ML20205J880

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Safety Insp Repts 50-456/86-65 & 50-457/86-49 on 861201- 870214.Violation Noted:Failure Re Reportability of ESF & Reactor Protection Sys Actuations
ML20205J880
Person / Time
Site: Braidwood  Constellation icon.png
Issue date: 03/23/1987
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20205J791 List:
References
50-456-86-65, 50-457-86-49, NUDOCS 8704010443
Download: ML20205J880 (33)


See also: IR 05000456/1986065

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U.S. NUCLEAR REGULATORY COMMISSION

REGION III

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Report No. 50-456/86065(DRP);50-457/86049(DRP)

Docket Nos. 50-456; 50-457

License Nos. NPF-59; CPPR-133

Licensee:

Commonwealth Edison Company

Post Office Box 767

Chicago, IL 60690

Facility Name: Braidwood Station, Units 1 and 2

Inspection At: Braidwood Site, Braidwood, Illinois

Inspection Conducted: December 1, 1986 through February 14, 1987

Inspectors:

NRC

T. M. Tongue

W. J. Kropp

T. E. Taylor

EG&G Idaho, Inc.

B. Barnes

Approved By:

W. S. Little, Director

Braidwood Project

Date

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Inspection Summary

Inspection on December 1, 1986 through February 14, 1987 (Report No.

50-456/86065(DRP); 50-457/86049(DRP))

Areas Inspected:

Routine, unannounced safety inspection of activities with

regard to licensee action on previously identified items; allegations;

regional recuesti licensee event reports; operational safety; Unit 2 tour

which incluced construction activities in the areas of welds, electrical,

and mechanical; report review; and meetings, training, and other activities.

Results: Of the eight areas inspected, no violations were found in seven

areas, one violation was identified concerning reportability of ESF and RPS

actuations (Paragraph 4).

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DETAILS

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1.

Persons Contacted

Comonwealth Edison Company (CECO)

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Corporate Personnel

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B. Thomas, Executive Vice President

C. Reed, Vice President, Nuclear Operations

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T. J. Maiman, Vice President, Projects

D. Galle, Assistant Vice President and General Manager

K. Graesser, Division Vice President

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D. J. Scott, Operations Manager, NSD

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D. Farrar. Director, Nuclear Licensing

W. Shewski, Quality Assurance Manager

B. M. Saunders, Nuclear Security Administrator

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  • S. C. Hunsader, Nuclear Licensing Administrator

Braidwood Personnel

  • M. J. Wallace, Project Manager
  • E. E. Fitzpatrick.. Station Manager
  • C. W. Schroeder, Station Services Superintendent
  • K. L. Kofron, Production Superintendent
  • D. L. Shamblin, Assistant Project Manager
  • M.' E. Lohmann, Project Startup Superintendent
  • W. E. Vahle, Project Construction Superintendent

C. J. Tomashek, Project Startup Superintendent

G. E. Groth, Project Field Engineering Manager

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  • D. E. O'Brien, Assistant Superintendent - Operations
  • L. E. Davis, Assistant Superintendent - Technical Services
  • D. E. Paquette Assistant Superintendent - Maintenance

P. Cretens, Assistant Superintendent - Work Planning and Startup

  • R. D. Kyrouac, Station Quality Assurance Superintendent
  • E. L. Martin, Station Quality Assurance Superintendent
  • P. L. Barnes, Regulatory Assurance Supervisor

R. M. Preston, Quality First Director

T. F. Hallaren, Administrative Services Director

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  • M. Takaki, Regulatory Assurance - Licensing Group
  • L. W. Raney, Supervisor Nuclear Safety Group
  • E. Wendorf, PCD Electrical Supervisor
  • R. Legner, Senior Operating Engineer

R. J. Ungeran, Operating Engineer

G. Masters, Operating Engineer

R. Yungk, Operations Engineer

F. D. Willaford, Security Administrator

T. C. Meyer, Station Fire Marshall

  • T. W. Simpkin, Regulatory Assurance - Operating Group
  • R. C. Bedford, Regulatory Assurance - Licensing Group
  • H. D. Pontius, Regulatory Assurance - Licensing Group
  • P. C. Zolan, Quality Assurance - Construction

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J. F. Phelan, Project Field Engineer

  • B. Peacock, Tech Staff
  • K. Buzek, Tech Staff
  • T. J. Lewis, Startup Staff
  • S. H. Stapp, Quality Assurance - Operation

Sargent & Lundy (S&L)

  • M. Bielman, Engineering Analyst

NRR Headquarters Personnel

  • J. Stevens, Licensing Project Manager
  • V. Benaroya, Facilities Operation Branch

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The inspectors also talked with and interviewed other licensee employees,

including members of the technical and engineering staffs, startup

engineers, reactor and auxiliary operators, shift engineers and foremen,

electrical, mechanical and instrument personnel, contract security

personnel, and construction personnel.

  • Denotes those attending one or more exit interviews conducted on

January 23, 29, February 6, and 13,1987, and informally at various

times throughout the inspection period.

2.

Licensee Action on Previously Identified Items

a.

Open Items

(Closed) 456/85015-05; 457/85016-05:

In the past, calibrated tools

or measuring devices used for electrical inspections or installa-

tions were not always recorded for specific components. An example

is the electrical penetration installations identified in violation

456/83018-06F. The licensee's electrical site contractor,

L. K. Comstock, issued Nonconformance Report (NCR) 3419 to identify

deficiencies in their calibration program. Calibrated tools or

measuring devices included in the scope of NCR 3419 were:

torque

wrenches, thermometers, dynamometers, welding machines, rod ovens,

volt amp meters, micrometers, wire crimpers, and wire strippers.

The inspector reviewed the disposition of NCR 3419, which was

closed August 16, 1986, and noted no problems. The inspector also

determined that the violation pertaining to the torquing of the

electrical penetrations was closed in Inspection Report 456/86005.

Based on the review of the disposition of NCR 3419 and the closure

of violation 456/83018-06F this item is considered closed.

(Closed) 456/85015-09; 457/85016-07:

The licensee's new Quality

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Control Inspector Reinspection Program (QCIRP) and the resolution

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of rejected items identified during original QCIRP were to be

reviewed. The original QCIRP, which was not governed by a detailed

established program, had identified numerous deficiencies during the

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reinspection to evaluate the Pittsburgh Testing Laboratory (PTL) QC

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inspectors. These original deficiencies were documented on PTL

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Nonconformance Report (NCR) 182,-Revision 3.

This NCR was closed

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on September 4, 1986. The inspector reviewed the disposition and

supporting documentation and noted no problems. The inspector,

along with an NRC Region III specialist, reviewed the revised QCIRP

which was described in; licensee's Procedure PM-11, Revision 2,

" Quality Control Inspector Reinspection." This review did not note

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any programmatic concerns. The inspector and regional specialist

reviewed the results of the QCIRP. The regional specialist reviewed

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the welding discrepancies noted during the QCIRP and found none to

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- be design significant. The resultant reductions in capacity did not-

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impact on the structural integrity of the plant in that adequate

design margins were maintained. This matter is considered closed.

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(Closed) 456/85053-03: The draft Technical Specifications did not

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identify surveillance requirements for the batteries utilized in the

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starting of the diesel driven AFW pump, IAF01PB. When this item was

identified the licensee initiated action to develop surveillance

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requirements in the plant procedures. These procedures have been

issued and define the daily, monthly, and quarterly surveillance

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requirements for these batteries.

In regards to surveillance

requirements in the Technical Specifications, it was determined by

NRR, with the inspector's concurrence, that specific surveillance

requirements for the AFW batteries were not needed in the Technical

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Specifications. However, one issue remains in regards to performing

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a specific surveillance on the AFW batteries. That issue pertains

to a need for performing a periodic discharge test on the batteries

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to evaluate their capacity.

Presently there is no regulatory

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requirement to perform a discharge test on the nickel cadmium AFW

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batteries. The licensee is evaluating the r.eed for discharge

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testing. Until such time as this' evaluation is complete, discharge

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testing of the AFW batteries will be considered an Open Item

(456/86065-01(DRP)).

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(Closed) 456/85053-04: The diesel AFW pump engine startup panel,

IAF01J, has a switch for selecting which one of the two battery

banks is utilized ter starting the diesel AFW pump. Two procedures

reviewed for lining up the AFW system for standby operation and for

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emergency operation did not adcquately address operator actuation of

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this switch to use the other battery bank in the event the diesel

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electric motor starter failed to crank,

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CECO has resolved this problem by revising the two procedures (Bw0P

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AF-7 and Bw0A ELEC-5) questioned by the NRC inspector.

Procedure

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Bw0P AF-7, Revision 52, Page 3, Item 12, approved October 9, 1986,

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and Procedure 18w0A, ELEC-5, Page 7, Item 3d, approved August 25,

1986, were each revised to prompt the operator to select the

alternate battery bank if the diesel starter motor fails to crank.

