ML20203E393
| ML20203E393 | |
| Person / Time | |
|---|---|
| Site: | Haddam Neck File:Connecticut Yankee Atomic Power Co icon.png |
| Issue date: | 12/01/1997 |
| From: | Conte R NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | Feigenbaum T NORTHEAST UTILITIES SERVICE CO. |
| References | |
| 50-213-97-03, 50-213-97-3, NUDOCS 9712170049 | |
| Download: ML20203E393 (3) | |
See also: IR 05000213/1997003
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December 1,1997
Mr. Ted C. Feigenbaum
Executive Vice President and Chief Nuclear Officer
Northeast Utilities Service Company
clo R. A. Mellor, Director
Site Operations and Decommissioning
Connecticut Yankee Atomic Power Company
362 Injun Hollow Road
East Hampton, CT 06424-3099
SUBJECT:
NRC INTEGRATED INSPECTION REPORT 50 213/97-03, NOTICE OF
VIOLATION, AND EXERCISE OF ENFORCEMENT DISCRETION
Dear Mr. Feigenbaum:
This letter refers to your November 9,1997 correspondence, in response to our October 9,
1997 letter.
Thank you for informing us of the corrective and preventive actions documented in your letter.
These actions will be examined during a future inspection of your licensed program.
Your cooperation with us is appreciated.
Sincerely,
Original Signed By:
Richard J. Conte, Chief
Projects Branch 8
Division of Reactor Projects
Docket No. 50-213
ac: w/o cv of Licensee's Response Letted
B. D. Kenyon, President - Nuclear Graup
D. M. Goebel Vice President - Nuclear Oversight
D. B. Amerine, Vice President - Nuclear Engineering and Support
F. C. Rothen, Vice President - Work Services
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R. Johannes, Director - Nuclear Training
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L. M. Cuoco, Senior Nuclear Counsel
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G. P. van Noordennen, Manager, Nuclear Licensing
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J. F. Smith, Manager, Operator Training
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9712170049 971201
ADOCK 05000213
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Mr. Ted C. Feigenbaum
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cc: w/cv of Licensee's Resoonse LetLqr
R. Bassilakis, Citizens Awareness Netwerk
J. M. Block, Attorney for CAN
J. P. Brooks, CT Attorney Generals Office
M. DeBold, Town of Haddam
W. Meinert, Nuclear Engineer
State of Connecticut SLO
Distribution w/cv of Licenste Resoonse letter
Region i Docke'. Room (with concurrences)
Nuclear Safety information Center (NSIC)
PUBLIC
NRC Resident inspector
R. Conte, DRP
M. Conner, DRP
C. O'Daniell, DRP
K. Kennedy, OEDO
S. Weiss, NRR, DRPM, PDND
M. Callahan, OCA
W. Travers, SPO
R. Correia, NRR
F. Talbot, NRR
D. Screnci, PAO, ORA
DOCDESK
Inspection Program Branch, NRR (IPAS)
DOCUMENT NAME: G:\\ BRANCH 7\\REPLYLTR\\HN-RPY.FRM
To receive a copy of this document. Indicate in the boa: 'C' = Copy without attachment /enclosurs
- E' = Copy with attachment / enclosure
'N' = No copy
' OFFICE
Hl/DRPAg
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NAME
RContV[/ I
DATt:
//Q97
//97
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OFFICIAL RECORD COPY
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CONNECTICUT YANKEE
ATOMIC POWER COMPANY
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HADDAM NECK PLANT
362 INJUN HOLLOW ROAD = EAST HAMPTON, CT 06424-3099
November 7,1997
DockeWp. 50-2_13
Re: 10CFR2.201
U.S. Nuclear Regulatory Commission
Attention: Document Control Desk
Washington, D.C. 20555
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Haddam Neck Plant
Reply to a Notice of Violation (NOV)
NRC Integrated Inspection Reoort No. 50-213/97-03
In a letter dated October 9,1997,m the NRC staff transmitted a report documenting the
results of an NRC inspection which was completed on July 7,1997 at the Connecticut
Yankee Atomic Power Corr.pany (CYAPCO), Haddam Neck Plant (HNP) and the results of a
teleconference and final exit summary between CYAPCO and the NRC staff
on August 5,1997. Areas reviewed by the NRC during this time period include engineering,
maintenance, decommissioning activities, and operations.
As noted in the report, at the final exit meeting, CYAPCO was given the choice to discuss
certain significant violations identified in this inspection at an enforcement conference.
