ML20205B129
| ML20205B129 | |
| Person / Time | |
|---|---|
| Site: | Callaway |
| Issue date: | 01/31/1987 |
| From: | Pratte D UNION ELECTRIC CO. |
| To: | |
| Shared Package | |
| ML20205B123 | List: |
| References | |
| NUDOCS 8703270553 | |
| Download: ML20205B129 (4) | |
Text
.e; DOCITT NO.
50-483
' UNIT NAME-
'CALLAWAY UNIT 1
-DATE.
2/12/87 COMPLETED BY D. B. PRAITE TELEPHONE 314/676-8460 PART A OPERATIONS SIDt!ARY The plant operated at full. power throughout the month with the exception of a forced shutdown for 25.7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> on 1/30/87 to investigate and repair RCS leakage (less than Tech Spec limits) on RCS Loop 1 hot leg RTD 2A outlet downstream isolation valve.. Additionally, there were two load reductions as reported in part E of this report.
PART B PORV AND SAFETY VALVE SLMtARY None CA-#804 04/10/85 QDP-ZZ-04204 070327055387021kS3 M M 05000 PDR
n-Part C AVERAGE DAILY UNIT POWER LEVEL
~
DOCKET NO...
50-483
~
JUNIT NAME CALLAWAY UNIT 1 DATE 2/12/87 COMPLETED BY D. B. PRATTE TELEPHONE 314/676-8460 MONTH:
JANUARY 1987 AVERACE DAILY POWER LEVEL AVERAGE DAILY POWER LEVEL.
DAY (PWe-Net)
DAY (NNe-Net) 1:
1079 17 1094
'2 1081 18 1099 3
'1082 19 1108 4
1081 20 1111 5
1088 21 1109 6
1100 22 1109 7
1107-12 3 1109 1
8
'1106 24 1110 9
1014 25 1110 10 1102 26 1105 11 1108 27 1106 12 1103 28 1106 t
13
-1030 29 1015 14-770 30 0
15 771 31 241 16 1058 CA-#804 04/10/85 QDP-ZZ-04204 Page 2 of 4
q c-t U'
PhrtD OPERATINC DATA REPORT DOCKET NO.
50-483 UNIT NAME CALLAWAY UNIT 1 DATE 2/12/87 COMPLETED BY D. B. PRATTE..
TELEPHONE
-314/676-8460
' OPERATING STATUS ~
~(YTD-CUM ).
-1.
REPORTING PERIOD: January 1987
' GROSS HOURS IN' REPORTING PERIODe~ 744 (744 18566.5):
2.- CURRENTLY AUTHORIZED POWER LEVEL (MWt):
3411 MAX. DEPEND. CAPACITY (MWe-Net):
1120 DESIGN ELECTRICAL RATING (MWe-Net):
1171*
' *At stretch power level which is not currently authorized under the Operating License.
- 3. - POWER LEVEL TO WHICH RESTRICTED (IF ANY) (MWe-Net):.100%
4 REASONS FOR RESTRICTION ~ (IF ANY):
THIS MONTH YR I0 DATE CUMULATIVE 5.
NUMBER OF HOURS REACIOR WAS CRITICAL...............
722.2 722.2 16,492.3 6.
REACTOR RESERVE SHUTDOWN HOURS.....................
0 0
0 7.
HOURS GENERATOR ON LINE............................
718.3 718.3 16,030.2 8.'
UNIT RESERVE SHUTDOWN HOURS........................
0 0
0 9.
GROSS THERMAL ENERGY GENERATED (MWH)...............
2,310,037 2,310,037 50,879,932
- 10. GROSS ELECTRICAL ENERGY GENERATED (MWH)............
785,327 785,327 17,178,465 11.
NET ELECTRICAL ENERGY GENERATED (MWH)..............
749,098 749,098 16,316,998
- 12. REACIOR SERVICE FACIOR.............................
97.1%
97.1%
88.8%
- 13. REACTOR AVAILABILITY FACIUR........................
97.1%
97.1%
88.8%
- 14. UNIT SERVICE FACTOR................................
96.5%
96.5%
86.3%
- 15. UNIT AVAILABILITY FACTOR...........................
96.5%
96.5%
86.3%
- 16. UNIT CAPACITY FACTOR (Using MDC)...................
89.9%
89.9%
78.5%
- 17. UNIT CAPACITY FACTOR (Using Design MWe)............
86.0%
86.0%
75.1%
- 18. UNIT FORCED OUTAGE RATE............................
3.5%
3.5%
4.8%
- 19. SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE, AND DURATION OF EACH):
37 day planned maintenance outage starting April 4,1987.
-20.
IF SHUI DOWN AT END OF REPORTING PERIOD, ESTIMATED DATE OF STARTUP:
CA-#804 l
04/10/85 QDP-ZZ-04204 l
Page 3 of 4 u
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__..m~~~
.. ~ ~ -
-m
- ~ -
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~ '
4,.e w-Part E
'L INIT SHUTDOWNS AND POWER RE UCTIONS-DOCKET 180 50-483
.INIT NAME
' Call.AWAY UNIT 1 DAIT 2/12/87 COMPLETED BY D. B. PRATTE TELEPHONE 314/676-8460-REPORT MONTH: JANUARY 1987 PETHOD OF TYPE SHUTTING DOWN F: mRCED DURATION
- THE REACIOR OR DATE S: SCHEDULED (HOURS)
REASON REDUCING POWER CORRECTIVE ACTIONS / COP 9ENTS 1.
1/9/87 F
0 A
1 Ioad reduction for 4.3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> to repair Main Feed Pump oil leak.
2.
1/13/87 F
0 A
1 Load reduction for 51 hours5.902778e-4 days <br />0.0142 hours <br />8.43254e-5 weeks <br />1.94055e-5 months <br /> to repair Main Feed Pump suction. flange leak.
3.
1/30/87 F
25.7 A
1-Plant shut down to investigate and repair RCS Ieakage (less than Tech Spec limits) on RCS Loop 1 hot leg RID 2A outlet downstream isolation valve.
SUMMARY
REASON PETHOD l
A: EQUIPPENI FAILURE (EXPLAIN) 1: MANUAL B: MAINT, OR TEST 2: MANUAL SCRAM C: REKELING
-3: AUTOMATIC SCRAM t
D: REGULATORY RESTRICTION 4: OTHER (EXPLAIN)
E: OPERATOR TRAINING AND LICENSE EXAMINATION F: ADMINISTRATIVE C: OPERATIONAL ERROR (EXPLAIN)
CA-#804 H: OTIER (EXPLAIN) 04/10/85' QDP-ZZ-04204 Page 4 of 4
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