ML20206P186

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Insp Repts 50-313/87-08 & 50-368/87-08 in Mar 1987.Violation Noted:Failure to Maintain Unit 2 Configuration Control of Seismic Class I Pipe Support & to Have Adequate Procedures
ML20206P186
Person / Time
Site: Arkansas Nuclear  
Issue date: 04/14/1987
From: Craig Harbuck, Hunter D, Johnson W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20206P159 List:
References
50-313-87-08, 50-313-87-8, 50-368-87-08, 50-368-87-8, NUDOCS 8704210118
Download: ML20206P186 (8)


See also: IR 05000313/1987008

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APPENDIX B

U. S. NUCLEAR REGULATORY COMMISSION

REGION IV

Inspection Report:

50-313/87-08

Licenses: DPR-51

50-368/87-08

NPF-6

Dockets: 50-313

50-368

Licensee:

Arkansas Power & Light Company

P. O. Box 551

Little Rock, Arkansas 72203

Facility Name:

Arkansas Nuclear One (AN0), Units 1 and 2

Inspection At:

AN0 Site, Russellville, Arkansas

Inspection Conducted:

March 1-31, 1987

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Inspectors:

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S~enior Resident Reactor

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R~. Hunter, Chief, Reactor

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Project Section B, Reactor Projects

Branch

8704210118 870415

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Inspection Summary '

' Inspection Conducted March 1-31, 1987 (Report 50-313/87-08).

Areas Inspected: Routine, unannounced inspection including operational' safety

verification, maintenance, surveillance, and the emergency operating

procedure.

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Results: Within the four areas inspected, no violations or deviations were

identified.

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-Inspection Conducted March 1-31, 1987 (Report 50-368/87-08)

Areas Inspected:

Routine, unannounced inspection of operational safety

- verification, maintenance, and surveillance.

Results: Within'the three areasLinspected, two violations were identified

(failure to maintain configuration control of a seismic class.I pipe support,

paragraph 2.B.8, and failure to have adequate procedures, paragraph 2.A.3).

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DETAILS

1.

Persons Contacted

J. Levine, Executive Director of Site Nuclear Operations

R. Ashcraft, Electrical Maintenance Supervisor

  • B. Baker, Operations Manager

D. Bennett, Mechanical Engineer

A. Cox, Unit 1 Operations Superintendent

  • E. Ewing, General Manager Technical Support

B. Garrison, Operations Technical Support

L. Gulick, Unit 2 Operations Superintendent

H. Hollis, Security Superintendent

  • D. Howard, Special Projects Manager
  • D. Lomax, Licensing Supervisor

B. McCord, Quality Control Inspection Supervisor

  • J. McWilliams, Maintenance Manager

J. Merryfield, Mechanical Maintenance Supervisor

P. Michalk, Licensing Engineer

G. Parks, Senior QC Inspector

V. Pettus, Mechanical Maintenance Superintendent

  • S. Quennoz, General Manager, Plant Operations

C. Taylor, Operations Technical Support Supervisor

G. Wrightam, I&C Supervisor

  • Present at exit interview.

The NRC inspectors also contacted other plant personnel, including operators,

technicians, and administrative personnel.

2.

Operational Safety Verification (Units 1 and 2)

The NRC inspectors observed control room operations, reviewed applicable

logs, and conducted discussions with control room operators.

The NRC

inspectors verified the operability'of selected emergency systems,

reviewed tagout records, and' verified proper return to service of affected

components, and ensured that maintenance requests had been initiated for

equipment'in need of maintenance.

The NRC inspectors made spot checks to

verify-that the physical security plan was being implemented in accordance

with the station security plan.

The NRC inspectors verified

. implementation of radiation protection controls during observation of

plant activities.

The NRC inspectors toured accessible areas of the units to observe plant

equipment conditions, including potential fire hazards, fluid leaks, and

excessive vibration.

The NRC inspectors also observed plant housekeeping

and cleanliness conditions, and verified implementation of radiation

protection controls during the tours.

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. System Walkdown

The NRC inspectors walked'down the accessible portions of the Unit 2-.

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emergency feedwater system using Procedure 2106.06-and Drawing M-2204 and

verified operability of the system. Several items were noted during the

walkdown.

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(1) Two valves, 2CV-1036-2 and.2CT-41 were noted to have minor packing

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leaks. The licensee initiated action to correct these.