Based upon the results of the inspection, the NRC Staff did not believe that an enforcement
conference was necessary in order to reach an enforcement decision. CYAPCO concurred
in this regard. In summary the violations were:
1. Failure to take timely corrective action from August 1996 to March 1997 on the potential
for water hammer on the service water supply to the spent fuel pool cooling system.
(1)
H. J. Miller (NRC) to T. C. Feigenbaum (CYAPCO), "NRC Integrated Inspection
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Report No. 50-13/97-03, Notice of Violation and Exercise of Enforcement
Discretion' dated October 9,1997.
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U. S. Nuctsar Regulatory Commission
CY-97-115/Page 3 :
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' The third violation concerns an inadequate safety evaluation which was performed to allow -
operator compensatory actions for feedwater regulating valves. As stated in Reference 1,
the NRC has decided not to issue a Notice of Violation or propose a civil penalty for this.
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-issue. The NRC rendered this decision because the violation was based upean events prior
to the plant being shutdown, and the fact that significant enforcement action had already
been imposed as documented in reference 2, for the technical and safety review program
inadequacies that led to this and other violations.
CYAPCO acknowledges the issues surrounding violation riumber 3 and has revised the
safety review program inadequacies that led to this violation.
The revised program
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incorporates many of the suggested improvements of NEl 96-07
" Guidelines for
10CFR50.59 Safety Evaluations" and draft NUREG-1606 " Proposed Regulatory Guidelines
Related to implementation of 10CFR50.59."
A review of the revised program was
conducted by the NRC staff as noted in Inspection Report 50-213/97-03 and the program
was' found to be acceptable.
CYAPCO consioers these vieNions very serious and is committed to implement- and
complete the corrective actions to improve station pedormance. We will continue to keep
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the NRC Staff informed of our progress in these areas.
Attachment 2 presents CYAPCO's commitments made within this letter and the
attachments. Other statements within this letter are provided for information only.
If there are any questions regarding this submittal, please contact Mr. G. P. van Noordennen
at (860) 267-3938.
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Very truly yours,
CONNECTICUT YANKEE ATOMIC POWER COMPANY
B
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ellor
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For
T. C. Feigenbaum
Executive Vice President and
Chief Nuclear Officer
Attachments
cc:
. H. J. Miller, NRC Region i Administrator
M. B. Fairtile, NRC Senior Project Manager, Haddam Neck Plant
-W. J. Raymond, NRC Senior Resident inspector, Haddam Neck Plant
D. Galloway, Acting Director, CT DEP Monitoring and Radiation Division
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Docket Number 50-213
Attachment 1
Haddam Neck Plant
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Reply to a Notice of Violation
NRC Inspection Report No. 50-213/97-03
November 1997
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U. S. Nucint Regulatory Commission -
CY-97-115/ Attachment 1/Page 1-
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Restatement of Violation
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During NRC inspections conducted on April 8 - August 5,- 1997, violations of NRC
requirements were identified. In accordance with the " General Statement of Policy and
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Procedure for NRC Enforcement Actions," (60 FR 34381; June 30,1995) the violations
are listed below.
10 CFR 50 Appendix B, Criterion XVI, " Corrective Actions," requires that measures be
established to assure that conditions adverse to quality are promptly identified and
corrected. In the case of significant conditions adverse to quality, the measures shall
assure that.the cause of the condition is determined and corrective action taken to
preclude repetition.
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1. Contrary to the above, from August 14,1996 to March 11,1997, the licensee did not
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assure that a significant condition adverse to quality was promptly corrected.
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Specifically, the licensee was notified by a consulting engineering firm report TM-
1788a, dated August 14,1996 that potential water hammer in the SW cooling lines to
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the SFP system could occur following a loss of normal power event, and that the
operability of the SW supply lines, and thus the SFP cooling system, could not be
assured contrary to Technical Specification 3.9.15.1.icensee actions to address this
issue were neither timely or effective until March 11,1997, when a design change was
developed to correct the desiga discrepancy and the matter was reported to the NRC.
(01013)
2. Contrary to the above, as of May 21,1997, the licensee did not assure that the cause
of a significant condition adver'se to quality was determined and that corrective actions
precluded repetition. Specifically, on November 27,1996, an operator failed to follow
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procedure PMP 9.1-31 which resulted in the operation of emergency diesel EG-2B
with the Jacking tool installed but no engine damage resulted. The licensee response
to this significant condition adverse to quality was neither timely nor thorough to
resolve the cause and preclude repetition (personnel errors and/or procedure
noncompliance). On May 21,1997, an operator again failed to follow procedure PMP
9.1-31, which resulted in the operation of ernergency diesel EG-2A with the Jacking
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toolinstalled and damage to the engine. (01023)
These violations have been categorized in the aggregate as a Severity Level lli problem
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CY-97-115/ Attachment 1/Page 2
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Reasons For The Violation
The SWS violation pertained to the discovery of a design discrepancy in the SWS,
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creating the potential for postulated water hammer eveus, which could have affected the
operability of the cooling water supply to the spent fuel pool cooling system following
certain design basis accidents.
