management should

address the issue of the operations staff being sensitive to system indicators

and ensure that before any system configuration change or event termination that

they are fully aware of plant conditions.

The NRC has emphasized reviewing reactor trip packages and surveillance data to

assure that components actuate properly and function within the required

parameters.

Furthermore, degraded flow of critical safety systems due to clams,

corbicula, or microbiological induced corrosion has also been the subject of

NRC bulletins and notices transmitted to power reactor licensees.

The NRC is encouraged by your consideration of the possibility of cdding flush

connections on those lines subject to biofouling.

The capability of periodically

flushing lines would expand your biofouling protection measures, especially in

light of your known susceptibility to that problem because of service water

pond clam infestation.

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In accordance with the "General Statement of Policy and Procedure for NRC

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Enforcement Actions," 10 CFR Part 2. Appendix C (1988), the violation described

in the enclosed Notice has been classified as a Severity t.evel !!! violation.

Normally, a civil penalty is considered for a Severity Level III violation.

However, after consultation with the Director. Office of Enforcement, and the

Deputy Executive Director for Regional Operations, I have decided that a civil

penalty will not be proposed in this case because of your actions, particularly

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with regard to improving your post-trip review.

Also, considered were the

actions of your independent review group which identified the problem although

it was missed during the initial post-trip review.

Finally, your prompt

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corrective action and good past performance, along with an increasingly

aggressive approach toward problem identification and resolution contributed

to no civil penalty being issued in this matter.

You are required to respond to this letter and the enclosed Notice and should

follow the instructions specified therein when preparing your response,

in

your response, you should document the specific actions taken and any additional

actions you plan to prevent recurrence.

Your response should describe those

particular actions taken or planned to improve the effectiveness of your

management control program.

After reviewing your response to this Notice,

including your proposed corrective actions and the results of future

inspections, the NRC will determine whether further NRC enforcement action

is necessary to ensure compliance with NRC regulatory requirements.

In accordance with Section 2.790 of the NRC's "Rules of Practice," Part 2,

Title 10. Code of Federal Regulations, a copy of this letter and its enclosure

will be placed in the NRC Public Document Room,

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South Carolina Electric

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The responses directed by this letter and its enclosure are not subject to the

clearance procedures of the Office of Management and Budget as required by the

Paperwork Reduction Act of 1980, Pub. L. No.96-511.

Should you have any questions concerning this letter, please contact us.

Sincerely,

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J. Nelson Grace

Regional Administrator

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Enclosure:

Notice of Violation

cc w/ enc 1:

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J. L. Skolds, General Manager

Nuclear Plant Operations

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J. B. Knotts, Jr.

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Bishop. Cook, Purcell & Reynolds

W. A. Williams, Jr., Technical

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Assistant, Nuclear Operations -

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Santee Cooper

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A. R. Koon, Jr. , Manager

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Nuclear Licensing

R. E. Rainear Executive Vice President,

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South Carolina Public Service Authority

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