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A review of these procedure revisions indicates that the issue has

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been completely resolved; the words used to prompt the operator to

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switch from one battery bank to the other in the event of a failure

to crank are, in both cases, are clear and easily interpreted.

This

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issue is closed,

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(Closed) 456/85057-02(DRP);457/85053-01(DRP): Routine NRC safety

inspections occurring between December 1, 1985, and February 1, 1986,

disclosed a conflict between two testing procedures (BwMP 3100-037

Revision 0, and BwVS 4.2.2-1, Revision 0,. including Temporary Change

No. 044) being used to test Braidwood Unit 1 pressurizer code safety

valves. ' Procedure BwMP 3100-037 required the leak test fluid to be

nitrogen, while Procedure BwVS 4.2.2-1 required the valves to be

' leak tested using water pressurized with nitrogen. The Nuclear Work-

Request (NWR) packages clearly established that the testing of the

code safety valves should be in accordance with both Procedures BwMP

3100-037 and BwVS 4.2.2-1.

This issue was resolved by:

(1) creation of Revision 2 of Procedure BwVS 4.2.2-1 which

eliminated the conflict in leak test fluids. Nitrogen is

specified as the leak test fluid for both this procedure and

Procedure BwMP 3305-028 which replaced Procedure BwMP 3100-037.

(2) revision of Maintenance Work Request Procedure BwAP 1600-1,

Revision 10, to require the use of a two part traveler (CECO

Forms 86-5165(S),8-79,and86-5218,10-79) whenever multiple

procedures are to be used.

In addition, special training was

given to cognizant maintenance personnel to sensitize them to

the need to look for conflicts between multiple procedures and

to use the written text of the traveler package to resolve and

eliminate these conflicts.

A sample review of. CECO training records showed that a special

course was given to maintenance personnel to train them to properly

implement procedure BwAP 1600-1. A part of that training was

reported by the' Quality Control Supervisor to include the use of a

traveler to resolve questions and conflicts arising from.the use of

multiple procedures.

Based on the above, this matter is closed.

(Closed) 456/86016-03(DRP): Quality of Release to Operations (RTO)

Evaluations. Due to the magnitude of the RTO review process, the

inspector expressed concern about the assurance that this process

would be conducted in a manner consistent with that expected of

nuclear plant operations. The inspector. conducted the following

review:

Preparation for actual review of RTO packages is conducted in

accordance with the two main procedures-governing the assembly

and content of RTO packages. These were reviewed in detail.

The procedures are " Instructions for System Turnover To

Operations" (PSU-01, Revision 6) and " System Turnover for

Operation" (BwAP 1205-11, Revision 3). Based upo

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review of these documents and discussions with li.n a thorough

censee

representatives, it appears that the licensee has developed

these procedures as a result of lessons learned earlier at

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other stations.

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These procedures appear to be well thought out; however,

resulting from.this review, it is suggested that Procedure

PSU-01, Revision 6, Section 2.0 (References) refer to Procedure

BwAP 1205-11.

It is noted that Procedure PSU-01 does call out

Procedure BwAP 1205-11 on Page 4, Section 4.0, Item 9.

This

omission is not a significant problem.

For this review, it was necessary to. review the RTO packages

with these procedures in hand. Though it is not apparent at

first, the RTO packages were found to be assembled in a very

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consistent format so that a person who is familiar with this

format could quickly locate and track the sequence and

chronology of signoffs and departmental approvals for most

any system or piece of equipment within that system.

" Station Review," Section 6. for each of the following RTO

packages was reviewed first:

RC-11

Reactor Coolant Air Operated Valves and Motor

Operated Valves

AP-13

Auxiliary Power Above 480 Volts (ESF)

SI-10

Safety Injection

SI-11

Safety Injection Accumulators

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SI-12

Safety Injection - Flow Balance

The inspector conducted a systematic review and determined that

checklists had been checked off and that signatures and dates

appeared in the proper blanks of each form. The inspector also

examined each list of work that remained to be done at the time

of acceptance of the system. This review is summarized by the

table shown below.

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Page

RTO

Numbers

-Description

Package

Within

of Forms

Volume

Section

and Materials

No.

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Reviewed

RC-11

1 to 92

BwAP 1205-11T6

93 to 99

BwAP 1205-11T2

100 to 102

BwAP 1205-11T3

103

BwAP 1205-11T4

104 to 110

BwAP 1205-11T5

AP-13

1 to 54

BwAP 1205-11T6

55 to 72

BwAP 1205-11T2

73 to 74

BwAP 1205-11T3

75 to 79

BwAP 1205-11T4

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BwAP 1205-11T5

There was no 11T5 form found.

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SI-10

1 to 84

BwAP 1205-11T6

85 to 94

BwAP 1205-11T2

95 to 99

BwAP 1205-11T4

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100 to 103

BwAP 1205-11T3

SI-11

1 to 19

BwAP 1205-11T6

20 to 25

BwAP 1205-11T2.

26 to 29

BwAP 1205-11T3

30 to 35

BwAP 1205-11T4

36

BwAP 1205-11T5

SI-12

1 to

BWAP 1205-11T6

11 pages

BwAP 1205-11T2

w/o numbers

17 pages

BwAP 1205-11T3

w/o numbers

5 pages .

BwAP 1205-11T4

w/o numbers

1 page

BwAP 1205-11T5

w/o number

All questions raised were adequately answered by licensee

personnel. The next review of the same RTO packages

concentrated upon Section 8.0 which dealt with the following

five topics:

Flush Package Documentation

Initial Pump Run Documentation

Initial Compressor Run Documentation

Initial Fan Run Documentation

Balancing Reports

- Not all packages had a section on each one of the above five

topics. Some of these topics are not applicable to each RTO

package and are hence not required.

Section 8 of RC-11 covers only Topic 1 and is divided into the

three sections shown below:

Flushing procedures and Forms - pages 1-51

Flush sign-offs - pages 53-76

Flush data sheets - pages77-117

Nothing was found inconsistent or missing from reviewing these

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documents.

Section 8 of SI-10 contains only topics 1 and 2.

There is

apparently no need for a Section 8 in SI-11. The next section

reviewed was the listing of " Master Deficiencies" in Section

4.0 of RC-11.

Each of the 256 listed deficiencies is

sequentially numbered at the top of the page.

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All questions were satisfactorily answered by licensee personnel

and it appears that the RTO process was conducted in an acceptable

manner. This matter is considered closed.

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(Closed) 456/86038-04:

In the area of _ controlling loss of stored

items and materials, the licensee has established an inventory of

safety-related items that would be conducted on a two year cycle.

This appears to be a rather long period of time between planned

reviews of the inventory for determining loss of stored items and

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materials. This policy was to be reviewed by the licensee to

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determine if it was timely.

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After thoroughly reviewing the problem, the licensee sees no need

to complete the inventory cycle more often than every two years.

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Over the four year period that this two year inventory cycle of

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safety-related equipment has been in effect, no instances of loss

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of items and materials have been identified . The licensee feels

the existing system is both adequate and cost effective. Should

loss become a problem, the licensee-has agreed to again consider

the need for more frequent inventory cycles. While reviewing this

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open item, the inspector noted that:

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(1) the existing two year inventory cycle of safety-related items

and materials is not done at the end of the 24th month, but

rather on a continuous monthly basis.

Therefore, there is

the potential to detect losses on a continuous monthly basis.

(2) The seriousness of a loss of, or the immediate detection of a

loss,-is further lessened by the licensee's " Combined System

Inventory" program where they have a computer listing of spare

parts at their other neighboring power plants. These

neighboring plants have either common spare parts or have parts

that can be interchanged. The following other neighboring

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plants are able to supply stock inventory items to Braidwood

upon request in a matter of hours:

Interchangeability or

Commonality of Spare

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Plant Name

Parts Inventory

Byron

Nearly 100%

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Zion

About 60%

LaSalle

About 30%

Quad Cities

About 30%

Dresden

About 30%

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In consideration of all of the above, this item is considered

closed.

(Closed) 456/86038-06: Special electronic equipment and

instrumentation parts, such as printed circuit boards are usually

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stored in a Level "A" storage area. The licensee has these items

presently stored in a Level "B" storage area -(inside and heated).

In ' order to verify that the licensee is following the storage

-requirements for Level "A" and Level "B" storage of hardware, the

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following was done:

(1) Reviewed Procedure BwWP 800-1, Revision 1. " Levels and

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Conditions of Storage. This licensee document was reviewed

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by the inspector with particular attention to the physical

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limits'of environmental conditions for Level "A" and Level

"B" storage. This licensee document references the storage

requirements of ANSI 45.2.2-(1972),-the licensee's Quality

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Assurance Manual (QP 13-51 and QP 10-54) and Regulatory Guide

1.38, Revision 2.