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(2) Backleakage from the "A" steam generator through Valve 2EFW-7A piping

pentration room noted during a previous inspection conducted in the

present cycle, was noted to still be occurring. -As found before,.

there did not appear to be any adverse effect on the system

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operation.

(3) On March 19, 1987, the NRC inspector found that Valve 2EFW-17 did not-

have a lock as specified by Procedure.2106.06. Operations was

infonned and a lock was placed on the valve.- The valve position had

been correct (open). Subsequent' investigation by the licensee

revealed that most likely the lock had been-placed on the valve

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during the lineup performed at the end of the last' refueling outage

' n September'1986, but had been removed during the unscheduled outage

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following the reactor trip in November 1986, when Procedure 2106.08,

" Steam Generator Secondary Fill Drain _ and Wet Layup," was used..

- Step 12.5 of this procedure only required ~2EFW-17 to be open 'but not

locked in the restoration valve lineup.

In that these two procedures

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are inconsistent regarding the_ locking of Valve 2EFW-17, they are

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inadcquate to properly control:its locked status. This is an

apparent violation.

(368/8708-02).

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b.

Observations and Concerns

The NRC. inspector made tne following observations and discussed each

with the licensee:

L(1) The main feedwater isolation valve in the north corner of the

upper north piping penetration room has had a steady inner

packing steam' leak during the present cycle,' which discharges to

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a floor drain via a ~ small tube. The result is that this area is

unusually. hot and humid. A concern was expressed to the

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licensee that during the hot summer-months there may be a

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possibility of adversely affecting safety-related equipment in

that area such as the EFW header isolation valves. Similarly,

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the added. heat from the EFW header pipe in the upper south

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piping penetration room due to the check valve backleakage, as

noted above, might also adversely affect safety-related valves

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nearby. The licensee plans to perform an evaluation of these

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concerns.

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$(2) The'NRC insp'ector noted that the excore' neutron flux indication-

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drawers on Panel 2C336iin the Unit 2 control room were not

secured.in that the screw fasteners were-loose._. Subsequently,

it was learned that most of the screws cannot be fastened

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properly. When notified, the_ licensee issued a job request to-

correct this deficiency. ~ The?NRC inspector later observed that

a similar problem also existed _with drawers.in the control-

element a'sembly drive mechanism. cabinets.

Having already

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. identified this,: license representatives stated their intent to

correct.these deficiencies during-scheduled outages,- but.they

had not yet developed a specific plan for doing so.

(3) The doors in the.back of control' panels in both control rooms

were frequently observed to-be partly open.

'(4) ~ The:NRC inspector noted that the' pump data trend book in Unit 2

was' missing the January 1987-data for 2P78 flow and differential

pressure.

This was promptly corrected by the licensee.

The

Unit I trend book also had missing data,_but this had already

-been identified and was being corrected.

(5) The NRC inspector found Unit 1 Fire Doors 51 and 57 ajar.on

March 17.

However, these doors were not required to be closed-

by_ Unit _1 Technical Specifications. On March 18, Fire Door 265

in Unit 2 was found ajar.

Security records.-showed it had been

that way for approximately 19 minutes.

It appeared that

security would probably have responded to the alarm within the

hour allotted by their procedure. The NRC inspector stated a

concern that some licensee personnel were apparently not

verifying fire doors closed after going through them.

(6) A large can of what appeared to be oil or cleaning solution and

an aerosol spray can were found sitting on the cover plate of

the Unit 2 "B" spray pump suction check valve.

Plant operations

was informed and the cans were removed.

(7) The flexible conduit to the low pressure safety injection

pump (2P60A) recirculation isolation motor operated control

valve (2CV-5123-1) was observed to be disconnected from the

limit switch cover fitting, exposing the cables inside.

This

problem was promptly corrected after the licensee was informed.

(8) A nut was observed to be missing from an anchor bolt on Seismic

Pipe Hanger 2HCB-15-H11.

This hanger supported the 20 inch pipe

supplying the suction of the Unit 2 "A"

train containment spray

(2P35A) and low pressure injection (2P60A) pumps from the

containment sump.

This was pipe also integral to the piping from

the refueling water storage tank which supplies these same pumps

and the high pressure safety injection pump (2P89A).

Failure to

maintain this support in the configuration depicted in the

design drawing (Hanger Sketch 2HCB-15-H11, Revision 3, as-built

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verified on' January 18,'1982) is an apparent violation (368/8708-01).

The licensee was informed and promptly replaced the missing nut.

Subsequent engineering inspection identified additional problems

with this pipe. hanger:

Nearlylall the anchor bolts had no washers (washers were

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subsequently installed).