This issue was identified in a technical report which was prepared by a Creare Inc. and
issued in August 1996. The design engineering supervisor who received the Creare Inc.
report failed to initiate an Adverse Condition Report (ACR) documenting the required
actions necessa"/ to address the SWS operability concerns. In December 1996, the
design engineering supervisor accepted a new position in the Northeast Utilities system.
. Transfer of work assignments to another engineer could not be verified.
An NRC
inspection in March of 1997 brought the SWS concems documented in the Creare Inc.
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- repoit forward. A design change was instituted in March of 1997.
The cause of this violation was a personnel error with respect to taking timely corrective
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actions to address the operability and reportability aspects of this matter when the
technical issue was first identified in August of 1996. A secondary cause was the failure
of the cognizant engineer, prior to re-assignment, to properly inform the new engineering
manager of the SWS issue.
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The Emergency Diesel Generator (EDG) violation pertains to the operation of the EDG in
May of 1997, with the jacking toolinstalled. This violation represents a repeat of a similar
incident which occurred in November of 1996. The cause of this violation was the failure
to take timely and adequate actions to address a personnel error and procedura
nonadherence from the initial November 1996 event. The operator involved in the
November 1996 event, had been distracted by a call which caused him to leave the
generator during performance of this task. Management inappropriately accepted this as
the cause and did not require a root cause investigation. Following the occurrence of the
May 1997 event, a root cause investigation was conducted and as recommended in the
associated report, a mechanical stop was added to the jacking tool to preclude closure of
the diesel flywheel housing cover with the jacking tool installed.
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Corrective Steps That Have Been Taken And The Results Achieved
Corrective actions which have been taken to address the HNP failure to aggressively
pursue problem resolution and identify root causes in a timely and efficient manner are
identified below. In addition, corrective actions to reduce human performance errors
before and during decommissioning, and corrective actions taken to ensure the adequacy
- of staff " turnover" controls are also identified below.
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U. S. Nuclear Regulatory Commission
CY-97-115/ Attachment 1/Page 3
Etrict Proca. dure ComplianGn
Site-wide and department standards have been issued that include strict procedure
compliance and increased management standards. All site personnel attended meetings
conducted by the Unit Director expressly for the purpose of reiterating management's
expectations relative to strict procedure compliance and error reduction.
All site
personnel are held accountable for improving upon past procedure compliance shortfalls.
Baducing_ Human PerfoImanCILEEf9fa
A trending and monitoring program has been implemented. Key Performance Indicators
(KPis) are reviewed. Trends which include personnel errors and procedure adherence
are monitorea and reviewed by plant management on a weekly basis. Quarterly KPI and
ACR's trend results are reviewed and analyzed for declining performance. After a second
quarter trend report showed an increase in human performance errors, a common cause
report was prepared.
This report recommended the following four actions to minimize personnel errors.
Lessons learned from the common cause analysis should be presented to all plant
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management with a special seminar to be held for all supervisors. It is noted that
management has been briefed with respect to the results documented in the common
cause report.
The use of the STAR (Stop, Think, Act, Review) process should be emphasized as a
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self checking tool in the lessons learned seminar to reduce personnel errors.
The common cause, lessons learned should be used in the work observation program
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to look for, and potentially prevent, personnel errors.
The common cause and contributing factors should be trended for the third and fourth
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quarters in order to monitor the effectiveness of the corrective action program.
Those corrective steps that have already been implemented to address the issue of
personnel errors have had a positive effect in reducing the total number of personnel
errors as evidenced by third quarter trends which shows a decrease from the second
quarter. Also the fact that a positive cultural change has emerged on site, i. e., people
willing to self identify problems and share information and potential fixes, verses people
who kept information as privileged, is also attributable to the current trend status.
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U. S. Nuclear Regulatory Commission
CY-97-115/ Attachment 1/Page 4
Timely Corrective Actions
- A new, more effective Adverse Condition Report (ACR) process and new ACR database
have been developed and implemented. To ensure thi.t adverse conditions are identified
-and captured in the ACR process, management has conducted all hands training which
began in June of 1997, Through this training program, management expressed the need
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to initiate low threshold ACRs for plant problems, Since completion of the training, there
has been a significant increase in the number of ACRs initiated by plant personnel. This
heightened awareness by CY personnel coupled with the corrective action program
initiatives greatly enhances the probability of being aware of site issues requiring
corrective action. The new ACR process is structured to facilitate data gathering activities
in the following areas:
Tracking of corrective actions.