No problems were noted,

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(2) Reviewed licensee documents which showed that the technical

staff has, where needed and requested, reviewed storage

requirements for components and parts to determine if Level

"A" or Level "B" storage is required. The licensee provided a

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' series of documents and notes dating back to November 23, 1983,

illustrating that they have in the past reviewed the storage.

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requirements for components or parts in accordance with

Procedure BwWP 800-1, Revision 1.

As of February 3, 1987, no

hardware was in the Level "A" storage area, but documents were

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reviewed showing that two hardware items currently on order

will be stored in the Level "A" area upon receipt. These items

were both printed circuit boards for security systems with

controlled environment shelf lives of 40 years.

Five other

documents -also describing items requiring level "A" storage,

but which are not currently stored, were also reviewed. No

problems were noted.in this review.

(3) -An inspection of the Braidwood service building Level "A"

storagearea(locatedwithintheQAvault)andtheLevel"B"-

storage area (located within the storeroom on the third floor)

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was made to see that the requirements of Procedure BwWP 800-1,

Revision 1, were being met.

The Level "A" temperature and

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humidity, recorders were inspected and found to be in operation

and were determined to be affixed with up to date calibration

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stickers. Because the Level "A" storage room contained no

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hardware at the time of the inspection, there was no require-

ment to log (on a weekly basis) the temperature and humidity

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readings on Form BwWP 800-1A2 that is part of Procedure BwWP

800-1, Revision 1.

No problems were noted in this review.

It has been determined that licensee personnel are continuing to

maintain and use separate storage areas for Levels A, B, C, and D

in accordance with ANSI Standard 45.2.2; CECO QA Manual, QP 13-51

and QP 10-54; and Regulatory Guide 1.38, Revision 2.

For equipment

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or materials where the storage level is questioned, the licensee

technical staff performs an evaluation, on a case by case basis,

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to determine the proper storage level.

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- Based on the above information, this matter is considered closed.

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(Closed) 456/86038-07:

10-CFR 50.59 specifies that annually the

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licensee shall submit to the NRC, a report containing a brief

description of any changes, tests, or experiments not described in

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the FSAR. The licensee's Technical Specification, Section 6.9.1.4

and site administrative procedures'did not include the requirement

for this annual report. Braidwood Unit 1 received it's license

to load fuel on October 17, 1986. The inspector reviewed the

licensee's General Surveillance Computer Program and noted that the

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first annual report is identified to be due October 17, 1987. This

annual reporting requirement is listed in Nuclear Stations Division

Directive.(NSDD) A01, Revision 3, dated June.2, 1986. This

directive is also cross referenced in the General Surveillance

Computer Program. This item is considered closed.

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(Closed) 456/86038-09: A routine safety inspection conducted during

August and September of 1986 concentrated upon Section 6.5.1 of the

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Braidwood Technical Specification pertaining to offsite review and

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investigation. Minor concerns were identified; however, licensee

personnel were able to correct all but one concern prior to the

exit meeting at the conclusion of the inspection. This exception

was the revision control process for the procedure manual used by

the offsite review and investigative function.- The specific concern

was that the revision number and date did not appear on each page

of the Department of Nuclear Safety Organization and Administrative

Manual.

Pending review by the NRC of the adopted review control

process, this was an open item.

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In response to this open item, the licensee has changed the revision

control process for.the procedure manual used for offsite review and

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investigation. A February 5, 1987 review of Revision 0 (dated

January 1, 1987), of the Department of Nuclear Safety Organization

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and Administration Manual showed that all five pages did have the

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revision number and date typed in the upper right corner of each

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page. This item is closed.

b.

Unresolved Items

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(Closed) 456/83016-02(DRP): While examining equipment in Braidwood

Unit 1 Containment, the NRC inspector noted that all four containment

coolers had damaged cooling fins'. The damage apparently resulted

from placement of construction scaffolding within the coolers.

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Though the fins on the cooling coils were observably damaged, it

was not possible to determine by observation whether or not related

damage had occurred to the reactor containment fan coolers (RCFC)

service water cooling coils until operational leak testing of the

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cooling coil pressure boundaries had been completed.

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This problem has been resolved by performing the steps listed below:

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(1) Construction scaffolding was removed and the work area was

cleaned. This occurred around September 18, 1984.

(2) Cooling coil nozzles were repaired and the damaged cooling fins

were repaired by straightening (combing). After repairs were

complete, temporary plywood protective covers were installed to

protect the cooling coils and fins from future damage. These

actions were completed by December 11, 1985, and are documented

by Phillips Getschow Company (PGCo) Field Change Orders (FCOs)

IVP-8013, IVP-8014, IVP-7424, and IVP-7425.

(3) Leak testing of the cooling coil pressure boundaries was

completed and no cooling coil leakage was detected. PGCo

Pressure Test Reports, No. 20,000 and No. 8335, plus 40

separate RCFC cooling coil drawings, each with signed and

dated pressure test completion and acceptance stamps,

document completion of this task; all leak testing was

complete by September 5, 1986.

A January 28, 1987 field inspection of all units except, IVP01CA,

showed the cooling units to be clean and serviceable. The access

door to unit IVP01CA was bolted shut and the unit was operating,

making inspection impossible. Based upon review of the documents

cited above and a satisfactory field inspection of the damaged

units, this issue is closed.

(0 pen)-456/85004-01(DRP);457/85004-01(DRP): Water Presence in

Containment Tendons. The licensee examined all tendons and those

with water were recorded for re-examination. By letter dated

February 2,1987, Sargent & Lundy recommended to Commonwealth Edison

that the examination be conducted with the Unit 1 containment

inservice inspection. The letter also suggested that an additional

horizontal tendon be sampled in addition to the normal sample of one

dome, one vertical, and one horizontal tendon.

If possible, the

samples will be from tendons that have shown a presence of water.

This matter will remain open for followup on the ongoing tests and

inspections.

(Closed) 456/85032-01; 457/85031-01: The inspector identified

deficiencies in the auxiliary building and requested that the

licensee evaluate the welded and bolted plate connections for

specification conformance and safety significance. The licensee

stated that nonconformance reports (NCR) mcy already exist for the

beam-angle plate installations. The licensee reviewed the specific

areas identified by the inspector in the unresolved item to address

both the welded and bolted structural connections. As a result of

this review, the structural steel site contractor, G.K. Newberg

(GKN), issued GKN NCR Number 213-1362 to identify concerns with six

,

connections.

These connections were dispositioned "Use-As-Is" for

e

four connections and " Rework" for the other two connections. Prior

'

to the issuance of this unresolved item, GKN was in the process of

mapping structural bolting and welding inspections for specification

11

.

._~

_ . _ _ .

_ _ _ ___ _ _ _ . _ _ _

._ ._

_

.-

,

..

conformance. .Therefore,'any other similar type concerns have been

identified-through this mapping process and resolved utilizing

established nonconformance procedures. While performing this

mapping process, GKN. identified that certain inspection records

could not be located. The licensee issued NCR 838 on September 2,

1986 to identify that-certain structural steel connection inspections

-were missing. During the processing of this_NCR, the licensee

identified the following causes on NCR 838 for the missing records:

E

(1)' The welded connections installed by Mid City were inspected by

Mid City with a 10% overview by Pittsburgh Testing Laboratory

(PTL). The Mid City documentation turnover may not have

included all of these inspections.

(2) The PTL field inspector documented the connections by

identifying the connections inspected on an inspection drawing.

His final inspection reports did not, in all cases, positively

identify all the connections that were inspected.

+

(3) During the September 1979 shutdown of-the Braidwood site, it!

was noted that some of the inspection drawings were misplaced.

,

These drawings were recreated from-final inspection reports.

-l

All the attributes _ inspected may not have been recreated from

the final inspection reports.

i

i

(4) Since the beams were not originally numbered by Sargent & Lundy

(S&L), each structural steel fabricator. numbered the beams.

Therefore, identical beams within a division could have the

!

same mark number.

PTL used the mark number to track their

,

I

-bolting inspections. This duplication of mark numbers within a

i

division could cause confusion as to which connection had been

i

inspected.

Based on the above, the licensee concluded that although

,

.

documentation of inspections could not be located, it was not as a

i

result of a lack of inspections and acceptance of the work

performed. The disposition of-NCR 838 was to accept "use-as-is"

i

these connections which were missing inspection records. This

disposition was reviewed by S&L in which they concurred with the

licensee's "use-as-is" recommendation. The results of S&L's review

,

I

was documented in a letter dated October 2, 1986. The basis of

j

S&L's concurrence for accepting the 1985 connections with missing

{

inspection documentation was that 54 had been reinspected under the

Quality Control Structural Steel Review (QCSSR) and 19 were

4

reinspected under the Braidwood Construction Assessment Program

(BCAP). S&L noted that none of the discrepancies identified under

the reinspection programs were of a nature or frequency to warrant

any further corrective action. S&L further stated that the

structural steel installation at Braidwood Station was found to be

.

of adequate quality. To determine the effectiveness of S&L's review

of the reinspection results noted above, an NRC Region III

specialist reviewed the 19 connections reinspected under BCAP. The

j

results reviewed were documented in the following S&L calculations:

1

4

12

1

. ,

, ,_-.-

-.