One anchor was closer to an adjacent support base plate

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anchor than allowed by the construction

specification (C-2305).

The licensee issued engineering

action request (EAR)87-208 to address the effect-of these

deficiencies on the operability of the pipe hanger.

The NRC inspector noted that operability evaluations of similar

deficiencies dating back to NRC Open Item 368/8622-01 had still

not been completed.

The NRC inspector stated his concern that

long delays in completing such evaluations could result in the

identification of an unacceptable condition long-after the event

was initially noted.

These reviews and observations were conducted to verify that facility

operations were in conformance with the requirements established under

Technical Specifications, 10 CFR, and administrative procedures.

3.

Monthly Maintenance Observation (Units 1 and 2)

Station maintenance activities of safety related systems and components

listed below were observed / reviewed to ascertain that they were conducted

in accordance with approved procedures, Regulatory Guides, and industry

codes or standards; and in conformance with Technical Specifications.

The following items were considered during this review:

the limiting

conditions for operation were met while components or systems were removed

from service; approvals were obtained prior to initiating the work;

activities were accomplished using approved procedures and were inspected

as applicable; functional testing and/or calibrations were performed prior

to returning components or systems to service; quality control records

were maintained; activities were accomplished by qualified personnel;

parts and materials used were properly certified; radiological controls

were implemented; and fire prevention controls were implemented.

Work requests were reviewed to determine status of outstanding jobs and to

ensure that priority is assigned to safety-related equipment maintenance

which may affect system performance.

Portions of the following maintenance activities were observed:

Adjustment to discharge flow indication FI-2400 for Spray Pump 2P358

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(Priority 1 Job Order 730451, Procedure 1304.01)

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Process monitor system calibration using Xe-133 for the main

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condenser offgas monitor (Job Order 729753, Procedure 2304.27)

Corrective maintenance on EFIC channel "B" LI 2673 (train-2 of "B"

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steam generator wide range level indication) (Job Order 731068,

Procedure 1304.99)

Removal of the Unit 2 "B" service water pump, 2P48, initial

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uncoupling (Job Order 729900, Procedure 2402.34)

Troubleshooting and adjustment of Letdown Flow Control

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. Valve'2CV-4816..(Job Order 730862, Procedure 2304.119)

Ultrasound inspection of degraded joint in jacket cooling water line

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for Diesel Generator 2K4B (Job Order 731349)

Troubleshooting of. Unit 2 reactor Trip Circuit Breaker TCB-7

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(Priority 1 Job. Order 3001)

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Verification of_ closing circuit for TCB-7 (Job Order 731485,

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' Procedure 2408.031)

Reassembly of service Water Pump 2P48 (Job Order 729900,

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Procedure 2402.34)

No violations or deviations were identified.

4.

Monthly Surveillance Observation (Units 1 and 2)

The NRC inspector observed the Technical Specification required

surveillance testing on Low Pressure Safety Injection Pump 2P60A

(Procedure 2104.40, Supplement 1) and verified that testing was performed

in accordance with adequate procedures, that test instrumentation was

calibrated, that limiting conditions for operation were met, that removal

and restoration of the affected components were accomplished, that test

results conformed with Technical Specifications and procedure

requirements, that test results were reviewed by personnel other than the

individual directing the test, and that any deficiencies identified during

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the testing were properly reviewed and resolved by appropriate management

personnel.

The NRC inspector also witnessed portions of the following test

activities:

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_ Core protection calculator channel "A" test (Procedure 2312.02,

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JO 729765)

Excore channel "B" monthly test (Procedure 2304.101, J0 730155)

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Area radiation monitor calibration check for the Unit 1, 317 ft.

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elevation area (Procedure 1304.95, JO 730695)

No violations or deviations were identified.

5.

Emergency Operating Procedure Review (Unit 1)

The-NRC inspector determined that the Procedures Generation Package (PGP)

-submitted in 1983 had not yet been completely approved by the NRC Office

of Nuclear Reactor Regulation.

The NRC inspector's' review of the E0P, which primarily consisted of verifying

that it met the commitments made in the PGP was continued, but was not yet

completed.

The review will be continued in a future inspection.

No violations or deviations were identified.

6.

Exit Interview

The NRC resident inspector met with Mr. S. M. Quennoz, General Manager,

Plant Operations, and other members of the AP&L staff at the end of-

inspection. At this meeting, the NRC inspector summarized the scope of the

inspection and the findings.

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