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Evaluating effectiveness of corrective actions (monitoring and trending).
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Providing guidance and training on initiation of adverse condition reports.
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. - Using KPis to monitor and trend corrective action effectiveness.
The causal factor coding provides the mechanism by which data can be categorized and
evaluated in order to facilitate recognition of programmatic or recurring causes and
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thereby readily allows for the assessment of the effectiveness of corrective actions.
Improved staff Turnover Controls
With respect to the issue of corrective actions taken to ensure the adequacy of staff
"tumover" controls, such that safety and quality issues are not compromised by being
inadvertently " dropped" or not acted upon, it is noted that a CY administrative procedure
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has been issued to address this concem. This procedure forma!izes a process presently
used by some departments.
Implementation of this procedure ensures that those
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individuals " moving" from current positions, to other positions either inside or outside of
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the CY organization, properly and systematically " turnover" their respective work
assignments to their reliefs or supervisors in " face to face meetings. This will ensure the
continuity of ongoing work assignments and commitments are maintained. Turnover
procedure, process effectiveness, will be assured by the Nuclear Oversight Group.
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Corrective Steps That Will Be Taken To Avoid Further Violations
The following corrective steps will be taken to avoid further violations.
Lessons teamed from the common cause analysis will be presented to all plant
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management with a special seminar to be held for all supervisors. The supervisors
seminar, conducted by management, addressing the results of the common cause
report is scheduled for November 1997.
The STAR process will be emphasized in the special seminar as a self checking tool
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to reduce personnel errors.
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U. S. Nucletr Regulatory Commission
CY-97-115/ Attachment 1/Page 5
he. common cause lessons leamed will be integrated into the- work observation
program to look for, and potendally. prevent, personnel errors. New work observation
forms will be issued in November 1997. -
The common cause'and contritating.factom are trended each quarter in order to
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monitor the effectiveness of the cocective action progc . Trending is performed in a
manner consistent with that performed for the first three quarters.
A team is
assembled under the direction of the CY Engineering Director to perform the common
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cause analysis. The total number of ACR's generated during the affected period are
divided amongst the team members with each member initiating a causal factor
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evaluation for each ACR. : After the causal factors are determined for each ACR, an
analysis of the common contributing factor is made and corrective actions for the most
prevalent contributing factors is recommended.
Date When Full Compliance Will Be Achieved
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The _ corrective action program has been' implemented as stated in letters
from T. C. Feigenbaum to the NRC dated June 11,1997* and September 30,1997.W
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Effectiveness reviews are ongoing with results being communicated to management and
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staff. The administrative procedure pertaining to "tumover" control has been approved for
use on-site. Management _will conduct a " supervisors seminar" in November,1997
expressly for the purpose of communicating the results of the common cause report.
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New work observation forms will be issued in November 1997, The corrective actions will
be completed by November 30,1997.
(3)
' C. Feigenbaum letter to the U. S. Nutar Regulatory Commission, " Reply to a
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Notice of Violation (NOV) Inspections 50-213/95-27, 96-06, 96-07, 96-08, 96-11,
96-80 & 96-201" dated June 11,1997
(4)
T. C. Feigenbaum letter to the U. S. Nuclear Regulatory Commission,
" Commitment Update," dated September 30,1997.
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Docket Number 50-213
Attachment 2
Haddam Neck Plant
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CYAPCO C,mmitments
NRC Inspection Rep
No. 50-213/97-03
November 1997
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CY-97-115/ Attachment 2/Page 1
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The following are-CYAPCO's commitments made within this letter and i;tachments.
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Other statements within this letter are provided for information only.
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CY-97-115-01
Lessons learned from the common cause analysis will be presented
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Io plant management with a special seminar to be held for all
. supervisors. The supervisors seminar is scheduled for November,
1997.
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CY-97-115-02
The STAR process will be emphasized in the special seminar as a -
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self checking tool to reduce prsonnel errors.
CY-97-115-03 -
The common cause, lessons learned will be integrated into the work
observation program to look for, and potentially prevent, persunnel
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errors.
CY-97-115-04
New work observation forms will be issued in November 1997
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CY-97-115-05
Turnover procedure process effectiveness will be assured by the
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Nuclear Oversight Group.
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