~ - - .

_,,

.-. - -.-~~ --. ---- ...

--- - ---.

- ..-

-

.

.

CSR-I-S-002-001-1

CSR-I-S-002-033-1

CSR-I-S-002-034-2

CSR-I-S-002-034-3

CSR-I-S-002-034-4

CSR-I-S-002-034-5

-CSR-I-S-002-034-6

CSR-I-S-002-037-1

CSR-I-S-002-037-2

CSR-I-S-002-041-1

CSR-I-S-002-041-2

CSR-I-S-002-041-4

CSR-I-S-002-044-1

CSR-I-S-002-044-2

CSR-I-S-002-044-3

CSR-I-S-002-044-4

CSR-I-S-002-045-1

CSR-I-S-002-051*

CSR-I-S-002-101*

CSR-I-S-002-110-1

CSR-I-S-002-141-1

CSR-I-S-002-146-2

CSR-I-S-002-147-1

CSR-I-S-002-147-2

CSR-I-S-002-152-1

CSR-I-S-002-152-2

CSR-I-S-002-153-1

CSR-I-S-002-153-3

  • No discrepancies.were identified during the reinspection.

~

The regional specialist determined that the S&L evaluations were

adequate and there were no discrepancies which would warrant further

reinspection of connections which have missing inspection

documentation. Based on the disposition of NCR 838 and the NRC

Region III Specialist's review of S&L calculations, this matter is

considered closed.

c.

Violations

(Closed) 456/85032-02:

Flexible metal hoses for instrument 1-PT-544

and 1-PT-545 had traps formed. The licensee tracked the deficiencies

with the flex hose traps on Phillips Getschow (PGCo) Nonconformance

Reports (NCR) 4388 (1-PT-544) and 5054 (1-PT-545). Also, a similar

deficiency had been identified by PGCo on the flexible hose for

1-LT-559, which was documented on PGCo NCR 5105. These NCRs have

been closed. Further corrective actions by the licensee included

the following:

For instrumentation flexible hoses (Unit 1) within the ASME

Code jurisdictional boundary, Sargent & Lundy (S&L) has

performed a walkdown under cold plant conditions. A functional

13

1

.-

,

.

review of the results of this walkdown was perfomed by S&L

and Engineering Change Notices (ECN) 27101 and 28632 were

issued to clarify flexible hose configuration acceptance.

criteria.

For instrumentation flexible hoses (Unit 1) within

the ANSI B31.1 Code jurisdictional boundary classified as

' Class H (safety-related), PGCo submitted as-built drawings to

S&L. S&L'then performed a functional review of the hoses to

determine whether reroutes were necessary. The acceptance

criteria in ECNs 27101 and 28632 were also applicable to ANSI

B31.1Property "ANSI code" (as page type) with input value "ANSI</br></br>B31.1" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., Class H, installations.

The inspector reviewed ECNs 27101 and 28632 and found the acceptance

,

criteria well defined for inspection purposes. The inspector also

'

verified that NCRs 4388, 5054, and 5105 were properly closed and

that the dispositions required the reworking of the flex hoses to

-

preclude traps.

The licensee's corrective action to avoid further violations

i

included the issuance of ECN 27101, which clarified flexible hose

configuration acceptance criteria, and developing a procedure

(PGCP-3, " Flexible Metal Hose Installation") to define actions to be

taken during hot plant conditions for collection and evaluation of

data for flexible hoses. The inspector reviewed Procedure PGCP-3,

Revision 6, and noted no problems. To determine the effectiveness

of the corrective action, the_ inspector performed a general tour of

the plant to determine if there were any instrument-flexible hoses

installed with traps. The inspector noted no problems during this

tour. Therefore, based on the implementation of the licensee's

corrective actions and the fact that the corrective action appears

effective, this item is considered closed.

(Closed) 456/85045-01(DRP);457/85044-01(DRP):

Inadequate

Corrective Actions on Housekeeping and Equipment Protection.

Between September 3 and November 1, 1985, NRC inspectors determined

that, contrary to the Commonwealth Edison Quality Assurance Manual,

corrective actions were not promptly implemented for the three

issues listed below:

(1) Correctiveactions(instructiontocontractors),inresponse

to NRC concerns over protecting systems and components from

intrusion of foreign matter, such as dust and moisture, were

insufficient and resulted in exposure of the internals of

reactor protection electrical components in the auxiliary

electrical room and control room panels to deposition of

significant dust from nearby ongoing masonry work.

(2) Numerous damaged flexible electrical cable conduits were

observed during a plant tour.

The damaged conduits exposed

the cable insulation to cuts and gashes from the sharp edges

of the conduit and also forced the cable to support the conduit.

14

_

.-

(3) An accumulation of oil was found inside the bearing

thermocouple junction box for centrifugal charging pump

1CV01PA. This caused the thermocouple cable insulation to be

immersed in oil and resulted in potential degradation of the

insulation.

In addition, this oil represented a potential

fire hazard to the pump.

The CECO response to the above. violation is documented in a

December 13, 1985 letter to NRC Region III.

The first of the three examples described above dealt with the

' failure to protect systems and components from foreign matter,

such as dust and moisture from nearby construction activities.

The licensee acknowledged.that housekeeping and equipment

protection measures were inadequate for the specific areas

described by the violation. These areas have since been

thoroughly. cleaned and vacuumed and are now not in violation of

the CECO Quality Assurance Manual.

To reduce the probability of~ recurrence of.this issue, the licensee

instructed construction contractors, on October 19, 1985, to seal

off these types of construction arens to prevent dust and dirt from

spreading to clean areas. This order had apparently not been fully

implemented.as of October 28, 1985 when the NRC inspectors verified

that nothing had been done to correct these conditions.

Further-

more, CECO's contractor personnel have been assigned on an ongoing

basis to maintain control panel cleanliness in all areas of the

plant. Additionally, openings through the control room and

auxiliary electrical equipment room ceilings from the overhead cable

spreading rooms have been equipped with temporary seals to prevent

debris from entering the panels.

Regarding the second example where numerous damaged flexible

electric cable conduits were observed, the licensee described it's

three ongoing programs to identify and repair damaged flexible

electric conduits. These three programs covered construction.

system testing, and plant area turnover phases of the project and

each identification, repair, and reinspection included specific

steps to detect and repair electric cable damage which may have

occurred incident to flexible conduit damage. Though occasional

instances of damaged flexible conduits may still be observed. CECO

felt the existing _three programs were adequate to cover the

detection and associated repair of all such deficiencies.

-

The third example was similar to the first because it involved

unwanted foreign matter found within an electrical enclosure. More

specifically, oil was detected inside a thermocouple junction box

for charging pump ICV 01PA. The referenced letter documents that oil

found within the thermocouple junction box has since been removed

and the junction box has been restored to original condition and

returned to service as of December 12, 1985.

15

4

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mad

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4

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.

4

.

-

Rece'nt observ'ations in Unit-1. indicate that housekeepong is

improving with the ongoing cleaning and painting in preparation

'

for operation. Observations in Unit 2 indicate a positive trend;

however, since it is still under construction, the concern. remains

high for system and component protection. This issue is considered

closed,

i

d.

10 CFR 50.55(e) Reportable Items

(Closed) 456/85005-EE: High Energy Line Breaks in the Auxiliary

Building. This item was previously discussed in Inspection Report

g

456/86016. The licensee has completed the necessary modifications

'

to automatically isolate the steam generator blowdown (SD) and

'

auxiliary steam system (AS) in event of a pipe rupture. The

licensee's proposed modification was reviewed by the Office of

,

'

Nuclear Reactor Regulation (NRR). This review was documented by

NRR in Safety Evaluations pertaining to the system aspects and the-

.

.

electrical aspects of the design. The results of NRR review were

'

!.

documented in a February 6, 1987 letter to the licensee. NRR

'

concluded that the SD and AS systems for protection.against

i

postulated piping failures in the auxiliary building were acceptable

and met the requirements of General Design Criterion (GVC) 4.

The

inspector verified these modifications were installed and the

'

appropriate testing was conducted. The inspector also verified that

procedures BwAR 0-31-C8, BwAR 1-15-E11, and BwAR 2-15-E11 relative

to this issue were developed, reviewed, and issued. This matter is

!

considered closed.

!

e.

Licensee Action on IE Bulletins

(Closed) 456/85001-BB; 457/85001-BB: Steam Binding of Auxiliary

1

Feedwater Pumps. Compliance for the Braidwood plant is based

upon following the lead .taken earlier by the Byron plant. This

,

review meets the requirements of Temporary Instruction TI2515/69.

The licensee's Architect-Engineering Firm, Sargent & Lundy (S&L),

reviewed IE Bulletin 85-01 relative to the Byron and Braidwood

L

plants. The S&L conclusion was that even though steam binding of

'

the AFW pumps is very unlikely because of the mechanical designs

used in these two plants, modification of operating procedures, as

,

!

suggested by the NRC, is prudent because it cannot be guaranteed

!

that steam binding will not occur. Based upon this recommendation,

the licensee's Project Engineering Department recommended that

Braidwood Station implement an operating procedure similar to Byron

!

Operating Abnormal Procedure (now B0A SEC-7, Revision 51) and

i

include a temperature check of the AFW pumps at the AF005 valves.

1

Isolation and cooldown of a loop to preclude steam binding of the

AFW pumps is initiated by either or all of the following:

(1)

If, as a result of a once per shift temperature check of valve

AF005, the temperature is observed to be greater than 130 F,

}

then Procedure Bw0A SEC-7, Revision 51 must be entered and

i

16

- - - , , - . -

.-

- . - -

- . . . . - , . - - - _ . . - . _ - . - - - - . - - - . -

,

- _ -

.

. - . -

- - -

.

.

- - - --. - - -.

4

.

4

>

...

followed. This procedure'provides the actions required to-

L

,

prevent steam binding of auxiliary feedwater pumps and.

1-

potential water hammer of auxiliary feedwater piping due to .

check valve leakage. The second step of this procedure

'

requires a check of series' downstream valve AF004 to determine

if it has a temperature of over 130 F.

If over 130 F, then

"

Step 3 initiates closure of the affected auxiliary feedwater

~

pump discharge isolation valves.

(2)

If steam vapor is released upon opening auxiliary feedwater-

,

piping high point vent (s), then Procedure Bw0A SEC-7, Revision

51 is entered and followed as described above.

.

(3) Braidwood Operating Procedure Bw0P AF-2, Revision 51 addresses

I

shutdown of the auxiliary feedwater system after its operation

to check and record the AFW pump discharge temperatures 30

minutes after the system has been secured.

If these

'

temperatures are determined to have increased since the AFW

was secured, the Shift Supervisor must be notified since the

increased temperatures are indicative of steam generator check

valve back leakage which could cause steam binding of the AFW

pumps. The Shift Supervisor will then opt to enter Procedure

Bw0A SEC-7, Revision 51 if the temperature rise is determined.

,

This item is closed.

1

(Closed) 456/86003-8B; 457/86003-88:

Potential Failure of Multiple

ECCS Pumps Due to Single Failure of Air-0perated Valve in Minimum

'

,

j

Flow Recirculation Line. By letter, dated November 14, 1986, the

licensee stated that a survey was conducted and documented by memo,

dated October 18, 1986. The safety injection system was identified

i

to have a common pump recirculation motor operated valve (ISI 8813).

This valve is required by technical specifications in Modes 1, 2,

i

and 3, to be de-energized, open, and it's position verified once per

i

shift. This bulletin is considered closed.

1

.

3.

Allegations

(Closed) RIII-86-A-0167: On October 2, 1986, the Senior Resident

1

'

Inspector (SRI) (0perations) received a concern from an individual

pertaining to the control of electrical cable. The individual stated

j

that millions of feet of electrical cable were missing and the concern

was related to prudency. The individual wrote memos to L.K. Comstock

!

(LKC) management and had not seen any corrective action. The individual

i

stated that the cable was missing from warehouses and none of the

installed cable had been removed from the plant.

The .indiv.idual further

'-

stated that this concern was identified to the licensee's Construction

Superintendent, Project Manager, and Quality First. Also, the individual

>

stated that the memos were stopped on the desk of an L.K. Comstock (LKC)

,

employee. On October 16, 1986, the individual again contacted the Senior

'

l

Resident Inspector (Operations).

In summary, the individual stated that

there were no safety problems with Braidwood construction; however, the

i

f

i

17

1

{.

.

- - - , - - - _ .

____,__.___,_.__,-,._.__..,.m._,,.._._..___

_ _ . _ _ . _.._,_._ ~.

-

-

- .

_

.

._

_ _ _ _ _

_-

.

r

-individual'had reservations.about the Quality First team. By letter,

'

dated October 21, 1986, the NRC Region III office requested the

,

licensee to conduct a review of the individual's concerns utilizing

an organization which is independent of the Construction. Superintendent,

LKC Project Manager, and Quality First. The results of this review

would then be reviewed by an inspector during a future onsite inspection.

Subsequently, the individual contacted the SRI-(Operations) on

c.

November 14, 1986 to discuss the NRC October 21, 1986 letter to the

licensee requesting a review of the individual's concern. The individual

reiterated that electrical cable was missing from storage and that the

individuci was concerned with Quality First. The individual also stated

that the Braidwood plant was built safely.

.

In a November 24, 1986 letter to Region III, the individual clarified

previous information.. The following clarifications warranted further

.

!

review by the NRC. These clarifications were:

someone was trying to cover up the report of missing cable by laying

the individual off for lack of work,

the entire package of memoranda and computer reports, which the

,

individual had given to the licensee's Project Manager, was stopped

at a LKC Manager's desk,

,

the storage requirements of cable onsite, which has nothing to do

'

with a safety concern, but under 10 CFR 50 are a valid NRC concern,

the indiv.idual never questioned, and does not now question, anything

regarding the safety or quality of the construction of Braidwood.

i

The concern was about missing cable.

4

'The results of the licensee's investigation of the individual's concerns,

-

I

were reviewed by the Senior Resident Inspector (Construction). The

licensee's investigation consisted of contacting.the individual by phone

on October 19, 30, and November 3, 1986. The licensee's investigation

was documented in a memo to the Project Manager and summarized as

follows:

There is sufficient quality control during cable installation to

assure that cable damaged during storage or damage due to improper

'

storage would be identified prior to installation.

1

.

If there were errors in reel records, traceability would not be

'

affected since traceability is established by Quality Control by

utilizing pull cards.

4

Currently existing cable inventories were deemed sufficiently

accurate to identify future cable needs based on Unit 2 completion.

The individual had no concern with Quality First or the Project

Construction Superintendent as stated during the phone conversations

of October 19 and 30, 1986.

!

l

18

_ _ .-_ _ - . _

.

. .

. .

. - . .

.

. _ _ _ _ _ . - _ . _ _ , _

.

.

The Senior Resident Inspector (SRI) (Construction) reviewed the

clarifications documented in the individual's November 24, 1986 letter to

the NRC Region III office and the results of the licensee's

investigation. The results of the review were as follows:

Individual's November 24, 1986 letter:

The individual believes that someone was trying to cover up the

a.

report of missing cable by terminating the individual for lack

of work.

Since the concern of missing cable is not a safety or quality

related matter, the individual's termination was not subject to

investigation by the inspector. The reason missing cable from

storage is not a safety or quality concern is explained in

Paragraph (d).

b.

The entire package of memos and computer reports, which were

given to the licensee's Project Construction Superintendent was

stopped at an LKC Manager's desk.

The inspector reviewed a memo, dated March 3, 1986, from LKC's

Project Administrator to distribution within LKC. This memo

was distributed to LKC's Project Management and Engineering

organizations. This memo requested that these organizations

review a handwritten memo received by the licensee's Project

Construction Superintendent pertaining to recommendations in

tracking cable inventory. This memo appeared to be written by

the alleger. A handwritten note in the margin, written by the

licensee's Project Construction Superintendent, requested LKC

management to review the handwritten memo's recommendation

which pertained to cable inventory. Based on the review of

this documentation the inspector could not substantiate this

portion of the allegation.

The storage requirements of cable onsite, which has nothing to

c.

do with a safety concern, but under 10 CFR 50 are a valid

Concern.

The inspector determined that the storage requirements for

cable reels is "outside." This type of storage is known as

" Level D."

Level D storage is an acceptable storage level for

cable reels.

In addition, it is a requirement for Quality

Control inspectors to inspect cable for damage prior to

installation.

Based on this inspection requirement and the

fact that the cable reels are allowed to be stored outdoors,

the inspector has no concerns in the method of storage of cable

reels at Braidwood.

In regards to manufacturer supplied cable,

the inspector does not have a concern with storage since this

type of cable is shipped and stored in either a drum or on

pallets.

A small quantity of cable was furnished by equipment

manufacturers.

This type of cable is also required to be

inspected for damage by Quality Control prior to installation.

19

I

.

.

d.

The individual never questioned, and does not now question,

anything regarding the safety or quality of the construction of

Braidwood. The concern was about missing cable.

It appears from the November 24, 1986 clarification that the

individual was aware that missing cable is not a safety or

quality concern. The inspector concurs with the individual for

the following reasons:

(1) All cable is procured " safety-related." Therefore, any

missing cable turning up later in construction phase and

installed would still have the appropriate test reports

substantiating its quality.

(2) The storage requirements for cable reels are those defined

for " Level D" storage. There are four levels of storage;

A, B, C, and D.

Level A has the most stringent storage

requirements (inside with temperature and humidity

control) and Level D has the least requirement (outside).

Therefore, if cable reels were missing from the assigned

storage area (Level D) the cable reels would then be

stored in a storage area that was equivalent (Level D) or

better (Level A, 8, or C).

Summary of Licensee's Investigation

.

a.

There are quality control inspections during cable installation

to assure that cable damaged during storage would be identified

prior to installation.

The inspector concurs with the licensee's conclusion. LKC

procedures require that cable be inspected for damage prior to

installation.

b.

If there were errors in cable reel records, traceability could

not be affected since traceability is established by Quality

Control by utilizing pull cards.

The inspector concurs with the licensee's conclusion. Cable

pull cards, which are required for every safety-related cable

pull, identify the source of the cable. Also, since all cable

, .is procured " safety-related," a receipt inspection of the cable

is performed. This receipt inspection includes a verification

that there are test records traceable to the cable reel being

received.

c.

Currently existing cable inventories were deemed sufficiently

accurate to identify future cable needs based on Unit 2

completion.

The inspector did not review this portion of the licensee's

investigation since the inventory of cable is not a quality or

safety concern.

20

.

.

.

d.

The individual had no concern with Quality First as stated

during a telephone conversation of October 19 and 30, 1986.

The inspector reviewed the documentation in the licensee's

Quality First file generated for the individual's concern.

Since missing cable is not a safety or quality concern, Quality

First actions of having the licensee's Project Construction

Department investigate the individual's concern was deemed

appropriate by the inspector.

e.

The individual's concern about the storage for cable reels is

not a safety concern since the acceptable storage for cable

reels is outside (Level D).

The inspector concurs with the licensee's conclusion. See

Paragraph (C) under the previous section of this report titled

" Individual's November 24, 1986 letter."

Based on the results of reviews documented above, the inspector concludes

that there are no safety concerns associated with this allegation and the

actions taken by the licensee appeared appropriate. Therefore, this

allegation is considered closed.

(Closed)RIII-86-A-0199: On December 22, 1986, the Senior Resident

Inspector (SRI) Operations was contacted by two Quality Control (QC)

inspectors from General Electric-MCIS with a concern that due to a

labor / management dispute, their inspections were being impaired. These

two QC inspectors were performing inspections for the site electrical

contractor, L.K. Comstock (LKC). These QC inspectors stated that the

labor / management dispute pertained to the overtime and absenteeism

policies. As a result of being frustrated or upset with the labor /

management dispute, the QC inspectors stated that one of them tore

up quality documents and the other did not properly carry out a rejcction

form for a motor operated valve (MOV). On December 23, 1986, the SRI

(Operations) had contact with the licensee's Construction Superintendent.

During this contact the SRI (Operations) informed the Construction

Superintendent of the potential concern expressed by the two QC

inspectors. The Construction Superintendent stated that he had been

unaware of any safety-related implications associated with the

labor / management dispute. The Construction Superintendent had previously

contacted the Resident Inspector (Operations) on December 22, 1986 to

brief the NRC on the labor / management dispute between the QC inspectors

and General Electric-MCIS.

Subsequent to the telephone contact with the SRI (Operations) on

December 23, 1986, the Construction Superintendent directed the LKC QC

Manager to meet with the inspectors. The purpose of this meeting was

to inform the inspectors that if any of them felt the current labor /

management situation was affecting their ability to do quality work

they should identify themselves. This meeting was convened in the

afternoon on December 23, 1986. The inspectors were instructed that if

1

they did not want to disclose themselves at the meeting that it could be

done at their convenience in a more private manner.

This meeting was

21

_

_

..

.

documented in a memo to file from the LKC QC Manager. This memo stated

there was no response from any individual either after the meeting or

in-private.

To determine if the labor / management dispute was affecting the work

performance of other QC inspectors the SRI (Construction) interviewed

nine QC inspectors and one document reviewer. .The following is a list

of the interviewee's certifications and experience:

Individual

Experience

Certifications

  1. 1

1 year at Braidwood

Level II in Weldinc

,

Configuration, anc

Concrete

Anchors

4 years at Clinton

in weld inspection

and Quality

  1. 2

2 years QC at

Level II in Welding,

Braidwood

Configuration Termination,

and Cable Pulling

6 years at Byron

,

  1. 3

31/2 years QC at

Level II in Weldinc

,

Braidwood

Configuration, anc

Receipt

Inspection

  1. 4

3 years QC at

Level II in Recei)t

j

Braidwood

Inspection, Cali3 ration,

Termination, and Cable

Pulling

  1. 5

Document Reviewer

,

  1. 6

3 years 10 months

Level II in Cable Pulling,

!

QC at Braidwood

Conduit, and Cable

Tennination

  1. 7

1 year QC at

Level II in Termination

l

Braidwood

Previous experience

l

at Millstone III

,

  1. 8

3 years QC at

Level II in Cable Pulling

Braidwood

and Conduit

  1. 9

1 year 10 months

Level II Welding and

at Braidwood

Configuration

..# 10

2 years at Braidwood

Level II Conduit, Welding

and Configuration

'

22

.

.

The following are the questions asked each individual and a summary of

their answers:

a.

Was each individual aware of the meeting convened on the afternoon

of December 23, 1986 by the LKC QC Manager?

All the individuals stated they were aware of this meeting and noted

no one coming forward with a concern that the labor / management was

affecting the quality of their work.

b.

Did they have any knowledge of any ins)ector's work being impaired

due to the labor / management dispute?

or example, were they aware

of any inspector destroying quality documents or failing to identify

deficiencies on the appropriate nonconforming documents?

None of the inspectors heard of or knew of any inspectors that had

their inspections impaired due to the labor / management dispute.

Also, none of the inspectors interviewed knew of any inspector who

destroyed quality documents or failed to identify nonconformances,

c.

At the present time, are there any inspectors who are still upset to

a point where their inspections are being impaired?

All of the inspectors stated they had no knowledge or knew of any

inspector whose inspections were being impaired. They had no

knowledge that any inspectors were presently destroying quality

documents or failing to document deficiencies.

In addition to interviewing randomly selected QC inspectors, the SRI

(Construction) interviewed the two QC inspectors who contacted the

SRI (Operations) on December 22, 1986. The following is a summary

of the interviews:

Individual "A"

This individual stated that he had torn up four draft Inspection

Correction Reports (ICRs) as a result of being frustrated with

the work policies pertaining to overtime and absenteeism.

Specifically, tearing up these draft ICRs was a result of

learning that an individual had been terminated for missing one

hour of work due to illness. This individual stated that the

ICRs that were torn up had not yet been given an ICR number

(logged). These draft ICRs were written as a result of a

partial Area Turnover Inspection he had performed, but had

later been replaced by another inspector. The area he had

inspected was reinspected by the other inspector. The

individual stated the four draft ICRs he had written were given

to the inspector who was assigned to complete the area turnover

inspection. The individual stated that the four draft ICRs he

had written identified the following deficiencies:

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Two ICRs for segregation labels.

One ICR for torquing on a strap.

One ICR for a loose bushing.

- The SRI (Construction) interviewed the QC inspector who had

been assigned to finish the individual's area turnover

inspection. This individual stated that he had been given

the four ICRs from individual "A" and that these ICRs were

rewritten and issued during his area turnover inspection. The

SRI (Construction) reviewed a computer printout of all the ICRs

issued during the area turnover inspection and determined that

the deficiencies identified by individual "A" were adequately

addressed. The individual further stated that the tearing up

of the four draft ICRs was the only time he did anything of

that nature.

Individual "B"

This individual stated that he had been frustrated with the

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labor / management dispute. When an individual was terminated

for missing one hour of work, he became very frustrated. This

frustration caused him to not write an ICR for a deficiency

that he noted in a MOV during a December 19, 1986 inspection.

The deficiency was a nick in a wire.

The individual stated

that after the December 23, 1986 meeting with the LKC QC

Manager, he initiated an ICR for the nicked wire. He could not

remember the ICR Number, but believed it was written for a MOV

associated with a Unit 2 essential service water valve.

The SRI (Construction) reviewed the ICR log at LKC and could

not find that an ICR was issued for a nicked wire in a MOV in

the time frame consistent with facts described by individual

"B".

The SRI (Construction) contacted individual "B" by

telephone on February 10 and 11, 1987 to discuss this anomaly.

Individual "B" stated he would review the LKC ICR log and

determine which ICR was issued by him to document the nicked

wire in the M0V. On February 10, 1987, individual "B"

contacted the Resident Inspector office. He gave the ICR

number in question to the SRI (Construction). The SRI

(Construction) contacted the LKC Assistant QC Manager and

asked him what was the subject of the ICR and when was it

issued. The LKC Assistant QC Manager stated that the ICR was

dated on December 19, 1986, and it pertained to a damaged

conductor and a loose flex connection with no identification.

This ICR pertained to valve ICV 084 located in the auxiliary

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building on the 364' elevation. The individual stated his

failure to document the deficiency for the MOV was the only

time he had acted in that manner.

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Based on the interviews of other QC inspectors, the SRI (Construction)

could not substantiate that the labor management dispute between the

QC inspectors and GE-MCIS impaired the inspection process.

The SRI

(Construction) evaluated the actions of the two QC inspectors pertaining

to the tearing up of ICRs and the failure to identify a deficiency in

the MOV. The SRI (Construction) confirmed the following:

a.

The ICRs that were torn up had not yet been logged.

In fact, these

" draft" ICRs were given to an inspector who had been reassigned to

the Area Turnover Inspection. The deficiencies noted on the " draft"

ICRs were subsequently addressed by ICRs issued during the Area

Turnover Inspection,

b.

The deficiency in the MOV was later identified on an ICR by the QC

inspector who failed to initially identify it on an ICR. This QC

inspector issued the ICR after the LKC QC Manager's meeting of

December 23, 1986.

The SRI (Construction) reviewed this ICR and

determined that this ICR addressed a nicked wire in an M0V. The SRI

(Construction) contacted the individual and asked him why the ICR

was dated December 19, 1986, when he earlier had stated that he

wrote the ICR after a December 23, 1986 meeting. The individual

stated that he performed the inspection on the M0V on December 19,

1986. Therefore, when he wrote the ICR on December 23, 1986, he

,

dated the ICR with the date of the inspection, December 19, 1986.

Based on the review of this ICR's content, the SRI (Construction)

has determined that this ICR was written for the deficiency in the

M0V, which had not been previously identified.

This allegation is closed.

No violations or deviations were identified.

4.

Regional Request

By memo, dated January 30, 1987, Region III, Division of Reactor

Projects, requested a summary of the licensee's actions on planned

action in response to IE Information Notice 86-106, "Feedwater Line

Break," relative to the catastrophic failure at Surry Power Station.

The questions asked and responses were:

a.

Question

For PWRs and DWRs, identify which licensees have and which

licensees have not prepe. red programs to determine whether their

large-diameter steam, feedwater, condensate, and connected system

piping is subject to thinning of the piping wall.

Response

Presently there are two procedures in place to test for thinning

in cross-under steam lines and MSR reheat lines:

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'BwVS 210-1, Rev. O, " Ultrasonic Thickness Measurement of

Extraction Steam Piping"

BwVS 210-2, Rev. O, " Examination of Cross-under Piping"

These procedures will be carried out during the refueling outages.

Prior to the Surry event, and in addition to the above procedures,

the licensee was in the process of developing a list of potential

pipe erosion points in the feedwater, heater drains, extraction

steam, and the steam generator blowdown piping. Since the Surry

event, the licensee has added consideration of main steam,

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condensate booster, and auxiliary feedwater piping.

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b.

Question

Piping for those systems is subject to wall thinnirg if the

following conditions exist:

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(1) Carbon steel fittings and spools.

(2) Fittings less than 10 pipe diameters apart.

(3) Bulk flow greater than 10 feet per second.

(4) Fluid temperature between 195'F and 440*F.

(5) 0xygen concentration less than 600 ppb.

Determine whether licensee's have included these factors in their

programs.

If other factors have been included, identify them.

Response

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The conditions for considering wall thinning are all of those in

the memo and in addition, the licensee considers high moisture

steam and 90* bends.

. c.

Question

Determine how many measurements will be taken and where they will

be taken.

Response

Presently specific locations for examinations are stated in the

two procedures listed in item above.

BwVS 250-1 identifies four extraction steam pipes with three

components on each pipe. The types of components are cold

reheat extraction tees, 90' elbows, reducers, and a reducer /

tee.

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BwVS 250-2' identified 25 locations for internal visual and UT -

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examinations of piping between the HP. turbine and the MSR,

and consists of 90' bends, diaphrages, 90* bend / ext, and

extractions.

Prior to the Surry event, the licasses wat.considering.three

additionalfeedwaterpipes.Ageheaterdrains,oneextraction

steam line, the steam genWatd

blowdown lines. These vary from

[

one to eight locations for examination on each line.

Commonwealth Edison has developed a corporate (SNED) task force to

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review this issue.

Dresden, Quad, and Zion are being appropriately

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reviewed first due to their age. LaSalle, Byron, and Braidwood will

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follow.

The licensee is using at least the following as a guide line:

EPRI, NP3944, Project 2231-2, Final Report April 1985

" Erosion / Corrosion in Nuclear Plant Steam Piping: Causes

and Inspection Program Guidelines"

INP0 list using Industry Procedures July 10, 1986. An INPO

.

Good Practice is expected in the future.

Westinghouse - guidelines,

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d.

Question

If measurements have been taken, provide the results.

Response

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No measurements have been taken at Braidwood.

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It is recognized that Braidwood is a preoperational PWR and pipe wall

thinning has not had the urgency associated with older plants.

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This information was forwarded to Region III on February 2,1987, and

will be further forwarded to NRC Headquarters for a " National Survey

on the Licensee's Actions Regarding Thinning of Secondary Piping."

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No violations or deviations were identified.

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S.

Licensee Event Reports (LER) Review

Through direct observations, discussions with licensee personnel, and

review of records, the following event report was reviewed to determine

that reportability requirements were fulfilled, immediate corrective

action was accomplished, and corrective action to prevent recurrence had

been accomplished in accordance with technical specifications:

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(Closed) 456/86002-00-L: All Action Requirements of Tech Specs

Not Met While Both Source Range Channels Were Inoperable.

Upon

discovery of missed valve position verification, two SRO's were

dispatched to verify the position. Long tenn followup will be to

have all associated personnel review this LER.

(Closed)456/86003-00-L:

Inoperable Hard Rubber Fire Hoses Due to

Couplings Separating from the Hoses.

Several of the hoses failed

the hydrostatic test. The licensee is replacing the hoses with

properly certified hoses. The personnel involved are being trained

to prevent recurrence.

(Closed) 456/86004-00-L:

Steam Generator Low-Low Level Results in

Reactor Trip Due to Misadjusted Valve. The trip signal resulted

from secondary leakage through leaking blowdown valves while the

steam generator was in wet layup recirculation. A foreman walked

down the system for verification and a locking device was placed on

the throttle valve.

(Closed) 456/86005-00-L:

Containment Purge Isolation From a Voltage

Transient Caused by Construction Activity. The licensee has

provided instruction to construction personnel working in sensitive

areas.

(Closed) 456/86006-00-L:

Failure to Follow Action Statement

3.3.3.10 on Failure of 1RT-PR028. The licensee provided training

to operating department personnel on this subject.

(Closed) 456/86007-00-L: Temporary Procedure Change Not Reviewed

Within 14 Days Due to Unclear Steps in Procedure. The licensee has

issued a temporary procedure change to BwAP 1300-3, " Preparation

and Approval of Temporary Procedures and' Temporary Changes to the

Permanent Procedures," and has initiated a permanent procedure

change to follow.

(Closed) 456/86008-00-L:

Failure to Comply With Technical

Specification Action Statement Due to Cognitive Personnel Errors.

The individuals involved in this event were counselled and the event

will be covered in routine training of other individuals.

(Closed) 456/86009-00-L: Diesel Generators Declared Inoperable Due

to Incorrect Design of Emergency Mode Circuitry. This was

identified to the licensee through the 10 CFR 21 reporting system.

A temporary modification was put in place to bypass the unqualified

switches.

In addition, a permanent modification will be processed

to bypass the electrical over-speed trip on an emergency start

signal.

(Closed) 456/86010-00-L: Reactor Trip Caused by Damage to Source

Range Cable Due to Personnel Error.

This reactor trip was caused

when a contractor working in an instrument cabinet bumped an

electric cable against a support strut causing the cable to be

nicked and shorted. The cable has been repaired and the sharp edge

on the strut removed.

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(Closed) 456/86011-00 and 01-L:

Containment Ventilation Isolation

Due to Spurious Signal.

Although it could not be. proven, the

licensee suspects this was caused by construction activities in

the vicinity of the radiation monitoring cabinet.

A valid isolation

signal could not be identified and all related valves were in closed

positions at the time of the signal.

A letter was issued to the

contractor management personnel re-emphasizing the need for greater

awareness during this phase of the plant life.

(Closed) 456/87001-00-L:

Failure to Take Required Gas Sample

With the H2 and 02 Analyzers Inoperable Due to Personnel Error.

The licensee installed a moisture separator filter in the

hydrogen-oxygen gas sampler line, recalibrated the analyzers and

held discussions with operating personnel.

In addition, the event

significance was small in that no hydrogen was in the Volume Control

Tank (VCT) at the time of the event.

(Closed) 456/87002-00-L:

Containment Ventilation Isolation Train A

Due to Loss of Power to a Radiation Monitor.

ESF Bus 141 breaker

tripped which resulted in loss of power to the area radiation

monitor 1RE-AR011.

Loss of power to the radiation monitor initiates

the containment ventilation isolation.

The breaker trip probably

was caused by contractor personnel working in area.

A letter

addressing the issue was written to contract personnel concerning

work activity problems.

Licensee failed to report this item within

the required time specified by 10 CFR 50.72.

This violation

(456/86065-02(DRP))isaddressedinParagraph6.

(Closed) 456/87003-00-L:

Containment Ventilation Isolation Signal

Due to Loss of Pulses from 1RE-AR012.

The licensee replaced the

detector which appears to have corrected the problem.

(Closed) 456/87004-00-L:

Train A Containment Ventilation Isolation

- Trainee Actuated.

During a training walk through, the trainee

tripped the 480 volt feed breaker to MCC 131X2.

The tripped breaker

interrupted power to 1RT-AR011, which initiated a Train A

Containment Isolation. The personnel involved were briefed to

prevent recurrence.

The preceding LERs have been reviewed against the criteria of 10 CFR 2,

Appendix C, and when the incidents described meet all of the following

requirements, no Notice of Violation is normally issued for that item.

a.

The event was identified by the licensee.

b.

The event was an incident that, according to the current enforcement

policy, met the criteria for Severity levels IV or V violations,

c.

The event was appropriately reported.

The event was or will be corrected (including) measures to prevent

d.

recurrence within a reasonable amount of time .

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The event was not a violation that could have been prevented by the

e.

licensee's corrective actions for a previous violation.

In addition to the foregoing, the inspector reviewed all of the

licensee's Deviation Reports (DVRs) generated during the inspection

period. This was done in an effort to monitor the conditions related

to plant or personnel performance, potential trends, etc.

It was also

reviewed for assurance that DVRs were generated appropriately and

dispositioned in a manner consistent with the applicable procedures

and the QA manual.

No violations or deviations were identified.

6.

Onsite Followup of Events Occurring During the Inspection

On two separate occasions, the licensee failed to promptly notify the

NRC Operations Center via the Emergency Notification System (ENS)

within the required time limit specified by 10 CFR 50.72(b)(2)(ii),

10 CFR 50.72(b)(2)(ii) requires an ENS notification within four hours

of the occurrence of any event or condition that results in manual or

automatic of any Engineered Safety Feature (ESF) including the Reactor

Protection System (RPS). Details of the two occasions in which the ENS

notifications were not within the required time limit are as follows:

On January 29, 1987, at approximately 2245, operations personnel

de-energized the Nuclear Instrumentation (NI) panel which resulted

in receipt of several RPS actuations. The NIs were de-energized to

preclude damaging the NI circuits due to a water leaking into the

control room from the upper cable spreading room. The water source

originated from painting activities which resulted in water backing

up into an area directly above the control room which drained thru

floor penetrations into the control room due to floor drainage

system blockage. The RPS actuation was not reported until 1611 on

January 30, 1987, which is beyond the four hours reporting require-

ments. The other occurrence happened on January 7, 1987 at 1127

at which time an ESF actuation (containment ventilation isolation)

occurred. The ESF actuation was due to a loss of power to the

1RE-AR011 radiation monitor which resulted from ESF Bus 141

de-energization. The actuation was not reported until approximately

1600 on January 7, 1987. These failures to make the required ENS

notifications within the required time limit is considered a

violation of 10 CFR 50.72 (b)(2)(ii) (456/86065-02(DRP)).

The Region III Branch Chief responsible for Braidwood and the resident

inspectors met with Braidwood management on February 5, 1987 to discuss

the immediate notification requirements of 10 CFR 50.72(b)(2)(ii).

It

was emphasized that NRC expects that the makeup of RPS or ESF initiation

logics be promptly reported even if reactor trip breakers did not actuate

because the breakers were already open, and even if the ESF equipment

did not actually start.

It was also emphasized that for the ESF or RPS

actuation to be part of a preplanned sequence, the sequence of events

resulting in the actuation must be preplanned from beginning to end.

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Loss of Component Cooling

On January 21, 1986, at 1745, the licensee experienced a complete loss

of Unit I component cooling (CC). The event occurred during a "B" train

outage and resulted from attempting to drain the CC side of the "B"

residual heat removal (RHR) heat exchanger (Hx) and the inlet. valve

leaking sufficiently to cause the event. The sequence of events led to a

lowering of the CC surge tank level to cause the "A" CC pump to trip and

the "B" CC pump to start and trip resulting in the loss of CC. At the

time, the plant was in cold shutdown (Mode 5) and the licensee was

conducting work activities that would lead to higher modes and initial

criticality. The inspectors have performed a preliminary review of the

licer.see's followup investigation and preliminary corrective actions and

found them to be acceptable.

This matter will be given a final review when the Licensee Event Report

is submitted to the NRC.

7.

Operational Safety Verification

The inspectors conducted routine plant tours during the inspection

period to make an independent assessment of equipment conditions, plant

conditions, construction activities, security, fire protection, general /

personnel safety, housekeeping, and adherence to applicable regulatory

requirements. During the tours, the inspectors reviewed various logs,

daily orders, interviewed personnel, attended shift briefings and plan

of the day meetings, witnessed various construction work activities, and

independently determined equipment status.

During the shift changes,

the inspector observed operator and shift engiaeer turnovers and panel

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walkdowns.

Throughout the entire inspection period, Unit I remained in Mode 5 (cold

shutdown). The inspectors verified that all applicable requirements for

Unit I were met during this period which included periodic checks of the

locked valves for boron dilution prevention as required by the licensee.

These reviews and observations were conducted to verify that facility

operations were in conformance with the requirements established under

technical specifications, 10 CFR, and administrative procedures.

While on a routine tour of the plant the inspectors discovered that the

mini flow manual isolation valve for the IB charging pump was not secure.

This valve is one that has been designated to be locked open.

The

condition found was that the handwheel nut was missing which allowed

removal of the handwheel with the lock and chain attached. This left

the valve in an unlocked condition.

In addition, the handwheel nut for

the 1A mini flow valve for the charging pump was loose, such that the

handwheel could be removed rendering the valve into an unlocked

condition. Subsequent to the above inspection activity the inspectors

identified two five protection (FP) header isolation valves that were of

concern. On one of the valves, the chain and lock was placed such that

at a distance it appeared locked, but closer inspection (moving of the

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tee) showed it was unlocked. The other valve had the chain and lock'

attached to the tee bar. The tee.bar was not attached to the valve,

which allowed removal of the tee bar rendering the valve unlocked.

This is considered an unresolved item (456/86065-03(DRP)).

,

No violations or deviations were identified.

f

8.

Unit 2 Plant Tour

The inspector observed work activities in progress, completed work and

plant conditions during general inspections in Unit 2 work areas.

Observation of work included cable trays, junction boxes, pipe support

welding and mechanical equipment. Particular. attention was given to

material identification, nonconforming material identification and

housekeeping. The inspector reviewed work activities by reviewing

travelers while touring the plant. These travelers pertained to

electrical, piping, and hanger installation.

No violations or deviations were identified.

9.

Report Review

During the inspection period, the inspector reviewed the licensee's

Monthly Operating Reports for November and December 1986. The inspector

confirmed that the information provided met the requirements of Technical Specification 6.9.1.8 and Regulatory Guide 1.16.

In addition, the

inspector' reviewed the licensee initiated changes to the Offsite Dose

Calculation Manual (ODCM) submitted as Attachments 1 and 2 to the December

report that was provided in accordance with Technical Specification 6.14.

The inspector also reviewed the licensee's Monthly Plant Status Reports

for October, November, and December 1986.

No violations or deviations were identified.

10. Meetings, Training, and Other Activities

Plant Status Meeting

A meeting was held on December 16, 1986 and January 23, 1987, between the

CECO Project Manager, the Region III Project Director, and members of

each of their staffs. The purpose of the meetings was for the licensee

to provide an update on the status of Units 1 and 2.

The meetings were

also an opportunity to discuss the licensee's list of items that must be

dispositioned prior to a mode change in Unit 1.

11. Open Items

Open items are matters which have been discussed with the licensee, which

will be reviewed by the inspector and which involve some action on the

part of the NRC or licensee or both. An open item disclosed during the

inspection is discussed in Paragraph 2(a).

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12. Unresolved Items

Unresolved items are matters about which more information is required

in order to ascertain whether they are acceptable items, violations,

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or deviations. An unresolved item disclosed during the inspection is

discussed in Paragraph 6.

13. Exit Interview

The inspector met with licensee and contractor representatives denoted

in Paragraph I during and at the conclusion of the inspection on

February 13, 1987. The inspector summarized the scope and results of

the inspection and discussed the likely content of this inspection

report. The licensee acknowledged the information and did not indicate

that any of the information disclosed during the inspection could be

considered proprietary in nature.

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